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    G30 during G28 issue

    Scheduled Pinned Locked Moved Solved
    My Duet controlled machine
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    • dc42undefined
      dc42 administrators @Leonard03
      last edited by

      @Leonard03 thanks for your feedback.

      Please try the new frmware build at https://www.dropbox.com/scl/fo/xk6t4cibc602j0s3qmp48/AGouwT4mDySsLdBItGjDUcM?rlkey=k8j1rrfx18ixoyvizvs0hbehz&dl=0 and report whether it is better/same/worse.

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

      Leonard03undefined 1 Reply Last reply Reply Quote 0
      • Leonard03undefined
        Leonard03 @dc42
        last edited by Leonard03

        @dc42 Thank you for the update
        Sadly, is still the same. 2mm shift in X-
        The left is without M556
        The right with M556
        20250519_173608.jpg

        droftartsundefined 1 Reply Last reply Reply Quote 0
        • droftartsundefined
          droftarts administrators @Leonard03
          last edited by droftarts

          @Leonard03 Thanks for your continued testing. Was the calibration cube on the right caused by a pause/resume, or by a "power failure" (please explain how you did this!)?

          I've just been testing this too, and find that I was able to provoke the bug when using G30 and skew compensation in 3.6.0-rc.3, but that it works correctly in 3.6.0-rc.3+1.

          With one bug resolved, I think there's something else going on when you pause and/or 'simulate a power failure', then resume/resurrect. It would seem that skew compensation is not applied, or the position is reset. When a print is paused, or there is a power failure, RRF creates a 'resurrect.g' file in the /sys folder, which is then used to return the tool to the correct position a resume the job. It could be that it is not applying skew compensation at the correct point during this.

          Could you:

          1. Start a print normally.
          2. Pause the print, or 'simulate a power failure'
          3. Send M556 to show the current skew compensation setting
          4. Copy the 'resurrect.g' file from /sys and post it
          5. resume the print and see if it shifts
          6. Post your pause.g, resume.g and the output of M556 (in case it has changed, or isn't being applied any longer)

          Thanks!

          Ian

          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

          Leonard03undefined 1 Reply Last reply Reply Quote 0
          • Leonard03undefined
            Leonard03 @droftarts
            last edited by Leonard03

            @droftarts I also thank you for the continued help with this issue
            Those are fair questions, and I will split my answer in two parts:
            How it works and what actually happens

            My printer has two power plugs (one and a half actually 😆)
            First, is the main power plug. Is the power plug for the UPS. Then, in the UPS is plugged the printer's ATX power supply and from it the Duet and DueX are powered.
            The second, is a phone charger. A 5V 500mA power supply that serves as a power feedback.
            From it I powering a 5V simple relay. The switching contacts of that relay (two of them) are wired to duex.e3stop

            On that input, I have defined two triggers in config.g:

            M950 J2 C"^duex.e3stop"										; Input 1 uses e2stop pin, pullup enabled (power feedback for UPS)
            M581 P2 T2 S1 R1											; external trigger 1, trigger occurs on the inactive-to-active edge, trigger at any time (UPS Backup power)
            M581 P2 T3 S0 R2											; external trigger 1, trigger occurs on the active-to-inactive edge, trigger only when not printing from SD card (AC back, resume prompt)
            

            Trigger2.g senses if that relay has power to it, so if a print is in progress, it will be executed.
            It's macro is this:

            ; Called when mains power is intrerrupted and UPS battery is in use
            
            M118 S"Running on backup power !" L0	; display warning message when using UPS battery
            M25										; Pause printing process
            M400
            M0										; cancel current job
            M568 P0 A0								; turn off nozzle heater
            
            G91
            ; G1 Z-5
            
            M18 X Y E0								; Disable steppers to conserve battery power, but leave Z stepper energized
            
            M552 S-1								; Disable Wi-Fi adapter
            
            if global.MMUmode = true
            	echo >>"0:/sys/MMU Control/errLog.txt" state.time, ",", "Blackout occured", "Z="^move.axes[2].machinePosition-5	; -5 is the Z lift in pause.g
            	M18 UVW								; disable MMU steppers
            

            If the power goes out, the printer will continue to run on the UPS's battery, in the end safely shutting down the printer.
            From what I intended to happen.. is as follows:

            • Show a dialog that the power is lost (really this never shows because of the pause dialog that is shown after that; not a problem)

            • list itemPause the print (using the M25), stage that the ressurect is created (if I'm not mistaken)

            • Cancel the print (M0) (stop.g behaves a bit differently in this case, compared with a normal job end, I will describe it later)

            • Turn off the nozzle heater, for a safe shutdown if the power is not restored in time

            • Disable X, Y and extruder steppers to conserve power

            • Disable the WiFi adapter (if the power goes out, the router will be also powered off, so to prevent the board from continuing to search for the network and flood the PanelDue interface with dialogs complaining that it can't find the network)

            • If the MMU is enabled, disable its steppers as well (to conserve power) and log this event to a file.

            As stated above, regarding the M0 or stop.g in this scenario:

            ; stop.g
            ; called when M0 (Stop) is run (e.g. when a print from SD card is cancelled)
            ;
            ; generated by RepRapFirmware Configuration Tool v3.2.0 on Tue Dec 29 2020 16:23:44 GMT+0200 (Eastern European Standard Time)
            
            G91
            G1 Z10 F6000										; lift z by 10mm
            
            if global.MMUmode = false
            	M221 S100 D0
            	T-1
            	M106 P0 S0
            else
            	M221 S100 D0
            	M221 S100 D1
            	M221 S100 D2
            	M221 S100 D3
            	M221 S100 D4
            
            	M572 D{state.currentTool} S0
            	G1 E3 F800
            
            	M106 P0 S0
            
            	T-1
            	M98 P"0:/sys/MMU Control/moveIdler.g" S5
            	M98 P"0:/sys/MMU Control/counterCheck.g"
            G90
            G0 X0 Y300 F3600																; go to the back left corner
            
            M18 X Y E0																		; disable X, Y and E steppers
            
            if global.MMUmode = true														; if MMU is enabled
            	M18 U V W																	; disable MMU steppers
            	if state.status = "processing"
            		echo >>"0:/sys/MMU Control/errLog.txt" state.time, ",", "Print complete!"
            
            M568 P0 A0																		; turn off tool 0 heater
            
            if sensors.gpIn[1].value = 1
            	M140 S-273.15																; turn off bed heater
            	if move.axes[2].machinePosition < 150
            		G1 Z150
            	M400
            	M18 Z
            	M81 S1																		; turn off ATX after nozzle cooldown
            

            In normal operation, at the end of the print, I lift the nozzle above the print, reset extrude factor override percentage just in case it was modified during the print, disable pressure advance, and an attempt to give the filament end a nice, sharp tip , so it can be loaded easily next time, then unload the filament.
            Then move the bed forward, park the tool carriage to endstop, disable the MMU steppers and turn off the nozzle heater.

            Now, if the power feedback says that there is no mains power (the charger, relay and duex.e3stop input), keep the bed at the print temperature, so the print will not detach from the print surface, and don't rise the Z too much but keep the Z steppers energized, so they keep their positions set by the G32 at the start of the print. Also, keep the power supply turned on (opposite to the M81 S1 if there are no power related issues)

            After this is completed, the printer will wait until the power is recovered. The UPS cand provide almost one and a half time to resume.

            How I resume after a power failure:
            If the printer is still powered on using the UPS and the mains power comes back, the phone charger will receive power again, turning on the relay. The relay, will tell the bord that power is back, so in the rising edge of the duex.e3stop will use the trigger3.g:

            ; Called when mains power is back
            
            M118 S"Back on AC power" L0									; display warning message when using UPS battery
            M552 S1														; Enable Wi-Fi adapter again
            
            if fileexists("0:/sys/resurrect.g")
            	M291 P"Back on AC power. Resume print ?" R"UPS Status" S3	; Prompt if printing can be resumed
            	M916														; Resume print after power loss
            
            	if global.MMUmode = true
            		echo >>"0:/sys/MMU Control/errLog.txt" state.time, ",", "Blackout recovered"
            

            Now that everything is good to go:

            • Reenable the WiFi module and reconect to the router

            • Search for the ressurrect.g and if it is found, ask if the print can be resumed.

            • If I confirm, run the M916 command to go ahead.

            Resurrect-prologue.g is this:

            M17 E0
            
            G28 X Y						; home X and Y, hope that Z hasn't moved
            if global.MMUmode = true
            	M98 P"0:/sys/MMU Control/homeMMU.g"
            
            G91
            G1 Z-5
            
            • Reenable the extruder stepper (this is a very old bug in RRF. I can't use the MMU to load filament if the extruder stepper is disabled, so enable it before anything else)
            • Home X and Y axis (Z axis has never been disabled)
            • Rehome the MMU (UVW axis)
            • Lower the Z axis (I can't remember exactly why this is necessary, but it works)
              And after, RRF executes ressurrect.g.

            Until now, is anything that seems out of place?

            Pause.g is this, but is complicated:

            ; pause.g
            ; called when a print from SD card is paused
            ;
            ; generated by RepRapFirmware Configuration Tool v3.2.0 on Tue Dec 29 2020 16:23:44 GMT+0200 (Eastern European Standard Time)
            
            if global.MMUmode = false
            	M83							; relative extruder moves
            	G10
            	G91							; relative positioning
            	G1 Z5 F600					; lift Z by 5mm
            	G90							; absolute positioning
            	G1 X0 Y0 F6000				; go to X=0 Y=0
            	M591 D0 S0
            
            else
            	if state.status != "paused"
            		echo >>"0:/sys/MMU Control/errLog.txt" state.time, ",", "Pause"
            
            	set global.pause = false
            
            	if state.status = "pausing"
            		if global.errQueue[#global.errQueue-1] = "SELECTOR_CANNOT_HOME" || global.errQueue[#global.errQueue-1] = "SELECTOR_CANNOT_MOVE" || global.errQueue[#global.errQueue-1] = "INSPECT_FINDA"
            			M18 U
            		elif global.errQueue[#global.errQueue-1] = "PULLEY_CANNOT_MOVE"
            			M18 V
            		elif global.errQueue[#global.errQueue-1] = "IDLER_CANNOT_HOME" || global.errQueue[#global.errQueue-1] = "IDLER_CANNOT_MOVE"
            			M18 W
            
            	if global.spoolJoin = false && global.loadNext = false
            		M83						; relative extruder moves
            		G10
            		G91						; relative positioning
            		G1 Z5 F600				; lift Z by 5mm
            		G90						; absolute positioning
            		G1 X0 Y0 F6000			; go to X=0 Y=0
            		M98 P"0:/sys/MMU Control/moveIdler.g" S5
            
            	elif global.spoolJoin = true
            		if global.loadNext = false
            			M83					; relative extruder moves
            			G10
            			G91					; relative positioning
            			G1 Z5 F600			; lift Z by 5mm
            			G90					; absolute positioning
            			G1 X0 Y0 F6000		; go to X=0 Y=0
            			M98 P"0:/sys/MMU Control/moveIdler.g" S5
            		else
            			M83
            			G10					; retract
            			G91					; relative positioning
            			G1 Z5				; lift
            			G90
            			G1 X310 Y0			; go outside bed
            			G11					; unretract
            
            			if state.currentTool = #tools - 1
            				T0
            			else
            				T{state.currentTool + 1}
            			
            			if global.errQueue[#global.errQueue-1] = null
            				G1 E30 F300		; purge air from the nozzle
            				G10				; retract
            

            During normal operation, or at least for now, commands after line 21 are not used
            Pausing and resuming a print (not a power failure) works without problems, and the skew compensation has its normal value.
            M556 is defined only in config.g, and for testing purposes I comment or uncomment it.
            So I can do a power failure simply by unplugging the charger from its mains socket

            Both cubes in the photo above, had a "power failure", the only difference between them is the skew compensation

            A side note: the ressurect.g contains a resume command, but it behaves like a M24 P0 because it don't run the resume.g

            1 Reply Last reply Reply Quote 0
            • Leonard03undefined
              Leonard03
              last edited by

              Started now a print. Pause and resume works as expected, skew compensation is active

              Axis compensations - XY: 0.00690, YZ: 0.00000, ZX: 0.00000
              

              Inducing a "power failure" and resuming:

              Axis compensations - XY: 0.00690, YZ: 0.00000, ZX: 0.00000
              

              So skew compensation is still active and correctly applied, but the shift is there

              dc42undefined 1 Reply Last reply Reply Quote 1
              • dc42undefined
                dc42 administrators @Leonard03
                last edited by

                @Leonard03 please post your resurrect.g file (after pausing) and your resurrect-prolog.g file.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                Leonard03undefined 1 Reply Last reply Reply Quote 0
                • Leonard03undefined
                  Leonard03 @dc42
                  last edited by

                  @dc42 This a ressuregt.g after a print that had a shift, that I cancelled

                  ; Resume printing file "0:/gcodes/xyzCalibration_cube,0.2mm,PLA,Anycubic PLA Pantone Spring Leaf,25m.gcode" after print paused at 2025-05-19 21:06
                  M140 P0 S60.0
                  G29 S1
                  M568 P0  A0 S210 R170
                  M568 P1  A0 S210 R170
                  M568 P2  A0 S210 R170
                  M568 P3  A0 S210 R170
                  M568 P4  A2 S210 R170
                  G21
                  M98 P"resurrect-prologue.g" X144.359 Y141.863 Z3.400 U57.000 V0.000 W17.998
                  M290 R0 X0.000 Y0.000 Z0.000 U0.000 V0.000 W0.000
                  M205 X10.00 Y10.00 Z0.40 U1.00 V4.00 W0.10
                  ; Workplace coordinates
                  G10 L2 P1 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P2 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P3 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P4 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P5 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P6 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P7 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P8 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  G10 L2 P9 X0.00 Y0.00 Z0.00 U0.00 V0.00 W0.00
                  M486 S-1
                  T4
                  G54
                  M106 S0.99
                  M116
                  G92 E1.83369
                  M83
                  G94
                  G17
                  M23 "0:/gcodes/xyzCalibration_cube,0.2mm,PLA,Anycubic PLA Pantone Spring Leaf,25m.gcode"
                  M26 S54031
                  G0 F6000 Z5.400
                  G0 F6000 X144.359 Y141.863 U57.000 V0.000 W17.998
                  G0 F6000 Z3.400
                  G1 F1871.0 P0
                  M204 P1000.0 T2000.0
                  G21
                  M106 P0 S0.99
                  M302 P0
                  M24
                  
                  

                  And this is resurrect-prologue.g

                  M17 E0
                  
                  G28 X Y						; home X and Y, hope that Z hasn't moved
                  if global.MMUmode = true
                  	M98 P"0:/sys/MMU Control/homeMMU.g"
                  
                  G91
                  G1 Z-5
                  

                  Please have a look at this description

                  @Leonard03 said in G30 during G28 issue:

                  Reenable the extruder stepper (this is a very old bug in RRF. I can't use the MMU to load filament if the extruder stepper is disabled, so enable it before anything else)
                  Home X and Y axis (Z axis has never been disabled)
                  Rehome the MMU (UVW axis)
                  Lower the Z axis (I can't remember exactly why this is necessary, but it works)
                  And after, RRF executes ressurrect.g.
                  Until now, is anything that seems out of place?

                  droftartsundefined 1 Reply Last reply Reply Quote 0
                  • droftartsundefined
                    droftarts administrators @Leonard03
                    last edited by droftarts

                    @Leonard03 We are homing in on a bug, related to applying the skew compensation when axes are homed at the same time. In 3.5.4, this worked correctly, but now doesn't seem to.

                    The difference is in how the skew compensation is applied. "resurrect-prologue.g" needs to run just X and Y homing, it runs home X, then home Y. Skew compensation is applied to X once Y is homed. In homeall.g, X and Y are homed at the same time, but doesn't seem to apply skew compensation until after the first move, which is when the axes move to resume the print, so will be in the wrong place.

                    A workaround for now is to modify your homeall.g so it homes X, then Y, rather than both at the same time. Either replace the X and Y homing lines with the lines from homex.g and homey.g, or as @fcwilt mentioned earlier in this thread, replace them by calling the homex.g and homey.g macros, eg

                    M98 P"homex.g"
                    M98 P"homey.g"
                    

                    Then it should resurrect in the same place. @dc42 is working on a fix.

                    Ian

                    Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                    Leonard03undefined 2 Replies Last reply Reply Quote 1
                    • Leonard03undefined
                      Leonard03 @droftarts
                      last edited by

                      @droftarts Interesting point of view. All right, I'm trying this now and report back

                      1 Reply Last reply Reply Quote 0
                      • Leonard03undefined
                        Leonard03 @droftarts
                        last edited by Leonard03

                        @droftarts Tried the suggested workaround
                        Umm.. I don't know what to say
                        I've modified the homeall.g from:

                        ; homeall.g
                        ; called to home all axes
                        ;
                        ; generated by RepRapFirmware Configuration Tool v3.2.0 on Tue Dec 29 2020 16:23:44 GMT+0200 (Eastern European Standard Time)
                        
                        G91							; relative positioning
                        G1 H2 Z5 F6000				; lift Z relative to current position
                        G1 H1 X-320 Y-306 F1800		; move quickly to X and Y axis endstops and stop there (first pass)
                        G1 X5 Y5 F6000				; go back a few mm
                        G1 H1 X-320 Y-306 F240		; move slowly to X and Y axis endstops once more (second pass)
                        G1 H1 Z-405 F240			; move Z down stopping at the endstop
                        
                        G90							; absolute positioning
                        G1 Z5
                        G1 X{(310/2)-sensors.probes[0].offsets[0]} Y{(310/2)-sensors.probes[0].offsets[1]} F6000
                        G30
                        G1 X0 Y0
                        
                        if global.MMUmode = true
                        	M98 P"0:/sys/MMU Control/homeMMU.g"
                        

                        to

                        ; homeall.g
                        ; called to home all axes
                        ;
                        ; generated by RepRapFirmware Configuration Tool v3.2.0 on Tue Dec 29 2020 16:23:44 GMT+0200 (Eastern European Standard Time)
                        
                        M98 P"homex.g"
                        M98 P"homey.g"
                        G1 H1 Z-405 F240			; move Z down stopping at the endstop
                        
                        G90							; absolute positioning
                        G1 Z5
                        G1 X{(310/2)-sensors.probes[0].offsets[0]} Y{(310/2)-sensors.probes[0].offsets[1]} F6000
                        G30
                        G1 X0 Y0
                        
                        if global.MMUmode = true
                        	M98 P"0:/sys/MMU Control/homeMMU.g"
                        

                        Is an improvement, still shifted but way less then before
                        20250520_210957.jpg
                        From left to right: No skew compensation, in homeall.g homing both X and Y at the same time and the last is calling independent macros in homeall.g
                        The shift is reduced from 2mm to 1mm

                        Update: if during a pause I rehome X or Y the print resume at the right position

                        droftartsundefined 1 Reply Last reply Reply Quote 0
                        • droftartsundefined
                          droftarts administrators @Leonard03
                          last edited by

                          @Leonard03 Okay, thanks for testing! Back to the drawing board...

                          Ian

                          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                          Leonard03undefined 1 Reply Last reply Reply Quote 0
                          • Leonard03undefined
                            Leonard03 @droftarts
                            last edited by

                            @droftarts sorry... 😐

                            droftartsundefined 1 Reply Last reply Reply Quote 0
                            • droftartsundefined
                              droftarts administrators @Leonard03
                              last edited by

                              @Leonard03 Are you still using RRF 3.6.0-rc3+2 firmware?

                              Ian

                              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                              Leonard03undefined 1 Reply Last reply Reply Quote 0
                              • Leonard03undefined
                                Leonard03 @droftarts
                                last edited by

                                @droftarts Yes, 3.6.0-rc.3+2 (2025-05-19 11:46:09)

                                dc42undefined 1 Reply Last reply Reply Quote 0
                                • dc42undefined
                                  dc42 administrators @Leonard03
                                  last edited by

                                  @Leonard03 please try this firmware.

                                  Duet2CombinedFirmware.bin

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  Leonard03undefined 1 Reply Last reply Reply Quote 1
                                  • Leonard03undefined
                                    Leonard03 @dc42
                                    last edited by

                                    @dc42 Thank you very much! I confirm that this issue is solved! Works very ewll 😊
                                    Also, thank you to everyone for every input and all the support !

                                    1 Reply Last reply Reply Quote 0
                                    • Leonard03undefined Leonard03 has marked this topic as solved
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