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    BLTouch stuck at 1000

    Scheduled Pinned Locked Moved
    Tuning and tweaking
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    • Messiahmanundefined
      Messiahman @rjenkinsgb
      last edited by

      @rjenkinsgb yeah no the entire extruder head is nearly to the top of the print area cuz my last print ended off pretty high up

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      • dc42undefined
        dc42 administrators @Messiahman
        last edited by

        @messiahman if the reading is 1000 when the pin is extended, most likely there is a break in the signal connection. On a genuine BLTouch this is usually the white wire.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

        Messiahmanundefined 1 Reply Last reply Reply Quote 0
        • Messiahmanundefined
          Messiahman @dc42
          last edited by

          @dc42 I've checked all the wires, theyre all pretty strong connections

          dc42undefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            Use a multimeter to test continuity of the wires themselves.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • dc42undefined
              dc42 administrators @Messiahman
              last edited by

              @messiahman you can test the Duet and your configuration by disconnecting the white wire and connecting that input on the Duet to ground. That should make the reading go to 0.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

              Messiahmanundefined 1 Reply Last reply Reply Quote 1
              • Messiahmanundefined
                Messiahman @dc42
                last edited by

                @dc42 that didn't work

                dc42undefined 1 Reply Last reply Reply Quote 0
                • dc42undefined
                  dc42 administrators @Messiahman
                  last edited by

                  @messiahman please post your config.g file and post a photo of the wiring connecting the BLTouch to the Duet.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  Messiahmanundefined 1 Reply Last reply Reply Quote 0
                  • Messiahmanundefined
                    Messiahman @dc42
                    last edited by

                    @dc42 will do, but i did just unplug the whole bltouch to try and dispel any charge in the capacitor and replugged it all in, and now it won't deploy or retract.

                    ; Configuration file for Duet WiFi (firmware version 3)
                    ; executed by the firmware on start-up
                    ;
                    ; generated by RepRapFirmware Configuration Tool v3.3.3 on Wed Oct 06 2021 12:37:23 GMT-0400 (Eastern Daylight Time)

                    ; General preferences
                    G90 ; send absolute coordinates...
                    M83 ; ...but relative extruder moves
                    M550 P"The Print-inator" ; set printer name
                    M918 P1 E4 F2000000 ; configure direct-connect display

                    ; Network
                    M552 S1 ; enable network
                    M586 P0 S1 ; enable HTTP
                    M586 P1 S0 ; disable FTP
                    M586 P2 S0 ; disable Telnet

                    ; Drives
                    M569 P0 S0 ; physical drive 0 goes backwards
                    M569 P1 S0 ; physical drive 1 goes backwards
                    M569 P2 S0 ; physical drive 2 goes backwards
                    M569 P3 S1 ; physical drive 3 goes forwards
                    M584 X0 Y1 Z2 E3 ; set drive mapping
                    M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                    M92 X80.00 Y80.00 Z400.00 E136.79 ; set steps per mm
                    M566 X1200.00 Y1200.00 Z24.00 E300.00 ; set maximum instantaneous speed changes (mm/min)
                    M203 X9000.00 Y9000.00 Z180.00 E6000.00 ; set maximum speeds (mm/min)
                    M201 X500.00 Y500.00 Z100.00 E5000.00 ; set accelerations (mm/s^2)
                    M906 X800 Y800 Z800 E1000 I50 ; set motor currents (mA) and motor idle factor in per cent
                    M84 S30 ; Set idle timeout

                    ; Axis Limits
                    M208 X0 Y0 Z0 S1 ; set axis minima
                    M208 X235 Y235 Z260 S0 ; set axis maxima

                    ; Endstops
                    M574 X2 S1 P"xstop" ; configure active-high endstop for high end on X via pin xstop
                    M574 Y2 S1 P"ystop" ; configure active-high endstop for high end on Y via pin ystop
                    M574 Z1 S2 ; configure Z-probe endstop for low end on Z

                    ; Z-Probe
                    M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch
                    M558 P9 C"^zprobe.in" H3 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
                    G31 P500 X40.00 Y5.0 Z1.250 ; set Z probe trigger value, offset and trigger height
                    M557 X40:220 Y25:220 S41 ; define mesh grid

                    ; Heaters
                    M308 S0 P"bedtemp" Y"thermistor" T100000 B4092 ; configure sensor 0 as thermistor on pin bedtemp
                    M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                    M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
                    M140 H0 ; map heated bed to heater 0
                    M143 H0 S150 ; set temperature limit for heater 0 to 150C
                    M308 S1 P"e0temp" Y"thermistor" T100000 B4092 ; configure sensor 1 as thermistor on pin e0temp
                    M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                    M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                    M143 H1 S275 ; set temperature limit for heater 1 to 275C

                    ; Fans
                    M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
                    M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
                    M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                    M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on
                    M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency
                    M106 P2 S1 H1:0 T45 ; set fan 2 value. Thermostatic control is turned on

                    ; Tools
                    M563 P0 D0 H1 F0 ; define tool 0
                    G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                    G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

                    ; Custom settings are not defined

                    ; Miscellaneous
                    M501 ; load saved parameters from non-volatile memory
                    M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss

                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @Messiahman
                      last edited by

                      @messiahman said in BLTouch stuck at 1000:

                      and now it won't deploy or retract.

                      Does it light up at all? The plug at the BLTouch end is very delicate.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Messiahmanundefined 1 Reply Last reply Reply Quote 0
                      • Messiahmanundefined
                        Messiahman @Phaedrux
                        last edited by

                        @phaedrux the red light comes on yes, but not the blue. it also goes through the startup sequence

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                        • wieman01undefined
                          wieman01
                          last edited by wieman01

                          Could you also post the contents of "deployprobe.g" and "retractprobe.g" please? There is a chance that's the source of your problem.

                          1 Reply Last reply Reply Quote 1
                          • wieman01undefined
                            wieman01
                            last edited by

                            The reason why I am asking is this:

                            When you are issuing either M401 or M402 your BL's pin should move down or retract. If it does not, then either these files are missing altogether or they are referring to the wrong servo pin number.

                            M950 S0 C"exp.heater3"
                            

                            The contents of deployprobe.g should look like this based upon your config.g (P0 = S0 = pin number):

                            M280 P0 S10 
                            

                            And second your retractprobe.g would be:

                            M280 P0 S90
                            

                            Issue single M401 and M402 to see if your BL responds.

                            Messiahmanundefined 1 Reply Last reply Reply Quote 0
                            • Messiahmanundefined
                              Messiahman @wieman01
                              last edited by

                              @wieman01 I haven't changed them since i first got them working, but sure, let me pull them up

                              M280 P0 S10 I1; deploy BLTouch

                              M280 P0 S90 I1; retract BLTouch

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                              • Phaedruxundefined
                                Phaedrux Moderator @Messiahman
                                last edited by

                                @messiahman said in BLTouch stuck at 1000:

                                I1

                                Remove those as they aren't used in RRF3 to invert. That's done in the pin definition now. Though it won't stop it from working.

                                I think you have a cabling issue. Can you show a photo of where the wires are plugged in both at the board and the probe? Can you test connecting the probe directly to the board with it's short pig tail wires to remove your extension wires from the equation?

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • wieman01undefined
                                  wieman01
                                  last edited by

                                  Also let us know what BL version you have got. Depending upon the version you may need different cabling (including a resistor, etc.). You find the version number on the back of the device.

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