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    Pause/resume issues in 3.5.0rc3+5?

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    • Exerqtorundefined
      Exerqtor
      last edited by Exerqtor

      EDIT 01.04.2024: Changed the title of the thread due to the problem seemingly being related to pause/resume and not filament runout.


      System info:
      Duet3 Mini Wifi & 1LC 1.2a in standalone with RRF 3.5.0rc3+5 on both boards, DWC 3.5.0.rc3 & WiFiServer 2.1b7


      I thought I should use up some near empty spools I had layiing around and test out the filament runout routine at the same time.

      I've got the printer configured with a HAL sensor right before the "intake" of my LGX-lite (direct drive). It's configured like this:

      
      ; Monitor before extruder (runout sensor)
      M591 P1 C"121.io0.in" S1 D0                                                    ; Filament monitor connected to 121.io0.in
      

      And it's functionally working with some manual testing, RRF detects when filament is/isn't there.

      So now for the chain of event's that revealed the issue:

      • I started printing it was maybe a couple meters of filament left on the first spool, so I started the print and checked that the first layer got put down like it should and left the house for a while.
      • When I came back i suspected the printer to have paused due to filament runout, which it had.
      • PanelDue indicated that extruder 0 had run out of filament, and it seemed like pause.g had ben run (based on where the toolhead was parked).
      • I load & prime the hotend new filament, check for proper function by extruding 20mm @ 5mm/s from PanelDue and press Resume.
      • The toolhead moves back over the workpiece (where i suspect it had run out) and then just hovers over it, not dropping down to the correct Z height.
      • I check the tool temp, and that's all ok. Then start to wonder what the fuck's going on.
      • I press Pause, the printer goes into a paused state and the toolhead moves off accordingly.
      • I try to extrude again with PD, which works.
      • Press Resume again, and the toolhead moves back to the same spot as before, stays there for maybe 1(?)
        second before it moves of to another place and then start raising the bed all "willy-nilly" and ends up ramming the print into the toolhead before I slap the E-stop.

      Here is the eventlog:

      2024-03-31 12:53:08 [warn] Started printing file 0:/gcodes//nevermore/V6_Plenum[2020_extrusion]_0.2mm_ABS_0.4n_2h41m.gcode
      2024-03-31 12:53:10 [warn] M150 sent for logo : yellow
      2024-03-31 12:53:10 [warn] M150 sent for nozzle : yellow
      2024-03-31 12:53:29 [warn] M150 sent for logo : teal
      2024-03-31 12:53:29 [warn] M150 sent for nozzle : bright_white
      2024-03-31 12:53:45 [warn] M150 sent for logo : light_pink
      2024-03-31 12:53:45 [warn] M150 sent for nozzle : bright_white
      2024-03-31 12:53:54 [warn] Leadscrew adjustments made: 0.094 0.123 0.103, points used 3, (mean, deviation) before (0.108, 0.011) after (0.000, 0.000)
      2024-03-31 12:54:04 [warn] Leadscrew adjustments made: -0.015 -0.004 -0.001, points used 3, (mean, deviation) before (-0.006, 0.005) after (-0.000, 0.000)
      2024-03-31 12:54:14 [warn] Leadscrew adjustments made: 0.001 0.001 -0.000, points used 3, (mean, deviation) before (0.001, 0.001) after (0.000, 0.000)
      2024-03-31 12:54:14 [warn] M150 sent for logo : teal
      2024-03-31 12:54:14 [warn] M150 sent for nozzle : bright_white
      2024-03-31 12:54:20 [warn] M150 sent for logo : green
      2024-03-31 12:54:20 [warn] M150 sent for nozzle : bright_white
      2024-03-31 12:54:58 [warn] 25 points probed, min error -0.046, max error 0.015, mean -0.015, deviation 0.013
      Height map saved to file 0:/sys/heightmap.csv
      2024-03-31 12:55:00 [warn] M150 sent for logo : dim_gray
      2024-03-31 12:55:00 [warn] M150 sent for nozzle : dim_red
      2024-03-31 12:55:01 [warn] M150 sent for logo : yellow
      2024-03-31 12:55:01 [warn] M150 sent for nozzle : yellow
      2024-03-31 12:55:25 [warn] M150 sent for logo : light_blue
      2024-03-31 12:55:25 [warn] M150 sent for nozzle : bright_white
      2024-03-31 12:55:36 [warn] M150 sent for logo : red
      2024-03-31 12:55:36 [warn] M150 sent for nozzle : bright_white
      2024-03-31 14:09:53 [warn] Error: Filament error on extruder 0: noFilament
      2024-03-31 14:09:53 [warn] Resume state saved
      2024-03-31 14:46:48 [warn] Printing resumed
      2024-03-31 14:46:56 [warn] Resume state saved
      2024-03-31 14:47:01 [warn] Printing paused at X215.0 Y231.8 Z18.6
      2024-03-31 14:47:11 [warn] Printing resumed
      2024-03-31 14:47:22 [warn] Resume state saved
      2024-03-31 14:47:23 [warn] Error: Failed to switch off remote heater 1: 
      2024-03-31 14:47:23 [warn] Cancelled printing file 0:/gcodes//nevermore/V6_Plenum[2020_extrusion]_0.2mm_ABS_0.4n_2h41m.gcode, print time was 1h 17m
      2024-03-31 14:47:23 [info] Event logging stopped
      power up + 00:00:03 [info] Event logging started at level warn
      power up + 00:00:03 [info] Running: Duet 3 Mini5plus WiFi: 3.5.0-rc.3+5 (2024-03-27 11:34:04)
      power up + 00:00:04 [warn] WiFi module started
      power up + 00:00:04 [warn] M150 sent for logo : n/a
      power up + 00:00:04 [warn] M150 sent for nozzle : n/a
      power up + 00:00:04 [warn] M150 sent for logo : n/a
      power up + 00:00:04 [warn] M150 sent for nozzle : n/a
      power up + 00:00:09 [warn] WiFi module is connected to access point RV32-IOT2G, IP address 192.168.10.x
      power up + 00:00:09 [warn] HTTP client 192.168.10.xx login succeeded (session key 2066145135)
      2024-03-31 14:47:34 [warn] Date and time set at power up + 00:00:09
      

      I haven't bothered utilizing filament-error.g since I haven't seen a need for it in my workflow/setup (yet?).

      But here is my pause/resume macro's:

      ; pause.g
      ; Called when a print from SD card is paused
      
      M83                                                                            ; Relative extruder moves
      G1 E-5 F3600                                                                   ; Retract 10mm of filament
      G91                                                                            ; Relative positioning
      G1 Z5 F360                                                                     ; Lift Z by 5mm
      G90                                                                            ; Absolute positioning
      G1 X0 Y0 F6000                                                                 ; Go to XY 0
      M98 P"/sys/lib/current/xy_current_high.g"                                      ; Restore normal XY currents
      M98 P"/sys/lib/current/z_current_high.g"                                       ; Restore normal Z currents
      
      ; resume.g
      ; Called before a print from SD card is resumed
      
      G1 R1 X0 Y0 Z5 F15000                                                          ; Go to 5mm above position of the last print move
      G1 R1 X0 Y0                                                                    ; Go back to the last print move
      M83                                                                            ; Relative extruder moves
      

      I can't see anything fishy in either of those that should call for the behaviour i experienced when resuming after the runout atleast? 😐

      Exerqtorundefined NeoDueundefined gloomyandyundefined 3 Replies Last reply Reply Quote 0
      • Exerqtorundefined
        Exerqtor @Exerqtor
        last edited by

        This post is deleted!
        1 Reply Last reply Reply Quote 0
        • NeoDueundefined
          NeoDue @Exerqtor
          last edited by NeoDue

          @Exerqtor Hm. My printer is running rc3+ date 2024-02-27 here, and filament run-out detection. manual load via PanelDue and resume works perfectly fine.

          In case it helps, here are my pause/resume config files:

          ; pause.g
          ; Called when a print from SD card is paused
          
          M400                     ; finish active moves 
          G10                      ; retract
          G91                      ; relative Positioning
          G1 Z5 F360               ; move bed 5mm down
          G90                      ; absolute positioning
          G1 H2 X{move.axes[0].min} U{move.axes[3].max} Y{move.axes[1].min} F6000    ; move heads to X=min/U=max and Y=min
          
          ; resume.g
          ; called before a print from SD card is resumed
          
          G1 R1 X0 Y0 Z5 F6000     ; move print head 5mm over last position saved in slot 1 
          G1 R1 X0 Y0 Z0           ; move bed up 5mm.
          M400                     ; finish active moves
          G11                      ; unretract if retracted
          
          Exerqtorundefined 1 Reply Last reply Reply Quote 0
          • Exerqtorundefined
            Exerqtor @NeoDue
            last edited by Exerqtor

            @NeoDue Thx for your feedback, but you're running a somewhat older version of 3.5.0 rc3 than I am. Please try these binaries and check if it still works.


            I just tried another print with a manual filamentchange (who worked on on 3.5.0b4) and this make the machine stuck in a loop.

            I've got the machine setup to automatically purge(if "ok") & resume the print once i click "ok" or "skip" in when M600 is called (I'll post the macros farther down in the post).

            This is the way it's supposed to work (and have worked until recently):

            • M600 in the job g-code and filament-change.g gets run (look farther down for contence of filament-change.g).
            • The printer goes into the filament change position and a M291 S4 message with "OK" & "SKIP" get's displayed.
            • "OK" is pressed it will extrude(purge) "n" amount of filament, dim the chamber lights back down, change global.FilamentCHG to true and the that's the end of filament--change.g.
              If "SKIP" is pressed no filament will get extruded(purged), dim the chamber lights back down, change global.FilamentCHG to true and the that's the end of filament--change.g.
            • The following condition in daemon.g get's ran:
              ; Resume after filament change
              if exists(global.FilamentCHG)
                if global.FilamentCHG = true && state.status = "paused"
                  M24                                                                      ; Resume the pause automatically now that the manual filament change is done
                  set global.FilamentCHG = false
            
            • M24 gets sent by daemon.g and resume.g gets ran and the print continues(look farther down for contence of resume.g).

            This is what happens now:

            • M600 in the job g-code and filament-change.g gets run (look farther down for contence of filament-change.g).
            • The printer goes into the filament change position and a M291 S4 message with "OK" & "SKIP" get's displayed.
            • "OK" is pressed it will extrude(purge) "n" amount of filament, dim the chamber lights back down, change global.FilamentCHG to true and the that's the end of filament-change.g.
              If "SKIP" is pressed no filament will get extruded(purged), dim the chamber lights back down, change global.FilamentCHG to true and the that's the end of filament--change.g.
            • The following condition in daemon.g get's ran:
              ; Resume after filament change
              if exists(global.FilamentCHG)
                if global.FilamentCHG = true && state.status = "paused"
                  M24                                                                      ; Resume the pause automatically now that the manual filament change is done
                  set global.FilamentCHG = false
            
            • M24 gets sent by daemon.g and resume.g gets ran and the print head returns over the point where it stopped printing but DON'T lower the nozzle down to the buildplate again.
            • Hovers over the buildplate for a split second and filament-change.g get's ran again, and hence it's stuck in a loop no matter if i press "OK" or "SKIP". The only way i can break the cycle is to power toggle the machine.

            Here is the event log from the failed filament change/resumes:

            2024-04-01 12:21:01 [warn] Started printing file 0:/gcodes/BFI/[a]_BFI_Front_with_Logo_M3_Symmetrical_x2_0.2mm_ABS_0.4n_21m8s.gcode
            2024-04-01 12:21:03 [warn] M150 sent for logo : yellow
            2024-04-01 12:21:03 [warn] M150 sent for nozzle : yellow
            2024-04-01 12:21:04 [warn] M150 sent for logo : teal
            2024-04-01 12:21:04 [warn] M150 sent for nozzle : bright_white
            2024-04-01 12:21:32 [warn] M150 sent for logo : green
            2024-04-01 12:21:32 [warn] M150 sent for nozzle : bright_white
            2024-04-01 12:21:46 [warn] 9 points probed, min error -0.014, max error 0.013, mean -0.004, deviation 0.008
            Height map saved to file 0:/sys/heightmap.csv
            2024-04-01 12:21:47 [warn] M150 sent for logo : dim_gray
            2024-04-01 12:21:47 [warn] M150 sent for nozzle : dim_red
            2024-04-01 12:21:48 [warn] M150 sent for logo : yellow
            2024-04-01 12:21:48 [warn] M150 sent for nozzle : yellow
            2024-04-01 12:22:13 [warn] M150 sent for logo : light_blue
            2024-04-01 12:22:13 [warn] M150 sent for nozzle : bright_white
            2024-04-01 12:22:23 [warn] M150 sent for logo : red
            2024-04-01 12:22:23 [warn] M150 sent for nozzle : bright_white
            2024-04-01 12:24:51 [warn] Resume state saved
            2024-04-01 12:26:46 [warn] Printing paused for filament change at X174.6 Y157.6 Z0.2
            2024-04-01 12:26:48 [warn] Printing resumed
            2024-04-01 12:26:48 [warn] Resume state saved
            2024-04-01 12:27:20 [warn] Printing paused for filament change at X174.6 Y157.6 Z5.2
            2024-04-01 12:27:21 [warn] Printing resumed
            2024-04-01 12:27:21 [warn] Resume state saved
            2024-04-01 12:27:38 [warn] Printing paused for filament change at X174.6 Y157.6 Z10.2
            2024-04-01 12:27:40 [warn] Printing resumed
            2024-04-01 12:27:40 [warn] Resume state saved
            2024-04-01 12:29:17 [warn] Printing paused for filament change at X174.6 Y157.6 Z15.2
            2024-04-01 12:29:18 [warn] Error: M0: Pause the print before attempting to cancel it
            2024-04-01 12:29:19 [warn] Printing resumed
            2024-04-01 12:29:19 [warn] Resume state saved
            2024-04-01 12:29:22 [warn] Error: M0: Pause the print before attempting to cancel it
            2024-04-01 12:32:34 [warn] HTTP client 192.168.10.1xx login succeeded (session key 4247479220)
            2024-04-01 12:34:00 [warn] Printing paused for filament change at X174.6 Y157.6 Z20.2
            2024-04-01 12:34:02 [warn] Printing resumed
            2024-04-01 12:34:02 [warn] Resume state saved
            2024-04-01 13:02:00 [warn] Warning: VIN under-voltage event (8.6V)
            power up + 00:00:03 [info] Event logging started at level warn
            power up + 00:00:03 [info] Running: Duet 3 Mini5plus WiFi: 3.5.0-rc.3+5 (2024-03-27 11:34:04)
            power up + 00:00:04 [warn] WiFi module started
            power up + 00:00:04 [warn] M150 sent for logo : n/a
            power up + 00:00:04 [warn] M150 sent for nozzle : n/a
            power up + 00:00:04 [warn] M150 sent for logo : n/a
            power up + 00:00:04 [warn] M150 sent for nozzle : n/a
            power up + 00:00:09 [warn] WiFi module is connected to access point RV32-IOT2G, IP address 192.168.10.x
            power up + 00:00:10 [warn] HTTP client 192.168.10.xx login succeeded (session key 3077884437)
            2024-04-01 13:02:19 [warn] Date and time set at power up + 00:00:10
            

            The [warn] Error: M0: Pause the print before attempting to cancel it errors got thrown because I tried pressing cancel in PD & DWC after pressing "OK" / "SKIP" btw.


            ; /sys/filament-change.g  v2.2
            ; Called when M600 is sent
            ; Used to do a filament change while printing
            
            ;---/
            ; -/--/--/--/--/--/--/--/--/--/--/--/--/--/--/--/--
            ; THIS MACRO ONLY WORKS WITH RRF 3.5.0b1 AND LATER!!
            ;--/--/--/--/--/--/--/--/--/--/--/--/--/--/--/--/--
            ;-/
            
            ; ====================---------------------------------------------------------
            ; Settings section
            ; ====================
            
            ; Will not be used if you're using a "goto" macro
            var x = 40                                                                     ; The X axis location where you want the hotend to "park" while changing filament
            var y = 0                                                                      ; The Y axis location where you want the hotend to "park" while changing filament
            
            var spd = 15000                                                                ; The speed of which you want the hotend to move to the "park" location
            
            var lift = 20                                                                  ; The Z clearance you want your nozzle to have from the print while changing filament
            
            var lights = true                                                              ; true / false depending if you have chamber lights or not that you want to turn on
            ; If you don't have lights you want to turn on don't mess with these
            var io = 0                                                                     ; The GPIO port number (set by M950) for the lights you want to turn on
            var pwm = 1                                                                    ; The PWM to be set on the GPIO port above, 0=off 1=full power
              
            var purge = 60                                                                 ; The amount of filament your hotend need to purge for a clean filament/color change
            
            ; Will be swaped out with global.unload_length if you have that defined!
            var unload = 12                                                                ; The length of which filament have to be retracted to clear the meltzone
             
            ; Don't touch anyting beyond this point(unless you know what you're doing)!!
            ; ====================---------------------------------------------------------
            
            
            if exists(global.unload_length)
              set var.unload = global.unload_length
            
            var pwm_res = state.gpOut[{var.io}].pwm                                        ; Store the PWM from the PPIO port so that it can be returned after changing filament
            if var.lights
              M42 P{var.io} S{var.pwm}                                                     ; Turn on the lights
            
            if fileexists("/sys/lib/beep/l.g")
              M98 P"/sys/lib/beep/l.g"                                                     ; Long beep
            
            M400                                                                           ; Wait for moves to finish
            G91                                                                            ; Relative positioning
            M83                                                                            ; Extruder relative positioning
            G10                                                                            ; Retraction
            G1 Z1.00 X20.0 Y20.0 F20000                                                    ; Short quick move to disengage from print
              
            G1 Z{var.lift - 1} F800                                                        ; Go to spesified Z clearance
            
            if !fileexists("/sys/lib/goto/front_right.g")
              G90                                                                          ; Absolute positioning
              G1 X{var.x} Y{var.y} F{var.spd}                                              ; Move the nozzle to the location defined in the settings section
            if fileexists("/sys/lib/goto/front_right.g")
              M98 P"/sys/lib/goto/front_right.g" {var.spd}                                 ; Move to front right for filament change
              
              
            G1 E2 F800                                                                     ; Extrude slightly to help form a nice tip on the filament
            G1 E{-(var.unload)} F800                                                       ; Retract filament from the meltzone
            M400                                                                           ; Wait for moves to finish
            
            if fileexists("/sys/lib/beep/xl.g")
              M98 P"/sys/lib/beep/xl.g"                                                    ; Extra long beep
            
            M291 S4 R"Manual Filament Change" P"Change & prime filament, then press OK." K{"OK","SKIP",}
            ; "OK"
            if input = 0
              G1 E{var.purge} F200                                                         ; Purge filament
            ; "SKIP"
            if input = 1
              G1 E{var.unload} F800                                                        ; Extrude filament back to the meltzone  
            
            M400                                                                           ; Wait for moves to finish
            if var.lights
              M42 P{var.io} S{var.pwm_res}                                                 ; Return lights to previous state
            
            if !exists(global.FilamentCHG)
              global FilamentCHG = true
            else
              set global.FilamentCHG = true
            
            ; resume.g
            ; Called before a print from SD card is resumed
            
            G1 R1 X0 Y0 Z5 F15000                                                          ; Go to 5mm above position of the last print move
            G1 R1 X0 Y0                                                                    ; Go back to the last print move
            M83                                                                            ; Relative extruder moves
            
            NeoDueundefined 1 Reply Last reply Reply Quote 0
            • NeoDueundefined
              NeoDue @Exerqtor
              last edited by

              @Exerqtor Will do, but probably not before the weekend - I have to finish a longer print first.

              In the meantime, I will try to understand that complicated filament change logic of yours... 😵

              Offtopic and just to understand: why the heck do you use daemon.g to restart the print instead of simply using filament-change.g to handle everything, including the decision to resume the print?

              Exerqtorundefined 1 Reply Last reply Reply Quote 0
              • Exerqtorundefined
                Exerqtor @NeoDue
                last edited by Exerqtor

                @NeoDue said in Pause/resume issues in 3.5.0rc3+5?:

                @Exerqtor Will do, but probably not before the weekend - I have to finish a longer print first.

                In the meantime, I will try to understand that complicated filament change logic of yours... 😵

                Offtopic and just to understand: why the heck do you use daemon.g to restart the print instead of simply using filament-change.g to handle everything, including the decision to resume the print?

                It's talked about in this thread from about this time last year lol. It might be that RRF has changed it's behaviour in regard to how the states and resume is dealt with on filament change by now that I haven't picked up on. But if you skim through that thread you will see what I/we wanted to achieve.

                NeoDueundefined 1 Reply Last reply Reply Quote 0
                • NeoDueundefined
                  NeoDue @Exerqtor
                  last edited by NeoDue

                  @Exerqtor Thanks for the link! I faintly remember reading it while I worked on my setup... and that it was the reason for deciding that a manual filament change is perfectly fine for now 😇

                  But @dc42's information in there that M24 within filament-change.g is not allowed is the answer to my question.

                  Edit: one thought however: I do not use M600 or such, but I do use a custom filament load macro (not named "filament-change.g") - which is however called by hand via pressing the corresponding Macro button in the PanelDue. When the filament is loaded, I press resume manually - which also works, at least for my firmware version. Did you already try to narrow down the issue, e.g. by calling your filament change macro manually / replacing M24 with a manual call etc?

                  Exerqtorundefined 1 Reply Last reply Reply Quote 0
                  • Exerqtorundefined
                    Exerqtor @NeoDue
                    last edited by

                    @NeoDue Well it's happening in two different scenarios for me now at least, one from the printer being paused by a filament runout, and one from a filament change.

                    And since i'm not using filament-error.g the filament runout is pretty much just a regular pause but with a runout flag.

                    So i'm quite sure it's something under the hood of RRF's thats broken and causing this 😅

                    NeoDueundefined 1 Reply Last reply Reply Quote 0
                    • NeoDueundefined
                      NeoDue @Exerqtor
                      last edited by

                      @Exerqtor Yes, but it might help the devs if you can tell them for example "step x works if I start the macro manually but if I let M600 start it it fails" or such, hence the question. You do have a rather complex routine there 😉

                      1 Reply Last reply Reply Quote 0
                      • gloomyandyundefined
                        gloomyandy @Exerqtor
                        last edited by

                        @Exerqtor We are currently investigating a problem with pause/resume in the latest builds of RRF. I suspect this may be what is causing this problem. You may want to hold off any further investigations until we have a fix for that problem available.

                        Exerqtorundefined 1 Reply Last reply Reply Quote 2
                        • Exerqtorundefined
                          Exerqtor @gloomyandy
                          last edited by Exerqtor

                          @gloomyandy Glad to hear my assumptions were right 😆 I'll avoid anything pause/resume related until then lol

                          Is it related to the commits made for fixing pause/resume issues made in the 3.5-mms-changes branch? I don't think I had any issues before MMS got merged with 3.5-dev 🤔

                          gloomyandyundefined 1 Reply Last reply Reply Quote 0
                          • gloomyandyundefined
                            gloomyandy @Exerqtor
                            last edited by

                            @Exerqtor MMS has been present in pretty much all of the 3.5 releases.

                            Exerqtorundefined 1 Reply Last reply Reply Quote 0
                            • Exerqtorundefined
                              Exerqtor @gloomyandy
                              last edited by Exerqtor

                              @gloomyandy Yeah I know, I meant the 3.5-mms-changes branch David made March first and the commits made to that branch March 4th [1] & [2] related to resume after pause. I stated the wrong branch name in the previous post(edited it by now).

                              dc42undefined 3 Replies Last reply Reply Quote 0
                              • dc42undefined
                                dc42 administrators @Exerqtor
                                last edited by

                                @Exerqtor please try the 3.5.0-rc.3+6 build at https://www.dropbox.com/scl/fo/x7ec0sg11a2zrevxoj3j8/h?rlkey=pcdfiv72z0dkkrbv5i8cem5fd&dl=0.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

                                1 Reply Last reply Reply Quote 1
                                • dc42undefined
                                  dc42 administrators @Exerqtor
                                  last edited by

                                  @Exerqtor oops, that's the wrong firmware build. Give me a few minutes to correct it.

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  1 Reply Last reply Reply Quote 1
                                  • dc42undefined
                                    dc42 administrators @Exerqtor
                                    last edited by

                                    @Exerqtor I've updated those files.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                                    Exerqtorundefined 1 Reply Last reply Reply Quote 1
                                    • Exerqtorundefined
                                      Exerqtor @dc42
                                      last edited by Exerqtor

                                      @dc42
                                      Aaah i just did a test with the first ones you supplied there and was about to repport that the issue is persistent.

                                      I'll try the NEWER ones after dinner and report back!


                                      @dc42 Naah that build is borked! Now Z won't even move after homing. Or if i try to move the bed from PD / DWC nothing happens.

                                      The printer reported Z0.54 after homing, and if i try to lower Z with 5mm the reported Z-height changes to 5.54 but no actual movement.

                                      Don't know if M122 reports will help any, but here they are:

                                      === Diagnostics ===
                                      RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-rc.3+6 (2024-04-02 14:34:06) running on Duet 3 Mini5plus WiFi (standalone mode)
                                      Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ
                                      Used output buffers: 29 of 40 (40 max)
                                      === RTOS ===
                                      Static ram: 103232
                                      Dynamic ram: 126672 of which 12 recycled
                                      Never used RAM 8380, free system stack 135 words
                                      Tasks: NETWORK(2,nWait 7,16.1%,229) HEAT(3,nWait 6,0.0%,351) Move(4,nWait 6,0.0%,256) CanReceiv(6,nWait 1,0.1%,797) CanSender(5,nWait 7,0.0%,336) CanClock(7,delaying,0.0%,339) TMC(4,nWait 6,0.8%,68) MAIN(1,running,81.2%,654) IDLE(0,ready,0.9%,30) AIN(4,delaying,0.8%,260), total 100.0%
                                      Owned mutexes: WiFi(NETWORK)
                                      === Platform ===
                                      Last reset 00:19:21 ago, cause: software
                                      Last software reset at 2024-04-02 15:40, reason: User, Gcodes spinning, available RAM 11360, slot 1
                                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00489000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                                      Error status: 0x04
                                      Aux0 errors 0,0,0
                                      MCU revision 3, ADC conversions started 1161890, completed 1161890, timed out 0, errs 0
                                      MCU temperature: min 39.6, current 43.6, max 47.8
                                      Supply voltage: min 2.8, current 24.1, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
                                      Heap OK, handles allocated/used 99/43, heap memory allocated/used/recyclable 2048/1500/940, gc cycles 264
                                      Events: 0 queued, 0 completed
                                      Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 32, reads 61101, writes 32, timeouts 0, DMA errors 0, CC errors 0
                                      Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 32, reads 61101, writes 32, timeouts 0, DMA errors 0, CC errors 0
                                      Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 61111, writes 22, timeouts 0, DMA errors 0, CC errors 0
                                      Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 21, reads 61111, writes 21, timeouts 0, DMA errors 0, CC errors 0
                                      Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 21, reads 61112, writes 21, timeouts 0, DMA errors 0, CC errors 0
                                      Driver 5: not present
                                      Driver 6: not present
                                      Date/time: 2024-04-02 16:36:25
                                      Cache data hit count 2117861953
                                      Slowest loop: 164.57ms; fastest: 0.13ms
                                      === Storage ===
                                      Free file entries: 16
                                      SD card 0 detected, interface speed: 22.5MBytes/sec
                                      SD card longest read time 7.6ms, write time 8.1ms, max retries 0
                                      === Move ===
                                      DMs created 83, segments created 11, maxWait 737572ms, bed compensation in use: none, height map offset 0.000, max steps late 1, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 0.00
                                      no step interrupt scheduled
                                      Moves shaped first try 5, on retry 0, too short 0, wrong shape 4, maybepossible 0
                                      === DDARing 0 ===
                                      Scheduled moves 25, completed 25, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === DDARing 1 ===
                                      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === Heat ===
                                      Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                                      Heater 0 is on, I-accum = 0.4
                                      Heater 1 is on, I-accum = 0.0
                                      === GCodes ===
                                      Movement locks held by null, null
                                      HTTP is idle in state(s) 0
                                      Telnet is idle in state(s) 0
                                      File is idle in state(s) 0
                                      USB is idle in state(s) 0
                                      Aux is idle in state(s) 0 0 0 0 0, running macro
                                      Trigger is idle in state(s) 0
                                      Queue is idle in state(s) 0
                                      LCD is idle in state(s) 0
                                      SBC is idle in state(s) 0
                                      Daemon is doing "G4 P250" in state(s) 0 0, running macro
                                      Aux2 is idle in state(s) 0
                                      Autopause is idle in state(s) 0
                                      File2 is idle in state(s) 0
                                      Queue2 is idle in state(s) 0
                                      Q0 segments left 0, axes/extruders owned 0x0000807
                                      Code queue 0 is empty
                                      Q1 segments left 0, axes/extruders owned 0x0000000
                                      Code queue 1 is empty
                                      === Filament sensors ===
                                      check 0 clear 0
                                      Extruder 0 sensor: no filament
                                      === CAN ===
                                      Messages queued 10493, received 23836, lost 0, errs 1307, boc 0
                                      Longest wait 2ms for reply type 6031, peak Tx sync delay 8139, free buffers 26 (min 25), ts 5810/5808/0
                                      Tx timeouts 0,0,1,0,0,0 last cancelled message type 30 dest 127
                                      === Network ===
                                      Slowest loop: 201.24ms; fastest: 0.00ms
                                      Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                                      HTTP sessions: 2 of 8
                                      === WiFi ===
                                      Interface state: active
                                      Module is connected to access point 
                                      Failed messages: pending 0, notrdy 1, noresp 1
                                      Firmware version 2.1beta7
                                      MAC address c4:5b:be:ce:91:93
                                      Module reset reason: Power up, Vcc 3.37, flash size 2097152, free heap 36232
                                      WiFi IP address 192.168.10.x
                                      Signal strength -54dBm, channel 6, mode 802.11n, reconnections 0
                                      Clock register 00002001
                                      Socket states: 0 0 0 0 0 0 0 0
                                      M122 B121
                                      Diagnostics for board 121:
                                      Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-rc.3+6 (2024-04-02 12:49:31)
                                      Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
                                      All averaging filters OK
                                      Never used RAM 3928, free system stack 134 words
                                      Tasks: Move(3,nWait 7,0.0%,135) HEAT(2,nWait 6,0.4%,105) CanAsync(5,nWait 4,0.0%,51) CanRecv(3,nWait 1,0.0%,71) CanClock(5,nWait 1,0.0%,59) ACCEL(3,nWait 6,0.0%,53) TMC(2,nWait 6,3.4%,53) MAIN(1,running,91.2%,315) IDLE(0,ready,0.0%,27) AIN(2,delaying,4.9%,112), total 100.0%
                                      Owned mutexes:
                                      Last reset 00:19:29 ago, cause: power up
                                      Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0
                                      Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok
                                      Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0
                                      Driver 0: pos 0, 568.8 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 11, reads 60547, writes 11, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0
                                      Moves scheduled 0, completed 0, in progress 0, hiccups 0, segs 0, step errors 0, maxLate 0 maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0, ebfmin 0.00 max 0.00
                                      Peak sync jitter -2/9, peak Rx sync delay 219, resyncs 0/0, no timer interrupt scheduled
                                      VIN voltage: min 23.7, current 24.7, max 24.9
                                      MCU temperature: min 65.2C, current 71.7C, max 71.7C
                                      Last sensors broadcast 0x00000012 found 2 15 ticks ago, 0 ordering errs, loop time 0
                                      CAN messages queued 24032, send timeouts 0, received 10573, lost 0, errs 0, boc 0, free buffers 18, min 18, error reg 0
                                      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                                      Accelerometer: LIS3DH, status: 00
                                      I2C bus errors 0, naks 3, contentions 0, other errors 0
                                      === Filament sensors ===
                                      Interrupt 5726621 to 0us, poll 4 to 1432us
                                      Driver 0: ok
                                      

                                      I just saw that the printer state is permanently "Busy" now after trying to home & lower Z. Dispite the printer not doing anything.

                                      dc42undefined 1 Reply Last reply Reply Quote 0
                                      • dc42undefined
                                        dc42 administrators @Exerqtor
                                        last edited by

                                        @Exerqtor I'm sorry about that, I'm about to run a print to test the correction.

                                        Duet WiFi hardware designer and firmware engineer
                                        Please do not ask me for Duet support via PM or email, use the forum
                                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                                        Exerqtorundefined 1 Reply Last reply Reply Quote 0
                                        • Exerqtorundefined
                                          Exerqtor @dc42
                                          last edited by

                                          @dc42 Nothing to say sorry for, it's a pre-release afterall 👌

                                          dc42undefined 1 Reply Last reply Reply Quote 0
                                          • dc42undefined
                                            dc42 administrators @Exerqtor
                                            last edited by

                                            @Exerqtor I've updated the files, same link as before. A remaining issue I have noticed is that when resuming after a pause there is a slight delay between restoring the XYZ position and starting printing again. I think I know the reason for that and I'll look into it tomorrow.

                                            Duet WiFi hardware designer and firmware engineer
                                            Please do not ask me for Duet support via PM or email, use the forum
                                            http://www.escher3d.com, https://miscsolutions.wordpress.com

                                            Exerqtorundefined 1 Reply Last reply Reply Quote 0
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