BL Probe deploys when Scanning Z probe cycles run
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Hello all,
I'm looking for some assistance setting up my Scanning Z Probe. The trouble comes when attempting to run the M558.1 calibration. The calibration runs successfully; however, the BL touch probe deploys at the same time and leaves the BL probe in error status at completion of the calibration routine. This behavior persists despite specifying the K1 parameter with M558.1 (M558.1 K1 S1.5 example command) where the BL is configured as K0 and the SZP as K1. Similarly, when running the bed mesh (G29 K1) the BL probe deploys which will damage the probe as the pin drags across the bed.While I could write a reset for the BL probe into a macro for M558.1 to solve the first issue I'm not aware of how I could similarly edit the G29 routine and this doesn't really address the root issue.
Any thoughts or advice is appreciated.
Firmware 3.5.2
Hardware is as follows;
Controller: Fysetc Big Dipper (mimics Duet Mini 3 5+)
Toolboard: Mellow Fly RRF address 124
Probes: Genuine BL Touch, Duet SZP (address 120)Config file and M122 outputs:
M586 P0 S1 ; enable HTTP
M586 P1 S0 ; disable FTP
M586 P2 S0 ; disable TelnetG4 S1 ;WAIT FOR TOOLBOARD CONNECTION
; Drives
M569 P0 S0 ; physical drive 0.0 goes forwards
M569 P1 S0 ; physical drive 0.1 goes forwards
M569 P2 S0 ; physical drive 0.2 goes REVERSE
M569 P3 S0 ;"
M569 P4 S0 ;"M569 P124.0 S1 ; physical drive 121.0 goes forwards
M584 X0 Y1 Z2:3:4 E124.0 ; set drive mapping
M671 X-68:290:650 Y 10:650:10 S150 ;SET LEADSCREW LOCATION FOR COMPENSATION
M350 Z16 I0 ; configure microstepping without interpolation
M350 X16 Y16 e16 I1 ; configure microstepping with interpolation
M92 X81.08 Y81.08 Z1600 E690.00 ; set steps per mm
M566 X1750 Y1250 Z26.00 E300.00 ; set maximum instantaneous speed changes (mm/min)
M203 X20000.00 Y20000.00 Z2500.00 E7000.00 ; set maximum speeds (mm/min)
M201 X3200.00 Y3000.00 Z400.00 E8000.00 ; set accelerations (mm/s^2)
M906 X1550 Y1550 Z1350 E1000 I30 ; set motor currents (mA) and motor idle factor in per cent ;X1400 Y1400 Z1000 E1000 I30
M84 S30 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; set axis minima
M208 X605 Y561 Z255 S0 ; set axis maxima; Endstops
M574 X1 S1 P"124.io2.in" ; configure active-high endstop for low end on X via pin io0.in
M574 Y1 S1 P"io0.in" ; configure active-high endstop for low end on Y via pin io1.in
;M574 Z2 S1 ; configure Z-probe endstop for high end on Z; Z-Probe
M950 S0 C"124.io0.out" ; create servo pin 0 for BLTouch
M558 k0 P9 C"^124.io0.in" H15 F120 T10000 R0.2 ; set Z probe type to bltouch and the dive height + speeds
G31 P500 X26 Y-8.5 Z2.58 ; set Z probe trigger value, offset and trigger height
;M557 X20:600 Y15:600 S40 ; define mesh gridM280 P0 S60 ; BLtouch - toggle switch mode
G4 P1000 ; wait 1 second
M280 P0 S120 ; BLtouch toggle self-test; Scanning Z probe
M558 K1 P11 C"120.i2c.ldc1612" F36000 T36000 ; configure SZP as probe 1, type 11, on CAN address 120
M308 A"SZP coil" S10 Y"thermistor" P"120.temp0" ; thermistor on SZP coil
G31 K1 Z2 Y-17 ; define probe 1 offsets and trigger heightm558.2 k1 S15 R137084
M557 X50:200 Y50:250 S10 ; Define mesh grid for probe 1 (overwrites probe 0 mesh grid)
; Heaters
M308 S0 P"temp1" Y"thermistor" T120000 B4138 ; configure sensor 0 as thermistor on pin temp0
M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
M140 H0 ; map heated bed to heater 0
M143 H0 S120 ; set temperature limit for heater 0 to 120CM308 S1 P"124.temp0" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin 121.temp0
M950 H1 C"124.out0" T1 ; create nozzle heater output on 121.out0 and map it to ;sensor 1
M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
M143 H1 S280 ; set temperature limit for heater 1 to 280C;routine for PID calibration
;M308 S1 P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin 121.temp0
;M950 H1 C"out0" T1 ; create nozzle heater output on 121.out0 and map it to sen
;M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
;M143 H1 S280;end routine
; Fans
;M950 F0 C"laser" ; create fan 0 on pin 121.out1 and set its frequency
;M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned offM950 F0 c"124.out2" Q250
M106 P0 S0 h-1M950 F1 C"vfd" Q500 ; create fan 1 on pin vfd and set its frequency
M106 P1 S1 H-1m950 F2 C"124.OUT1" Q250
M106 P2 T35 S255 H1 ; set fan 1 value. Thermostatic control is turned off; Tools
M563 P0 D0 H1 F0 ; define tool 0
G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0CM572 D0 S0.035 ;SET PRESSURE ADVANCE
M955 P124.0 I02 ; ;ACCELEROMETER
M308 S2 P"124.temp1" Y"thermistor" A"Chamber Temperature" T100000 B4092 ;CHAMBER TEMP
M593 P"zvd" F45 ;CONFIGURE INPUT SHAPING
M591 D0 P1 C"io1.in" s1 ;CONFIGURE FILAMENT SWITCH
; Custom settings are not defined
; Miscellaneous
M501 ; load saved parameters from non-volatile memory
M911 S22 R22.5 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
T0 ; select first tool8/4/2024, 11:25:47 AM: m122 b124: Diagnostics for board 124:
Duet FLY36RRF firmware version 3.5.2 (2024-06-13 00:56:43)
Bootloader ID:
All averaging filters OK
Never used RAM 218224, free system stack 436 words
Tasks: Move(3,nWait 7,0.0%,132) HEAT(2,nWait 6,0.2%,116) CanAsync(5,nWait 4,0.0%,64) CanRecv(3,nWait 1,0.0%,356) CanClock(5,nWait 1,0.0%,334) ACCEL(3,nWait 6,0.0%,52) TMC(2,delaying,2.3%,52) MAIN(1,running,95.7%,434) IDLE(0,ready,0.0%,26) USBD(2,blocked,0.0%,150) AIN(2,delaying,1.8%,248), total 100.0%
Owned mutexes:
Last reset 00:39:32 ago, cause: power up or brownout
Last software reset data not available
Driver 0: pos 0, 690.0 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 55332, writes 0, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0
Moves scheduled 0, completed 0, in progress 0, hiccups 0, segs 0, step errors 0, maxLate 0 maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0, ebfmin 0.00 max 0.00
Peak sync jitter -11/18, peak Rx sync delay 339, resyncs 0/0, no timer interrupt scheduled
VIN voltage: min 23.7, current 23.7, max 23.8
MCU temperature: min 29.0C, current 39.3C, max 39.8C
Last sensors broadcast 0x00000006 found 2 11 ticks ago, 0 ordering errs, loop time 0
CAN messages queued 72644, send timeouts 0, received 23597, lost 0, errs 0, boc 0, free buffers 38, min 38, error reg 0
dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
Accelerometer: LIS3DH, status: 00
8/4/2024, 11:25:52 AM: m122 b120: Diagnostics for board 120:
Duet SZP firmware version 3.5.2 (2024-06-10 13:23:26)
Bootloader ID: SAMC21 bootloader version 2.10 (2023-11-16)
All averaging filters OK
Never used RAM 14000, free system stack 110 words
Tasks: HEAT(2,nWait 6,0.1%,132) CanAsync(5,nWait 4,0.0%,54) CanRecv(3,nWait 1,0.0%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,71.8%,420) IDLE(0,ready,0.0%,26) AIN(2,nWait 2,28.0%,72), total 100.0%
Owned mutexes:
Last reset 00:39:36 ago, cause: power up
Last software reset data not available
Peak sync jitter -3/8, peak Rx sync delay 214, resyncs 0/0, no timer interrupt scheduled
VIN voltage: min 5.0, current 5.0, max 5.0
MCU temperature: min 23.2C, current 27.6C, max 27.8C
Last sensors broadcast 0x00000400 found 1 157 ticks ago, 0 ordering errs, loop time 0
CAN messages queued 4737, send timeouts 0, received 7670, lost 0, errs 0, boc 0, free buffers 18, min 18, error reg 0
Accelerometer: LIS2DW, status: 00
Inductive sensor: raw value 36950956, frequency 3.44MHz, current setting 15, ok
I2C bus errors 0, naks 0, contentions 0, other errors 0
8/4/2024, 11:25:58 AM: m122: === Diagnostics ===
RepRapFirmware for Duet 3 Mini 5+ version 3.5.2 (2024-06-11 17:14:16) running on Duet 3 Mini5plus WiFi (standalone mode)
Board ID: 6KSY8-12401-8D3J0-4018D-MYS0Z-ZKUV9
Used output buffers: 3 of 40 (34 max)
=== RTOS ===
Static ram: 103368
Dynamic ram: 123036 of which 24 recycled
Never used RAM 14988, free system stack 202 words
Tasks: NETWORK(2,nWait 7,14.1%,240) LASER(5,nWait 7,0.0%,269) HEAT(3,nWait 6,0.0%,331) Move(4,nWait 6,0.0%,355) CanReceiv(6,nWait 1,0.1%,796) CanSender(5,nWait 7,0.0%,336) CanClock(7,delaying,0.0%,348) TMC(4,nWait 6,1.4%,101) MAIN(1,running,83.6%,665) IDLE(0,ready,0.0%,29) AIN(4,delaying,0.8%,259), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 00:39:42 ago, cause: power up
Last software reset at 2024-08-03 17:30, reason: User, Gcodes spinning, available RAM 11452, slot 1
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00487000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
MCU revision 0, ADC conversions started 2382981, completed 2382981, timed out 0, errs 0
MCU temperature: min 35.0, current 35.6, max 36.1
Supply voltage: min 23.9, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Events: 0 queued, 0 completed
Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 53734, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 53734, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 53735, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 53735, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 53734, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 5: standstill, SG min 0, read errors 0, write errors 0, ifcnt 10, reads 53735, writes 0, timeouts 0, DMA errors 0, CC errors 0
Driver 6: standstill, SG min 0, read errors 0, write errors 0, ifcnt 10, reads 53735, writes 0, timeouts 0, DMA errors 0, CC errors 0
Date/time: 2024-08-04 11:25:57
Cache data hit count 4294967295
Slowest loop: 26.18ms; fastest: 0.16ms
=== Storage ===
Free file entries: 20
SD card 0 detected, interface speed: 22.5MBytes/sec
SD card longest read time 3.6ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, max steps late 0, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 0.00
no step interrupt scheduled
Moves shaped first try 0, on retry 0, too short 0, wrong shape 0, maybepossible 0
=== DDARing 0 ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== DDARing 1 ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Movement locks held by null, null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
File2 is idle in state(s) 0
Queue2 is idle in state(s) 0
Q0 segments left 0, axes/extruders owned 0x0000803
Code queue 0 is empty
Q1 segments left 0, axes/extruders owned 0x0000000
Code queue 1 is empty
=== Filament sensors ===
check 0 clear 11605462
Extruder 0 sensor: ok
=== CAN ===
Messages queued 5336, received 16598, lost 0, errs 0, boc 0
Longest wait 7ms for reply type 6024, peak Tx sync delay 6, free buffers 26 (min 25), ts 2955/2955/0
Tx timeouts 0,0,0,0,0,0
=== Network ===
Slowest loop: 200.31ms; fastest: 0.01ms
Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
HTTP sessions: 1 of 8
=== WiFi ===
Interface state: active
Module is connected to access point
Failed messages: pending 0, notrdy 4, noresp 1
Firmware version 2.1.0
MAC address bc:ff:4d:e6:b1:78
Module reset reason: Hardware watchdog, Vcc 3.39, flash size 2097152, free heap 43044
WiFi IP address 192.168.1.111
Signal strength -59dBm, channel 4, mode 802.11n, reconnections 0
Clock register 00002002
Socket states: 0 0 0 0 0 0 0 0 -
@Invader_Zoom Do you have any deployprobe files in your sys directory? If so what is in them?
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Yes, I am using deployprobe.g and retractprobe.g subroutines containing a single M280 command each.
M280 P0 s10 extend
M280 P0 S90 retract
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@Invader_Zoom Try renaming those to deployprobe0.g and retractprobe0.g at the moment I think it may be running your current files for both probes.
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@gloomyandy Renaming the deploy and retract subroutines solved my issue. Thank you for your help.
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