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Duet 3 fails to start print

Scheduled Pinned Locked Moved Solved
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  • undefined
    Phaedrux Moderator @Phaedrux
    last edited by 10 Mar 2022, 18:16

    @phaedrux said in Duet 3 fails to start print:

    access the service logs from this particular unit by running journalctl -u duetcontrolserver -e. This will output the latest logs

    Were you able to gather this?

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 1 Reply Last reply 10 Mar 2022, 18:22 Reply Quote 0
    • undefined
      michaelr123 @Phaedrux
      last edited by 10 Mar 2022, 18:22

      @phaedrux

      yes here it is, had to login to the pi and send this. It looks like there is a line about the spi connection right before the system spits out some info about the heaters. Maybe that is a result of the config override having M307 code in it and its just reporting some info on the H0 and H1 heaters. The other interesting thing is that I didn't add or tune H0. H0 is so that I can have a thermistor on the bed which is an AC heater. I just create the channel so I can monitor it. At the moment I just let it heat to max temperature (around 45C) without any PWM or bang-bang control going to the SSR.

      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] Environment initialized
      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] Connection to Duet establis
      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] IPC socket created at /run/
      Mar 10 12:09:25 Duet3 systemd[1]: Started Duet Control Server.
      Mar 10 12:09:26 Duet3 DuetControlServer[447]: [info] Starting macro file config.
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: [error] Failed to open 0:/sys/fila
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: System.IO.FileNotFoundException
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: File name: '/opt/dsf/sd/sys/filame
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at Microsoft.Win32.SafeHandles.
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at Microsoft.Win32.SafeHandles.
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.Strategies.OSFileS
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.Strategies.FileStr
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.FileStream..ctor(S
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at DuetControlServer.SPI.Interf
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file config-
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [warn] M307: Heater 0 predicted ma
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [warn] M307: Heater 1 predicted ma
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file config-
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file tpre0.g
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file tpre0.g
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file tpost0.
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file tpost0.
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file config.
      lines 7-29/29 (END)
      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] Environment initialized
      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] Connection to Duet established
      Mar 10 12:09:25 Duet3 DuetControlServer[447]: [info] IPC socket created at /run/dsf/dcs.sock
      Mar 10 12:09:25 Duet3 systemd[1]: Started Duet Control Server.
      Mar 10 12:09:26 Duet3 DuetControlServer[447]: [info] Starting macro file config.g on channel Trigger
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: [error] Failed to open 0:/sys/filaments.csv for reading
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: System.IO.FileNotFoundException: Could not find file '/opt/dsf/sd/sys/filaments.csv'.
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: File name: '/opt/dsf/sd/sys/filaments.csv'
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at Microsoft.Win32.SafeHandles.SafeFileHandle.Open(String path, OpenFlags flags, Int32 mode)
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at Microsoft.Win32.SafeHandles.SafeFileHandle.Open(String fullPath, FileMode mode, FileAccess access, FileShare share, FileOptions options, Int64 preallocationSize)
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.Strategies.OSFileStreamStrategy..ctor(String path, FileMode mode, FileAccess access, FileShare share, FileOptions options, Int64 preallocationSize)
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.Strategies.FileStreamHelpers.ChooseStrategy(FileStream fileStream, String path, FileMode mode, FileAccess access, FileShare share, Int32 bufferSize, FileOptions options, Int64
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at System.IO.FileStream..ctor(String path, FileMode mode)
      Mar 10 12:09:28 Duet3 DuetControlServer[447]: at DuetControlServer.SPI.Interface.HandleOpenFile() in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/SPI/Interface.cs:line 1434
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file config-override.g on channel Trigger
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [warn] M307: Heater 0 predicted maximum temperature at full power is 114°C
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [warn] M307: Heater 1 predicted maximum temperature at full power is 507°C
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file config-override.g
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file tpre0.g on channel Trigger
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file tpre0.g
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Starting macro file tpost0.g on channel Trigger
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file tpost0.g
      Mar 10 12:09:29 Duet3 DuetControlServer[447]: [info] Finished macro file config.g

      1 Reply Last reply Reply Quote 0
      • undefined
        Phaedrux Moderator
        last edited by 10 Mar 2022, 18:50

        Can you perform this loop back test?

        https://github.com/Duet3D/DuetSoftwareFramework/wiki/SBC-Setup-Guide#check-spi-data-lines-in-loopback-mode

        Z-Bot CoreXY Build | Thingiverse Profile

        undefined 1 Reply Last reply 10 Mar 2022, 23:58 Reply Quote 0
        • undefined
          michaelr123 @Phaedrux
          last edited by 10 Mar 2022, 23:58

          @phaedrux

          herer are the results from running the 3 script line. only difference I see is the SPI mode, is that something that should be fixed?

          spi mode: 4
          bits per word: 8
          max speed: 500000 Hz (500 KHz)

          FF FF FF FF FF FF
          40 00 00 00 00 95
          FF FF FF FF FF FF
          FF FF FF FF FF FF
          FF FF FF FF FF FF
          DE AD BE EF BA AD
          F0 0D

          undefined 1 Reply Last reply 11 Mar 2022, 04:20 Reply Quote 0
          • undefined
            Phaedrux Moderator @michaelr123
            last edited by 11 Mar 2022, 04:20

            @michaelr123 said in Duet 3 fails to start print:

            spi mode: 4

            I'm not sure. I'll have to check.

            Do you happen to have another Pi to test with?

            Z-Bot CoreXY Build | Thingiverse Profile

            undefined 1 Reply Last reply 11 Mar 2022, 20:54 Reply Quote 0
            • undefined
              michaelr123 @Phaedrux
              last edited by 11 Mar 2022, 20:54

              @phaedrux

              I have a raspberry Pi 4 that I've tried with this system before and had the same issue as before unfortunately.

              I can run the same check and see what it says though,

              1 Reply Last reply Reply Quote 0
              • undefined
                Phaedrux Moderator
                last edited by 11 Mar 2022, 22:58

                The other thing I would try is a fresh download and image of DuetPi.

                Z-Bot CoreXY Build | Thingiverse Profile

                undefined 1 Reply Last reply 14 Mar 2022, 21:11 Reply Quote 0
                • undefined
                  michaelr123 @Phaedrux
                  last edited by michaelr123 14 Mar 2022, 21:11

                  @phaedrux

                  So here's what I've done so far:

                  -Fresh install of duetPi on my raspberry PI 4, re-ran RRF configurator with the latest settings to get a clean config file set going.
                  -shielded cable install on X-axis stepper driver and for Z-probe
                  -moved x-axis stepper driver to output 0.4 to see if it was something up with the 0.0 drive

                  Here's where I'm at:

                  I think I still am seeing the issue, but now I've seen it happen in an additional instance, I used the thermostatic cooler option for my coldside fan on my hemera which I kind of like, but then I accidently turned this on when I meant to turn on the part cooling fan, and this instantly gave me the same error that I've seen before, but for a different reason now. The M122 is listed below.

                  Other thought I had, is there any chance my ribbon cable is bad? Would that being faulty cause this type of issue?

                  M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.4.0rc2 (2022-02-22 17:04:17) running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-9P63L-DJ3T8-6J1D4-3SD6R-9U479
                  Used output buffers: 1 of 40 (14 max)
                  === RTOS ===
                  Static ram: 150984
                  Dynamic ram: 65804 of which 0 recycled
                  Never used RAM 133884, free system stack 219 words
                  Tasks: SBC(resourceWait:,0.5%,506) HEAT(notifyWait,0.0%,353) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,944) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,343) TMC(notifyWait,7.3%,92) MAIN(running,91.2%,1245) IDLE(ready,0.9%,30), total 100.0%
                  Owned mutexes: HTTP(MAIN)
                  === Platform ===
                  Last reset 00:00:18 ago, cause: software
                  Last software reset at 2022-03-14 16:06, reason: AssertionFailed, GCodes spinning, available RAM 133376, slot 0
                  Software reset code 0x4123 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x2041b504 Task MAIN Freestk 1675 ok
                  Stack: 00001014 004a3b10 00485807 00000000 2042ba18 20419a7c 2042d6e4 00000000 00000001 00000000 004844d7 2042d6e4 00000000 00000000 0048480f 00000000 00000000 20429860 2042d6e0 00000000 2042d6e4 20419a7c 00000000 55700d65 a5a5a5a5 a5a5a5a5 0048493b
                  Error status: 0x00
                  Step timer max interval 134
                  MCU temperature: min 50.6, current 50.9, max 50.9
                  Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                  Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                  Events: 0 queued, 0 completed
                  Driver 0: pos 0, standstill, SG min 0, mspos 8, reads 39308, writes 11 timeouts 0
                  Driver 1: pos 0, standstill, SG min 0, mspos 40, reads 39305, writes 14 timeouts 0
                  Driver 2: pos 0, standstill, SG min 0, mspos 40, reads 39305, writes 14 timeouts 0
                  Driver 3: pos 0, standstill, SG min 0, mspos 888, reads 39305, writes 14 timeouts 0
                  Driver 4: pos 0, standstill, SG min 0, mspos 232, reads 39305, writes 14 timeouts 0
                  Driver 5: pos 0, standstill, SG min 0, mspos 8, reads 39308, writes 11 timeouts 0
                  Date/time: 2022-03-14 16:06:19
                  Slowest loop: 1.09ms; fastest: 0.05ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is doing "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty
                  === CAN ===
                  Messages queued 168, received 0, lost 0, boc 0
                  Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 95/0/0
                  Tx timeouts 0,0,94,0,0,72 last cancelled message type 30 dest 127
                  === SBC interface ===
                  Transfer state: 4, failed transfers: 0, checksum errors: 0
                  RX/TX seq numbers: 11267/750
                  SPI underruns 0, overruns 0
                  State: 5, disconnects: 0, timeouts: 0, IAP RAM available 0x2b8b0
                  Buffer RX/TX: 0/0-0, open files: 0
                  === Duet Control Server ===
                  Duet Control Server v3.4-rc2
                  Code buffer space: 4096
                  Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 45
                  Full transfers per second: 39.82, max time between full transfers: 131.9ms, max pin wait times: 57.0ms/3.3ms
                  Codes per second: 2.85
                  Maximum length of RX/TX data transfers: 3404/1664
                  3/14/2022, 4:06:02 PM Warning: M307: Heater 0 predicted maximum temperature at full power is 321°C
                  3/14/2022, 4:06:02 PM Warning: SPI connection has been reset

                  config (2).g

                  undefined 1 Reply Last reply 14 Mar 2022, 21:20 Reply Quote 0
                  • undefined
                    michaelr123 @michaelr123
                    last edited by 14 Mar 2022, 21:20

                    And here's one after running for a few minutes on a print:

                    M122
                    === Diagnostics ===
                    RepRapFirmware for Duet 3 MB6HC version 3.4.0rc2 (2022-02-22 17:04:17) running on Duet 3 MB6HC v1.01 or later (SBC mode)
                    Board ID: 08DJM-9P63L-DJ3T8-6J1D4-3SD6R-9U479
                    Used output buffers: 1 of 40 (12 max)
                    === RTOS ===
                    Static ram: 150984
                    Dynamic ram: 65804 of which 0 recycled
                    Never used RAM 133884, free system stack 219 words
                    Tasks: SBC(resourceWait:,0.6%,482) HEAT(notifyWait,0.0%,359) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,944) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,343) TMC(notifyWait,7.3%,92) MAIN(running,90.6%,1245) IDLE(ready,1.5%,30), total 100.0%
                    Owned mutexes: HTTP(MAIN)
                    === Platform ===
                    Last reset 00:00:11 ago, cause: software
                    Last software reset at 2022-03-14 16:19, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 133668, slot 1
                    Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x0044a804 BFAR 0xa5a5a5a6 SP 0x2041b520 Task MAIN Freestk 1682 ok
                    Stack: a5a5a5a5 2042b570 00000001 2042406c 00000002 0045c81b 00418cba 21000000 2042b400 00457c1b 2042b510 ffffff00 2042b570 20429f28 00000000 0045c6ef ffffffff 00000000 23d66c2b 00484b0f 2042b570 20429f28 00000000 23d66c2b a5a5a5a5 0045c81b 2042a980
                    Error status: 0x00
                    Step timer max interval 141
                    MCU temperature: min 50.7, current 50.9, max 51.0
                    Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                    12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                    Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                    Events: 0 queued, 0 completed
                    Driver 0: pos 0, standstill, SG min 0, mspos 8, reads 313, writes 11 timeouts 0
                    Driver 1: pos 0, standstill, SG min 0, mspos 840, reads 310, writes 14 timeouts 0
                    Driver 2: pos 0, standstill, SG min 0, mspos 8, reads 310, writes 14 timeouts 0
                    Driver 3: pos 0, standstill, SG min 0, mspos 648, reads 310, writes 14 timeouts 0
                    Driver 4: pos 0, standstill, SG min 0, mspos 184, reads 311, writes 14 timeouts 0
                    Driver 5: pos 0, standstill, SG min 0, mspos 8, reads 314, writes 11 timeouts 0
                    Date/time: 2022-03-14 16:19:33
                    Slowest loop: 1.09ms; fastest: 0.05ms
                    === Storage ===
                    Free file entries: 10
                    SD card 0 not detected, interface speed: 37.5MBytes/sec
                    SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                    === Move ===
                    DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                    === MainDDARing ===
                    Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                    === AuxDDARing ===
                    Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                    === Heat ===
                    Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                    === GCodes ===
                    Segments left: 0
                    Movement lock held by null
                    HTTP* is doing "M122" in state(s) 0
                    Telnet is idle in state(s) 0
                    File is idle in state(s) 0
                    USB is idle in state(s) 0
                    Aux is idle in state(s) 0
                    Trigger* is idle in state(s) 0
                    Queue is idle in state(s) 0
                    LCD is idle in state(s) 0
                    SBC is idle in state(s) 0
                    Daemon is idle in state(s) 0
                    Aux2 is idle in state(s) 0
                    Autopause is idle in state(s) 0
                    Code queue is empty
                    === CAN ===
                    Messages queued 105, received 0, lost 0, boc 0
                    Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 60/0/0
                    Tx timeouts 0,0,59,0,0,44 last cancelled message type 30 dest 127
                    === SBC interface ===
                    Transfer state: 4, failed transfers: 0, checksum errors: 0
                    RX/TX seq numbers: 42465/476
                    SPI underruns 0, overruns 0
                    State: 5, disconnects: 0, timeouts: 0, IAP RAM available 0x2b8b0
                    Buffer RX/TX: 0/0-0, open files: 0
                    === Duet Control Server ===
                    Duet Control Server v3.4-rc2
                    Code buffer space: 4096
                    Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 71
                    Full transfers per second: 39.25, max time between full transfers: 66.1ms, max pin wait times: 59.8ms/7.0ms
                    Codes per second: 5.65
                    Maximum length of RX/TX data transfers: 3472/1664

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      Phaedrux Moderator
                      last edited by 14 Mar 2022, 22:05

                      Was the loop back test the same result with the new Pi?

                      The ribbon could be bad, but would be unusual. You could make a small jumper cable harness to test instead of the ribbon cable.

                      Can you post some photos of your setup? Are there cables running close together in a drag chain or bundle?

                      Z-Bot CoreXY Build | Thingiverse Profile

                      undefined 1 Reply Last reply 14 Mar 2022, 22:44 Reply Quote 0
                      • undefined
                        michaelr123 @Phaedrux
                        last edited by 14 Mar 2022, 22:44

                        @phaedrux

                        here are the results from the SPI test on the PI 4:

                        spi mode: 4
                        bits per word: 8
                        max speed: 500000 Hz (500 KHz)

                        FF FF FF FF FF FF
                        40 00 00 00 00 95
                        FF FF FF FF FF FF
                        FF FF FF FF FF FF
                        FF FF FF FF FF FF
                        DE AD BE EF BA AD
                        F0 0D

                        All the cables are pretty tightly fitted in a drag chain, as they were before, but here are pictures of the setup:

                        IMG_0370.JPEG IMG_0369.JPEG IMG_0373.JPEG IMG_0372.JPEG IMG_0371.JPEG

                        1 Reply Last reply Reply Quote 0
                        • undefined
                          michaelr123
                          last edited by 14 Mar 2022, 23:57

                          I followed this a bit deeper and went to Danal's original SPI test tool and ran the full test with the two jumper cables. My results came back identical to his except for SPI mode being 0x4 instead of 0x0. I'm not sure if that's making a difference or not, but the test tool reports my PI is all good to go?

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            Phaedrux Moderator
                            last edited by 15 Mar 2022, 00:12

                            How long is your ribbon cable? Is that the one that came with the board? Do you have another to test with or are you able to make up a jumper set?

                            This shows which pins are actually required.

                            https://github.com/Duet3D/DuetSoftwareFramework/wiki/SBC-Setup-Guide#measure-continuity-of-the-ribbon-cable

                            Z-Bot CoreXY Build | Thingiverse Profile

                            undefined 1 Reply Last reply 15 Mar 2022, 00:15 Reply Quote 0
                            • undefined
                              michaelr123 @Phaedrux
                              last edited by michaelr123 15 Mar 2022, 00:15

                              @phaedrux

                              Its the original ribbon cable that came with the wire and connector kit.

                              I could make a short ribbon cable and give that a go. The little jumpers I have aren't the nicest, but they should work.

                              Do you have a pin map for the orientation and exactly which pin is which on the duet? I was able to find one for the pi's, but this is as much detail as I can find on the duet doc site :

                              234dd193-3dee-4a3c-b0e6-e85db52721e0-image.png

                              undefined 1 Reply Last reply 15 Mar 2022, 07:37 Reply Quote 0
                              • undefined
                                T3P3Tony administrators @michaelr123
                                last edited by 15 Mar 2022, 07:37

                                @michaelr123

                                The pin numbers are printed on the silkscreen under the board - but of course that's not possible to read after its mounted! I have updated the documentation to show the numbering:
                                0f8d1180-3ace-421b-9587-b034541a31c5-image.png

                                www.duet3d.com

                                undefined 1 Reply Last reply 15 Mar 2022, 13:05 Reply Quote 3
                                • undefined
                                  michaelr123 @T3P3Tony
                                  last edited by 15 Mar 2022, 13:05

                                  @t3p3tony

                                  Ah that makes sense, I've got the board mounted to an acrylic plate, so I could have climbed under the machine to see that, thank you though!!

                                  1 Reply Last reply Reply Quote 0
                                  • undefined
                                    michaelr123
                                    last edited by 20 Mar 2022, 18:48

                                    Update:

                                    I tried switching out the SPI cable: the printer ran fine with the somewhat sketchy ribbon cable I made. Still saw the same issue, SPI reset after a minute or so of running.

                                    • I'm going back to the X-axis, here's where I'm at -

                                    I left the X-axis motor plugged, wires in the wire loom, but I took the set screw out of the pulley and de-tensioned the belt, letting the motor shaft just spin freely inside the pulley:

                                    This ran for 10 - minutes with no issues (This is my slow descent into madness, so humor me with this rabbit hole - we're going to call 10 min+ running a success, more testing will follow). This verifies that everything with the motion control to this specific electrical and mechanical system are sound, which is good.

                                    I then reattached the pulley to the motor shaft with the pulley still de-tensioned: this also ran for 10 minutes plus. This is all with the same basic cylinder G-code I've been using for the last few weeks mind you. Again, this verifies this further verifies that its not a signal to the motor issues, cable issue, driver issue, etc.

                                    So then I reinstalled the belt, not quite as tight as I had it before, and within 2 minutes of running, I had a partial failure, which I've never seen before [console output below]:

                                    3/20/2022, 1:17:19 PM Connection to Duet established
                                    3/20/2022, 1:17:19 PM Warning: Lost connection to Duet (Board is not available (no header))
                                    3/20/2022, 1:15:50 PM M24 Printing resumed

                                    The print kept running after this. Maybe I'm going crazy, but somehow it seems like my old belt attachment system grounded the belt, while the new one completely isolates it in plastic. 5 minutes after this weird half failure happened, the system totally reset:

                                    3/20/2022, 1:22:42 PM Warning: SPI connection has been reset
                                    3/20/2022, 1:22:42 PM Connection to Duet established
                                    3/20/2022, 1:22:38 PM Warning: Lost connection to Duet (Board is not available (no header))

                                    here's a picture of the old system -right side of the picture at the end of the 20x40 extrusion (again, its not pretty, I'm not proud of it, but it worked):
                                    65376751966__DA11A263-1DDC-4E8E-85A0-89FFDC9F6F2B.JPG

                                    basically I cut a slit in the GT2 belt, and sandwiched it around an M5 bolt that clamped 2 plastic pieces around it. This bit into the aluminum as there are spots where the anodized coating is rubbed off. My theory is this somehow connects the belt to the aluminum extrusion piece - am I wrong?

                                    Here's a picture of the new belt tensioner:

                                    IMG_0389.JPEG

                                    There's a connection between the pulley on the X-axis and ground, so that doesn't seem to be helping with the discharge issue. But it does seem like the belt is somehow the issue. I'm probably going to try the old tensioning system and see where that takes me.

                                    undefined 1 Reply Last reply 20 Mar 2022, 22:04 Reply Quote 0
                                    • undefined
                                      michaelr123 @michaelr123
                                      last edited by 20 Mar 2022, 22:04

                                      I just updated 3.4 hoping to get some better error reporting on this issue, M122 reports don't provide anything interesting, but the DCS report log did:

                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [warn] Bad data CRC32 (expected 0xcd39fe63, got 0x4b271ab2)
                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [warn] Bad data CRC32 (expected 0xcd39fe63, got 0x4b271ab2)
                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [warn] Bad data CRC32 (expected 0xcd39fe63, got 0x4b271ab2)
                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [warn] Restarting transfer because the number of maximum retries has been exceeded
                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [warn] Lost connection to Duet (Board is not available (no header))
                                      Mar 20 16:52:11 Duet3 DuetControlServer[2555]: [info] Connection to Duet established
                                      Mar 20 16:53:20 Duet3 DuetControlServer[2555]: [warn] SPI connection has been reset
                                      Mar 20 16:53:20 Duet3 DuetControlServer[2555]: [info] Aborted job file

                                      Does this provide any clues?

                                      1 Reply Last reply Reply Quote 0
                                      • undefined
                                        Phaedrux Moderator
                                        last edited by 20 Mar 2022, 22:07

                                        At this point we've tried many software solutions and swapped out the cable and Pi. I think we should swap the Duet3. When and where did you purchase the Duet3?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        undefined 1 Reply Last reply 20 Mar 2022, 22:14 Reply Quote 0
                                        • undefined
                                          michaelr123 @Phaedrux
                                          last edited by 20 Mar 2022, 22:14

                                          @phaedrux

                                          I already warrantied my board, this is the new one that I just got

                                          undefined 1 Reply Last reply 21 Mar 2022, 03:33 Reply Quote 0
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