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    Strange z offset after printing.

    Scheduled Pinned Locked Moved
    Tuning and tweaking
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    • lolmoduleundefined
      lolmodule
      last edited by

      Ok. I re did my Z0 and my probe trigger height just to make sure everything was ok. Which is why my trigger height is a tad different than before. I printed a calibration cube and put in the commands you suggested @dc42 this is the results:

      G10 P0
      Tool 0 offsets: X0.00 Y0.00 Z0.00, active/standby temperature(s): 0.0/0.0

      M290
      Baby stepping offset is 0.000mm

      G31 T5
      Threshold 500, trigger height 2.19, offsets X0.0 Y-40.0

      Everything looks good right?


      https://gyazo.com/e708fbecbdc5baf48ebf945f10f2fadf


      Notice the commanded position and the readout in the top right.

      I tried the suggestion by @Phaedrux and manually entered that move command ( verified Z 0, sent the G1 Z+10.00 F20000, then back to 0 and it was fine.)

      I have no idea whats going on. I haven't updated to 2.0 yet but I think it might fix whatever issue I might be having but I will wait to see what you all have to say.

      I really do appreciate the time you guys ( even though it may not be much time) put into helping me out.

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      • dc42undefined
        dc42 administrators
        last edited by dc42

        It looks to me that you have some sort of bed compensation in use that is causing a 0.4mm adjustment. Please run M122 and see what the "Bed compensation in use" field reports.

        Another possibility is that the GCode file you printed uses a M206 commands to offset the Z axis.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

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        • lolmoduleundefined
          lolmodule
          last edited by

          No bed compensation: https://gyazo.com/9193b8b3715ef0341789c3e7e04b06f3

          Checked the last few files and there are no M206 commands. My start script does have an M207 that has a Z0.4 in it.

          M207 S8.5 F4000 T1800 Z0.4 ; setup firmware retraction

          Could that be it? like I mention earlier I am not fully up on Gcode so when my friend gave me the scripts for FW retraction I just used them. Is there a reason to have a Z0.4 in the FW retraction?

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            The Z parameter for firmware retraction controls Z hop.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • lolmoduleundefined
              lolmodule
              last edited by

              Ah ok. I dont know what the issue could be then... Everything appears to be setup right.

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Might be time to give 2.0 a try.

                If that doesn't work, you could try backing up all your existing config files from the /sys folder and then starting fresh with a new config bundle generated by the RepRap configurator. It would likely take some tuning and adjusting to get it working properly for your printer again, as the configurator really provides more of a starting point than a final working config. This would also give you a chance to dig into RepRap firmware and gcode a little more which is really quite powerful once you get into it.

                I still suspect some binding or skipped steps occasionally, can you verify what the rated current for your z stepper is and whether you're running it at close to 85% of rated?

                Z-Bot CoreXY Build | Thingiverse Profile

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                • deckingmanundefined
                  deckingman
                  last edited by

                  I thought that the 20,000 mm/min (333mm/sec) for the Z move in the end gcode was way too fast (which it is) but then it'll be limited to 1,000 because that's what is in config.g.

                  Like Phaedrux, I'm also inclined to think it's binding or skipping steps. You could try lower Z acceleration.

                  Ian
                  https://somei3deas.wordpress.com/
                  https://www.youtube.com/@deckingman

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                  • lolmoduleundefined
                    lolmodule
                    last edited by

                    It may be that, but like I posted above. I ran that high Accel z move manually and it returned to 0 no problem. ( But that doesn't mean it isn't the cause)

                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @lolmodule
                      last edited by

                      @lolmodule Just a theory, but at the end of the print the motor may be hot and may not respond the same.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      lolmoduleundefined 1 Reply Last reply Reply Quote 0
                      • lolmoduleundefined
                        lolmodule @Phaedrux
                        last edited by lolmodule

                        @phaedrux that's possible. I'm running dual leadscrew steppers for my Z so I didn't think it could be that but it's definitely not out of the realm of possibility.

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                        • lolmoduleundefined
                          lolmodule
                          last edited by

                          I updated to 2.0. printed a calibration cube. removed the print and sent the head to X150 Y150 Z10 ( 10mm above the center of my bed) and this is the result...

                          https://gyazo.com/384ec6ddfaa195b510a2755408a18a8c


                          No more strange offset after a print!

                          Thanks to everyone for all the help and tips!

                          1 Reply Last reply Reply Quote 1
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