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    Duet2 Firmware Upgrade Issue

    Scheduled Pinned Locked Moved
    Firmware installation
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      What are the motor specs?
      What current have you set them to?
      How fast are you trying to move them?
      Can you share your config.g and the results of sending M122 and M98 P"config.g" in the gcode console?
      If you swap the motors to other drivers does the problem follow the motor or the driver?

      Z-Bot CoreXY Build | Thingiverse Profile

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      • Bewarenundefined
        Bewaren @Phaedrux
        last edited by

        @Phaedrux said in Duet2 Firmware Upgrade Issue:

        M122

        M122
        === Diagnostics ===
        RepRapFirmware for Duet 2 WiFi/Ethernet version 3.5.1 (2024-04-19 14:40:46) running on Duet Ethernet 1.02 or later
        Board ID: 08DGM-917DA-G4MSD-6JKDA-3SN6Q-TST39
        Used output buffers: 1 of 26 (14 max)
        === RTOS ===
        Static ram: 23256
        Dynamic ram: 67932 of which 0 recycled
        Never used RAM 21956, free system stack 184 words
        Tasks: NETWORK(1,ready,27.9%,220) HEAT(3,nWait 5,0.0%,330) Move(4,nWait 5,0.0%,359) MAIN(1,running,72.0%,761) IDLE(0,ready,0.1%,29), total 100.0%
        Owned mutexes:
        === Platform ===
        Last reset 00:27:25 ago, cause: software
        Last software reset at 2024-04-19 22:48, reason: User, Gcodes spinning, available RAM 21812, slot 0
        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
        Error status: 0x00
        Aux0 errors 0,0,0
        MCU temperature: min 35.4, current 36.7, max 37.3
        Supply voltage: min 24.2, current 24.3, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
        Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
        Events: 0 queued, 0 completed
        Driver 0: standstill, SG min n/a
        Driver 1: standstill, SG min n/a
        Driver 2: standstill, SG min n/a
        Driver 3: standstill, SG min n/a
        Driver 4: standstill, SG min n/a
        Driver 5:
        Driver 6:
        Driver 7:
        Driver 8:
        Driver 9:
        Driver 10:
        Driver 11:
        Date/time: 2024-04-19 23:15:40
        Cache data hit count 4294967295
        Slowest loop: 15.20ms; fastest: 0.18ms
        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
        === Storage ===
        Free file entries: 10
        SD card 0 detected, interface speed: 20.0MBytes/sec
        SD card longest read time 13.0ms, write time 0.0ms, max retries 0
        === Move ===
        DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, max steps late 0, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 0.00
        no step interrupt scheduled
        Moves shaped first try 0, on retry 0, too short 0, wrong shape 0, maybepossible 0
        === DDARing 0 ===
        Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === Heat ===
        Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
        === GCodes ===
        Movement locks held by null
        HTTP is idle in state(s) 0
        Telnet is idle in state(s) 0
        File is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger is idle in state(s) 0
        Queue is idle in state(s) 0
        LCD is idle in state(s) 0
        Daemon is idle in state(s) 0
        Autopause is idle in state(s) 0
        Q0 segments left 0
        Code queue 0 is empty
        === Network ===
        Slowest loop: 6.92ms; fastest: 0.01ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
        HTTP sessions: 1 of 8
        Interface state active, link 100Mbps full duplex
        Socket states: 5 2 2 2 2 2

        M98 "config.g"
        Error: M98: No P or R parameter

        Nema 17 Specs:
        Motor Type: Bipolar Stepper.
        Step Angle: 1.8°
        Holding Torque: 26Ncm(36.8oz.in)
        Rated Current/phase: 0.4A.
        Phase Resistance: 30ohms.
        Inductance: 37mH+/-20%(1KHz)

        Config.g:
        config (1).g

        Phaedruxundefined Bewarenundefined 3 Replies Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator @Bewaren
          last edited by

          @Bewaren said in Duet2 Firmware Upgrade Issue:

          M98 "config.g"
          Error: M98: No P or R parameter

          The command is M98 P"config.g"
          Please try running it again.

          Z-Bot CoreXY Build | Thingiverse Profile

          Bewarenundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @Bewaren
            last edited by

            @Bewaren said in Duet2 Firmware Upgrade Issue:

            Nema 17 Specs:
            Motor Type: Bipolar Stepper.
            Step Angle: 1.8°
            Holding Torque: 26Ncm(36.8oz.in)
            Rated Current/phase: 0.4A.
            Phase Resistance: 30ohms.
            Inductance: 37mH+/-20%(1KHz)

            Does it have a model number?

            Are your motors getting very hot?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • Bewarenundefined
              Bewaren @Bewaren
              last edited by

              @Bewaren M98
              P"config.g"
              HTTP is enabled on port 80
              FTP is disabled
              TELNET is disabled

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              • Bewarenundefined
                Bewaren @Phaedrux
                last edited by

                @Phaedrux Motors are cold to the touch

                Motors model number is:
                JK42HS40-1704-13A

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                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  try increasing your motor current set in M906 to 1200

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • Bewarenundefined
                    Bewaren @Phaedrux
                    last edited by

                    @Phaedrux Tried this and still getting the same error message 😕

                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                    • Bewarenundefined
                      Bewaren @Phaedrux
                      last edited by

                      @Phaedrux It's also now giving me this error, not sure if it's possibly related?

                      20/04/2024, 18:20:07 Error: in file macro line 7: G1: Failed to enable endstops

                      Phaedruxundefined 1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator @Bewaren
                        last edited by

                        @Bewaren said in Duet2 Firmware Upgrade Issue:

                        20/04/2024, 18:20:07 Error: in file macro line 7: G1: Failed to enable endstops

                        Sounds like your homing files are trying to use an endstop that doesn't exist. Post your homing files.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • Phaedruxundefined
                          Phaedrux Moderator @Bewaren
                          last edited by

                          @Bewaren said in Duet2 Firmware Upgrade Issue:

                          @Phaedrux Tried this and still getting the same error message 😕

                          Phase disconnected means that either the wiring isn't good, or the driver is internally damaged. I'd replace the wiring, particularly the crimps.

                          Are you still getting expected movement from the motors?

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • Bewarenundefined
                            Bewaren @Phaedrux
                            last edited by

                            @Phaedrux Unfortunately I've checked the wires already and have replaced them all, the motors are moving as expected however when it's homing multiple axis at once (X and Y) it seems to encounter an issue and starts skipping on the belt.

                            I'm assuming it's a issue with the driver then?

                            If so I assume there's nothing I can really do to repair it? I'm running two Z motors and a X and Y so won't have a free one once I add the extruder also

                            Thanks again for the help!

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                            • Bewarenundefined
                              Bewaren @Phaedrux
                              last edited by

                              @Phaedrux Yeah it's just clicked it'll be my Z axis, I've not set the bed up as of yet so don't even have those motors connected 😄

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                Are you getting the driver warning from the driver that the Z axis is connected to?

                                Z-Bot CoreXY Build | Thingiverse Profile

                                Bailey Jamesundefined 1 Reply Last reply Reply Quote 0
                                • Bailey Jamesundefined
                                  Bailey James @Phaedrux
                                  last edited by

                                  @Phaedrux I don't have anything connected to the Z axis drivers currently

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                                  • Phaedruxundefined
                                    Phaedrux Moderator @Bewaren
                                    last edited by Phaedrux

                                    @Bewaren said in Duet2 Firmware Upgrade Issue:

                                    I'm now getting a issue with Driver 2

                                    'Warning: Driver 2 warning: phase A may be disconnected, phase B may be disconnected'

                                    M584 X0 Y1 Z2 E3 ; set drive mapping

                                    @Bailey-James said in Duet2 Firmware Upgrade Issue:

                                    @Phaedrux I don't have anything connected to the Z axis drivers currently

                                    Yes, but your error is coming from the driver defined for Z which you don't have anything connected to, which is what the error is telling you.

                                    Z-Bot CoreXY Build | Thingiverse Profile

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