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    BLTouch stuck at 1000

    Scheduled Pinned Locked Moved
    Tuning and tweaking
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Use a multimeter to test continuity of the wires themselves.

      Z-Bot CoreXY Build | Thingiverse Profile

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      • dc42undefined
        dc42 administrators @Messiahman
        last edited by

        @messiahman you can test the Duet and your configuration by disconnecting the white wire and connecting that input on the Duet to ground. That should make the reading go to 0.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

        Messiahmanundefined 1 Reply Last reply Reply Quote 1
        • Messiahmanundefined
          Messiahman @dc42
          last edited by

          @dc42 that didn't work

          dc42undefined 1 Reply Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators @Messiahman
            last edited by

            @messiahman please post your config.g file and post a photo of the wiring connecting the BLTouch to the Duet.

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            Messiahmanundefined 1 Reply Last reply Reply Quote 0
            • Messiahmanundefined
              Messiahman @dc42
              last edited by

              @dc42 will do, but i did just unplug the whole bltouch to try and dispel any charge in the capacitor and replugged it all in, and now it won't deploy or retract.

              ; Configuration file for Duet WiFi (firmware version 3)
              ; executed by the firmware on start-up
              ;
              ; generated by RepRapFirmware Configuration Tool v3.3.3 on Wed Oct 06 2021 12:37:23 GMT-0400 (Eastern Daylight Time)

              ; General preferences
              G90 ; send absolute coordinates...
              M83 ; ...but relative extruder moves
              M550 P"The Print-inator" ; set printer name
              M918 P1 E4 F2000000 ; configure direct-connect display

              ; Network
              M552 S1 ; enable network
              M586 P0 S1 ; enable HTTP
              M586 P1 S0 ; disable FTP
              M586 P2 S0 ; disable Telnet

              ; Drives
              M569 P0 S0 ; physical drive 0 goes backwards
              M569 P1 S0 ; physical drive 1 goes backwards
              M569 P2 S0 ; physical drive 2 goes backwards
              M569 P3 S1 ; physical drive 3 goes forwards
              M584 X0 Y1 Z2 E3 ; set drive mapping
              M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
              M92 X80.00 Y80.00 Z400.00 E136.79 ; set steps per mm
              M566 X1200.00 Y1200.00 Z24.00 E300.00 ; set maximum instantaneous speed changes (mm/min)
              M203 X9000.00 Y9000.00 Z180.00 E6000.00 ; set maximum speeds (mm/min)
              M201 X500.00 Y500.00 Z100.00 E5000.00 ; set accelerations (mm/s^2)
              M906 X800 Y800 Z800 E1000 I50 ; set motor currents (mA) and motor idle factor in per cent
              M84 S30 ; Set idle timeout

              ; Axis Limits
              M208 X0 Y0 Z0 S1 ; set axis minima
              M208 X235 Y235 Z260 S0 ; set axis maxima

              ; Endstops
              M574 X2 S1 P"xstop" ; configure active-high endstop for high end on X via pin xstop
              M574 Y2 S1 P"ystop" ; configure active-high endstop for high end on Y via pin ystop
              M574 Z1 S2 ; configure Z-probe endstop for low end on Z

              ; Z-Probe
              M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch
              M558 P9 C"^zprobe.in" H3 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
              G31 P500 X40.00 Y5.0 Z1.250 ; set Z probe trigger value, offset and trigger height
              M557 X40:220 Y25:220 S41 ; define mesh grid

              ; Heaters
              M308 S0 P"bedtemp" Y"thermistor" T100000 B4092 ; configure sensor 0 as thermistor on pin bedtemp
              M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
              M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
              M140 H0 ; map heated bed to heater 0
              M143 H0 S150 ; set temperature limit for heater 0 to 150C
              M308 S1 P"e0temp" Y"thermistor" T100000 B4092 ; configure sensor 1 as thermistor on pin e0temp
              M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
              M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
              M143 H1 S275 ; set temperature limit for heater 1 to 275C

              ; Fans
              M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
              M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
              M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
              M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on
              M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency
              M106 P2 S1 H1:0 T45 ; set fan 2 value. Thermostatic control is turned on

              ; Tools
              M563 P0 D0 H1 F0 ; define tool 0
              G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
              G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

              ; Custom settings are not defined

              ; Miscellaneous
              M501 ; load saved parameters from non-volatile memory
              M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @Messiahman
                last edited by

                @messiahman said in BLTouch stuck at 1000:

                and now it won't deploy or retract.

                Does it light up at all? The plug at the BLTouch end is very delicate.

                Z-Bot CoreXY Build | Thingiverse Profile

                Messiahmanundefined 1 Reply Last reply Reply Quote 0
                • Messiahmanundefined
                  Messiahman @Phaedrux
                  last edited by

                  @phaedrux the red light comes on yes, but not the blue. it also goes through the startup sequence

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                  • wieman01undefined
                    wieman01
                    last edited by wieman01

                    Could you also post the contents of "deployprobe.g" and "retractprobe.g" please? There is a chance that's the source of your problem.

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                    • wieman01undefined
                      wieman01
                      last edited by

                      The reason why I am asking is this:

                      When you are issuing either M401 or M402 your BL's pin should move down or retract. If it does not, then either these files are missing altogether or they are referring to the wrong servo pin number.

                      M950 S0 C"exp.heater3"
                      

                      The contents of deployprobe.g should look like this based upon your config.g (P0 = S0 = pin number):

                      M280 P0 S10 
                      

                      And second your retractprobe.g would be:

                      M280 P0 S90
                      

                      Issue single M401 and M402 to see if your BL responds.

                      Messiahmanundefined 1 Reply Last reply Reply Quote 0
                      • Messiahmanundefined
                        Messiahman @wieman01
                        last edited by

                        @wieman01 I haven't changed them since i first got them working, but sure, let me pull them up

                        M280 P0 S10 I1; deploy BLTouch

                        M280 P0 S90 I1; retract BLTouch

                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator @Messiahman
                          last edited by

                          @messiahman said in BLTouch stuck at 1000:

                          I1

                          Remove those as they aren't used in RRF3 to invert. That's done in the pin definition now. Though it won't stop it from working.

                          I think you have a cabling issue. Can you show a photo of where the wires are plugged in both at the board and the probe? Can you test connecting the probe directly to the board with it's short pig tail wires to remove your extension wires from the equation?

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • wieman01undefined
                            wieman01
                            last edited by

                            Also let us know what BL version you have got. Depending upon the version you may need different cabling (including a resistor, etc.). You find the version number on the back of the device.

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