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    Heater 1 fault: monitor 0 was triggered

    Scheduled Pinned Locked Moved Solved
    Using Duet Controllers
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    • General_kaosundefined
      General_kaos @Phaedrux
      last edited by

      @phaedrux

      Thanks for the reply.

      Running 3.4 on both the Duet 3 & Toolboard.

      I copied the results to config.g as opposed to saving with M500

      m122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.4.0 (2022-03-15 18:57:24) running on Duet 3 MB6HC v1.01 or later (SBC mode)
      Board ID: 08DJM-956L2-G43S8-6J1FL-3S46L-1S2AD
      Used output buffers: 1 of 40 (12 max)
      === RTOS ===
      Static ram: 151000
      Dynamic ram: 65900 of which 292 recycled
      Never used RAM 133480, free system stack 200 words
      Tasks: SBC(ready,0.5%,467) HEAT(notifyWait,0.0%,149) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,772) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,339) TMC(notifyWait,7.8%,92) MAIN(running,91.6%,923) IDLE(ready,0.0%,30), total 100.0%
      Owned mutexes: HTTP(MAIN)
      === Platform ===
      Last reset 01:11:04 ago, cause: software
      Last software reset at 2022-03-21 20:46, reason: User, GCodes spinning, available RAM 133480, slot 2
      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
      Error status: 0x00
      Step timer max interval 134
      MCU temperature: min 28.8, current 29.1, max 32.5
      Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 11.9, current 12.0, max 12.1, under voltage events: 0
      Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
      Events: 2 queued, 2 completed
      Driver 0: standstill, SG min 0, mspos 904, reads 20206, writes 15 timeouts 0
      Driver 1: standstill, SG min 0, mspos 680, reads 20207, writes 15 timeouts 0
      Driver 2: standstill, SG min 0, mspos 872, reads 20207, writes 15 timeouts 0
      Driver 3: standstill, SG min 0, mspos 536, reads 20207, writes 15 timeouts 0
      Driver 4: standstill, SG min 0, mspos 872, reads 20207, writes 15 timeouts 0
      Driver 5: standstill, SG min 0, mspos 8, reads 20211, writes 11 timeouts 0
      Date/time: 2022-03-21 21:57:25
      Slowest loop: 28.01ms; fastest: 0.03ms
      === Storage ===
      Free file entries: 10
      SD card 0 not detected, interface speed: 37.5MBytes/sec
      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
      === MainDDARing ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === AuxDDARing ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      === GCodes ===
      Segments left: 0
      Movement lock held by null
      HTTP* is doing "M122" in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger* is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is idle in state(s) 0
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty
      === Filament sensors ===
      Extruder 0 sensor: ok
      === CAN ===
      Messages queued 38394, received 87404, lost 0, boc 0
      Longest wait 3ms for reply type 6053, peak Tx sync delay 277, free buffers 49 (min 48), ts 21323/21322/0
      Tx timeouts 0,0,0,0,0,0
      === SBC interface ===
      Transfer state: 4, failed transfers: 0, checksum errors: 0
      RX/TX seq numbers: 35829/35829
      SPI underruns 0, overruns 0
      State: 5, disconnects: 0, timeouts: 0, IAP RAM available 0x2b880
      Buffer RX/TX: 0/0-0, open files: 0
      === Duet Control Server ===
      Duet Control Server v3.4.0
      Code buffer space: 4096
      Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0
      Full transfers per second: 39.16, max time between full transfers: 65.1ms, max pin wait times: 39.6ms/9.7ms
      Codes per second: 0.02
      Maximum length of RX/TX data transfers: 2988/584
      
      M122 b121
      Diagnostics for board 121:
      Duet TOOL1LC rev 1.1 or later firmware version 3.4.0 (2022-03-15 09:00:04)
      Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1)
      All averaging filters OK
      Never used RAM 2556, free system stack 88 words
      Tasks: Move(notifyWait,0.0%,153) HEAT(notifyWait,0.2%,61) CanAsync(notifyWait,0.0%,65) CanRecv(notifyWait,0.0%,76) CanClock(notifyWait,0.0%,65) ACCEL(notifyWait,0.0%,61) TMC(notifyWait,3.0%,57) MAIN(running,91.9%,351) IDLE(ready,0.0%,26) AIN(delaying,4.9%,142), total 100.0%
      Last reset 01:11:44 ago, cause: software
      Last software reset data not available
      Driver 0: pos 0, 409.0 steps/mm,standstill, SG min 0, read errors 0, write errors 1, ifcnt 42, reads 55071, writes 12, timeouts 1, DMA errors 0, CC errors 0, failedOp 0x01, steps req 0 done 0
      Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
      Peak sync jitter 4/9, peak Rx sync delay 214, resyncs 0/0, no step interrupt scheduled
      VIN voltage: min 23.7, current 24.1, max 24.1
      MCU temperature: min 36.6C, current 39.0C, max 44.1C
      Last sensors broadcast 0x00000002 found 1 18 ticks ago, 0 ordering errs, loop time 0
      CAN messages queued 88247, send timeouts 0, received 38761, lost 0, free buffers 37, min 37, error reg 0
      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
      Accelerometer: LIS3DH, status: 00
      I2C bus errors 0, naks 3, other errors 0
      === Filament sensors ===
      Interrupt 5726621 to 0us, poll 4 to 1236us
      Driver 0: ok
      
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      • General_kaosundefined
        General_kaos @Phaedrux
        last edited by

        @phaedrux said in Heater 1 fault: monitor 0 was triggered:

        M98 P"config.g

        M98

        Imgur

        1 Reply Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          Error: unterminated string

          That would seem to indicate that you're missing a quote mark somewhere in your config.g which may be causing chaos.

          Z-Bot CoreXY Build | Thingiverse Profile

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            I can't spot it, maybe you see it?

            but your config is a bit messy. I suggest you make a backup of it, and then create a fresh config using the online tool and manually adjust it to match your config leaving it as organized and clean as possible. Then let's see if we can be rid of the string error.

            https://configtool.reprapfirmware.org/Start

            Even just having a basic config for testing here would be helpful even if it didn't get updated completely for your setup.

            Z-Bot CoreXY Build | Thingiverse Profile

            General_kaosundefined 1 Reply Last reply Reply Quote 0
            • General_kaosundefined
              General_kaos @Phaedrux
              last edited by

              @phaedrux Thanks for the pointer - I'll try that tomorrow and see if it fixes it (& let you know).

              I can't see a missing ", but not easy to spot!

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @General_kaos
                last edited by

                @general_kaos said in Heater 1 fault: monitor 0 was triggered:

                I can't see a missing ", but not easy to spot!

                It could also be a case of a bad character. Or a command that was expecting a quoted string and not getting it.

                That makes me think that perhaps your PID values aren't actually getting executed.

                Z-Bot CoreXY Build | Thingiverse Profile

                General_kaosundefined 2 Replies Last reply Reply Quote 0
                • General_kaosundefined
                  General_kaos @Phaedrux
                  last edited by

                  @phaedrux I realise it's probably just because I mistyped the command first time! Missing " in the console entry of M98 - the repeat above is green.

                  Phaedruxundefined 1 Reply Last reply Reply Quote 0
                  • General_kaosundefined
                    General_kaos @Phaedrux
                    last edited by

                    @phaedrux It actually faults the moment I activate the heater - you can see here it isn't even being told to heat up.

                    Imgur

                    deckingmanundefined 1 Reply Last reply Reply Quote 0
                    • deckingmanundefined
                      deckingman @General_kaos
                      last edited by

                      @general_kaos There are a bunch of M307 commands in your config.g. Most are commented out with a semicolon except the last one which I assume is the active one. However, while it does not have the semicolon, it is indented. So I'm wondering if it's the indentation that is causing the problem? Or perhaps there is a hidden character showing as an indent?

                      Ian
                      https://somei3deas.wordpress.com/
                      https://www.youtube.com/@deckingman

                      General_kaosundefined 1 Reply Last reply Reply Quote 1
                      • Phaedruxundefined
                        Phaedrux Moderator @General_kaos
                        last edited by

                        @general_kaos said in Heater 1 fault: monitor 0 was triggered:

                        @phaedrux I realise it's probably just because I mistyped the command first time! Missing " in the console entry of M98 - the repeat above is green.

                        Ah yes, of course, now it's obvious.

                        Can you send M307 H0 and M307 H1 and compare the results it shows to what you have entered in your config.g to confirm they are actually being applied?

                        My recommendation to start with a clean config still stands.

                        Z-Bot CoreXY Build | Thingiverse Profile

                        General_kaosundefined 1 Reply Last reply Reply Quote 0
                        • General_kaosundefined
                          General_kaos @deckingman
                          last edited by

                          @deckingman Thanks Ian - I tried that, but removing the indent did not fix it. New Config G does though.

                          1 Reply Last reply Reply Quote 0
                          • General_kaosundefined
                            General_kaos @Phaedrux
                            last edited by

                            @phaedrux

                            M307 showed the values being loaded:

                            22/03/2022, 17:48:35: M307 h0: Heater 0: heating rate 0.350, cooling rate 0.158, dead time 31.25, max PWM 1.00, mode PID
                            Predicted max temperature rise 180°C
                            PID parameters: heating P16.3 I0.110 D357.0, steady P16.3 I0.211 D357.0
                            22/03/2022, 17:48:38: M307 h1: Heater 1: heating rate 4.800, cooling rate 0.546, dead time 1.38, max PWM 1.00, mode PID, calibrated at 23.8V
                            Predicted max temperature rise 500°C
                            PID parameters: heating P26.9 I1.612 D26.0, steady P26.9 I4.921 D26.0

                            So onto a new config via the configurator, which worked and still works after copying across all the specific settings for my printer.

                            I am at a loss what was wrong, but it seems to work now. Thanks for your help.

                            ; Configuration file for Duet 3 (firmware version 3.3)
                            ; executed by the firmware on start-up
                            ;
                            ; generated by RepRapFirmware Configuration Tool v3.3.10 on Tue Mar 22 2022 17:23:42 GMT+0000 (Greenwich Mean Time)
                            
                            ; General preferences
                            G90                                              ; send absolute coordinates...
                            M83                                              ; ...but relative extruder moves
                            M550 P"Duet 3"                                   ; set printer name
                            M669 K1                                          ; select CoreXY mode
                            
                            ; Drives
                            M569 P0.0 S0                                     ; physical drive 0.0 goes backwards
                            M569 P0.1 S1                                     ; physical drive 0.1 goes forwards
                            M569 P0.2 S1                                     ; physical drive 0.2 goes forwards
                            M569 P0.3 S0                                     ; physical drive 0.3 goes backwards
                            M569 P0.4 S0                                     ; physical drive 0.4 goes backwards
                            M569 P121.0 S0                                   ; physical drive 121.0 goes backwards
                            M584 X0.0 Y0.1 Z0.2:0.3:0.4 E121.0               ; set drive mapping
                            M350 X16 Y16 Z16 E16 I1                          ; configure microstepping with interpolation
                            M92 X200.00 Y200.00 Z1600.00 E397.00             ; set steps per mm
                            M566 X950.00 Y950.00 Z66.00 E1000.00             ; set maximum instantaneous speed changes (mm/min)
                            M203 X18000.00 Y18000.00 Z540.00 E3600.00        ; set maximum speeds (mm/min)
                            M201 X3000.00 Y3000.00 Z66.00 E1500.00           ; set accelerations (mm/s^2)
                            M906 X1100 Y1100 Z1000 E900 I30                  ; set motor currents (mA) and motor idle factor in per cent
                            M84 S30                                          ; Set idle timeout
                            
                            ;Leadscrew locations
                            M671 X-60:-60:330  Y35:270:170 S7.5  			 ;Front left, Rear Left, Right  S7.5 is the max correction
                            
                            ; Axis Limits
                            M208 X0 Y0 Z0 S1                                 ; set axis minima
                            M208 X290 Y280 Z330 S0                           ; set axis maxima
                            
                            ; Endstops
                            M574 X1 S1 P"io2.in"                             ; configure switch-type (e.g. microswitch) endstop for low end on X via pin io2.in
                            M574 Y1 S1 P"121.io1.in"                         ; configure switch-type (e.g. microswitch) endstop for low end on Y via pin 121.io1.in
                            ;M574 Z1 S2                                       ; configure Z-probe endstop for low end on Z
                            
                            ; Z-Probe
                            M950 S0 C"121.io0.out"                           ; create servo pin 0 for BLTouch
                            M558 P9 C"121.io0.in" H10 F120 T6000             ; set Z probe type to bltouch and the dive height + speeds
                            G31 P500 X45 Y-40 Z1.4                           ; set Z probe trigger value, offset and trigger height
                            M557 X50:250 Y50:250 S20                         ; define mesh grid
                            
                            ; Heaters
                            M308 S0 P"temp0" Y"thermistor" T100000 B4138     ; configure sensor 0 as thermistor on pin temp0
                            M950 H0 C"out0" T0                               ; create bed heater output on out0 and map it to sensor 0
                            M307 H0 B0 S1.00                                 ; disable bang-bang mode for the bed heater and set PWM limit
                            M140 H0                                          ; map heated bed to heater 0
                            M143 H0 S115                                     ; set temperature limit for heater 0 to 115C
                            M307 H0 R0.350 K0.158:0.000 D31.25 E1.35 S1.00 B0 ;PID tune bed heater 21mar22
                            
                            M308 S1 P"121.temp0" Y"thermistor" T100000 B4725 C7.060000e-8 ;e3D thermistor settings
                            M950 H1 C"121.out0" T1                           ; create nozzle heater output on 121.out0 and map it to sensor 1
                            M307 H1 B0 S1.00                                 ; disable bang-bang mode for heater  and set PWM limit
                            M143 H1 S300                                     ; set temperature limit for heater 1 to 300C
                            M307 H1 R4.880 K0.553:0.843 D1.23 E1.35 S1.00 B0 V23.8 ;PID tune w/ e£D thermistor set 23Mar22
                            
                            M308 S3 Y"drivers" A"DRIVERS"  					 ; configure sensor 3 as temperature warning and overheat flags on the TMC2660 on Duet
                            M308 S4 Y"mcu-temp" A"MCU" 						 ; configure sensor 4 as thermistor on pin e1temp for left stepper
                            M912 P0 S-2.7									 ; 2.7C offset from PT100 at RT 4/7/2020
                            
                            ; Fans
                            M950 F0 C"121.out2" Q500                         ; create fan 0 on pin 121.out2 and set its frequency
                            M106 P0 S0 H1 T45                                ; set fan 0 value. Thermostatic control is turned on
                            M950 F1 C"121.out1"                              ; create fan 1 on pin 121.out1 and set its frequency
                            M106 P1 S1 H-1                                   ; set fan 1 value. Thermostatic control is turned off
                            M950 F2 C"out6" Q500                             ; create fan 2 on pin out6 and set its frequency
                            ;M106 P2 S0.25 H1 T30                             ; set fan 2 value. Thermostatic control is turned on
                            M106 P2 S0.3 H3:4 L0.15 X1 B0.3 T30				 ;electronics fan linked to MCU/drivers
                            
                            ;filament sensor
                            M591 D0 P2 C"121.io2.in" S1 					 ;simple trianglelabs filament sensor on toolboard IO2
                            
                            ; Tools
                            M563 P0 D0 H1 F1                                 ; define tool 0
                            G10 P0 X0 Y0 Z0                                  ; set tool 0 axis offsets
                            G10 P0 R0 S0                                     ; set initial tool 0 active and standby temperatures to 0C
                            
                            ; Custom settings are not defined
                            M572 D0 S0.020									 ;set pressure advance
                            
                            ; Miscellaneous
                            T0                                               ; select first tool
                            
                            
                            
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