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    Object got knocked over?

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    • Chrissundefined
      Chriss
      last edited by

      Hi *,

      I use my new build (ratrig corexy) to print some extensions for itself. I had to print a temp tower yesterday, the tower got knocked over by the nozzle at 72mm. I heard that grinding noise when the nozzle is to low.. well, I think that you know what I mean. I have other objects, from that printer, which are very close to the designated height. So I do net assume that the steps for z are completely wrong. I use the driver config from the ratrig duet examples.

      I measured the actual traveled distance when I "z-100" and it looked OKish to me. The bed may have raveled one millimeter more than is should, but the top of the lead screw is not flat, so I would not overrate that. And the the problems is not hat the bed travels to much obviously. The only explanation I have now is a inaccurate angle of the leadscrew to the bed. So I remeasured it a couple of times now and it seams very fine to me now.

      Hardware:
      Duet3 6hc Fw: 3.1.1
      Stepper sourced from ratrig, 1.8°
      Frame: Ratrig Rat Rig V-Core V2.0

      Snipit from the config.g

      ;; Drives
      ; XY
      M569 P0.0 S1									; physical drive 0.2 goes backwards - left motor
      M569 P0.2 S1									; physical drive 0.1 goes backwards - right motor
      
      ;Z
      M569 P0.3 S0									; physical drive 1.2 goes backwards - left motor
      M569 P0.4 S0									; physical drive 1.1 goes backwards - right motor
      M569 P0.5 S0									; physical drive 1.0 goes backwards - rear motor
      
      ; Extruder
      M569 P1.0 S0									; Extruder Motor
      
      
      M584 X0.0 Y0.2 Z0.3:0.4:0.5 E1.0				; set drive mapping
      M671 X-31.5:437.4:198.5 Y63:63:440 S30.0        ; Z-Level leadscrews at left (connected to E6(9)) and right (connected to E2) of X axis (S=MaxCorrection)
      
      
      M350 X16 Y16 Z16 E16 I1							; configure microstepping with interpolation
      M92 X80.00 Y80.00 Z400.00 E420.00				; set steps per mm
      M566 X900.00 Y900.00 Z12.00 E120.00				; set maximum instantaneous speed changes (mm/min)
      M203 X30000.00 Y30000.00 Z300.00 E1200.00		; set maximum speeds (mm/min) Z180
      M201 X500.00 Y500.00 Z20.00 E250.00				; set accelerations (mm/s^2)
      M906 X2000 Y2000 Z1000 E600 I30					; set motor currents (mA) and motor idle factor in per cent
      M84 S30                                         ; Set idle timeout
      

      What else should I check?

      Cheers, Chriss

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      • OwenDundefined
        OwenD
        last edited by

        Over extrusion or blobs caused by incorrect retraction or pressure advance could cause that. Only takes a tiny bit of plastic sticking up that the nozzle can hit. If it's in a fast travel move it can easily dislodge a small part, especially if bed adhesion is marginal.
        How smooth is the first layer?

        Chrissundefined 1 Reply Last reply Reply Quote 0
        • Chrissundefined
          Chriss @OwenD
          last edited by

          @OwenD said in Object got knocked over?:

          Well, all of my stinging and extrusion tests came out good.

          How smooth is the first layer?

          The first layer was very flat, even, smooth and looked very good to me. ( I have no picture at the moment and the printer is busy at the moment.)

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          • Chrissundefined
            Chriss
            last edited by

            Here are two pictures from the first layer:
            IMG_20201101_015212.jpg IMG_20201101_015157.jpg

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            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              That looks a bit over extruded but only on that one corner, which could mean the bed isn't very level or flat. Have you done a G29 to map out the bed surface?

              Z-Bot CoreXY Build | Thingiverse Profile

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              • Chrissundefined
                Chriss @Phaedrux
                last edited by

                @Phaedrux

                Which corner do you mean?

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                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  The back right one that looks rough as if the nozzle were too close.

                  Z-Bot CoreXY Build | Thingiverse Profile

                  Chrissundefined 1 Reply Last reply Reply Quote 0
                  • Chrissundefined
                    Chriss @Phaedrux
                    last edited by

                    @Phaedrux

                    Well... yes, maybe. But why should have that impact at a part at 72mm height than? II mean so hard that the nozzle knocked over the part? I have to mention that my temp tower was much smaller than that first layer.

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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Well I didn't see a photo of the failed print, just the first layer and that's what I noticed.

                      Over a long print a small amount of over extrusion can result in quite a bit.

                      I assume you've been through this calibration?

                      https://duet3d.dozuki.com/Guide/Ender+3+Pro+and+Duet+Maestro+Guide+Part+4:+Calibration/40

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Chrissundefined 1 Reply Last reply Reply Quote 0
                      • Chrissundefined
                        Chriss @Phaedrux
                        last edited by

                        @Phaedrux said in Object got knocked over?:

                        I assume you've been through this calibration?

                        Oh yes... I did.. I learned that drill with my CR10 already. 😉

                        Her the bottom of the knocked over print:
                        IMG_20201101_022241.jpg

                        Her the top:
                        IMG_20201101_022221.jpg

                        Cheers, Chriss

                        Stephen6309undefined 1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Well it does look like it got stuck at the blob there.

                          Was this being printed as a temperature tower with varying temps?

                          Z-Bot CoreXY Build | Thingiverse Profile

                          Chrissundefined 1 Reply Last reply Reply Quote 0
                          • Chrissundefined
                            Chriss @Phaedrux
                            last edited by

                            @Phaedrux

                            Yes it was

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              What temp did it fail on?

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                Can you post your full config.g?

                                Did you happen to get a heater fault message?

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • Chrissundefined
                                  Chriss @Phaedrux
                                  last edited by

                                  @Phaedrux 195°

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                                  • Chrissundefined
                                    Chriss @Phaedrux
                                    last edited by

                                    @Phaedrux
                                    I did not get a error message... why?

                                    ; Configuration file for Duet 3 (firmware version 3)
                                    ; executed by the firmware on start-up
                                    ;
                                    ; generated by RepRapFirmware Configuration Tool v3.1.1 on Thu Jun 04 2020 17:41:46 GMT+0200 (Central European Summer Time)
                                    
                                    ; General preferences
                                    G90												; send absolute coordinates...
                                    M83												; ...but relative extruder moves
                                    M550 P"Blimy"									; set printer name
                                    M669 K1											; select CoreXY mode
                                    
                                    ;; Drives
                                    ; XY
                                    M569 P0.0 S1									; physical drive 0.2 goes backwards - left motor
                                    M569 P0.2 S1									; physical drive 0.1 goes backwards - right motor
                                    
                                    ;Z
                                    M569 P0.3 S0									; physical drive 1.2 goes backwards - left motor
                                    M569 P0.4 S0									; physical drive 1.1 goes backwards - right motor
                                    M569 P0.5 S0									; physical drive 1.0 goes backwards - rear motor
                                    
                                    ; Extruder
                                    M569 P1.0 S0									; Extruder Motor
                                    
                                    
                                    M584 X0.0 Y0.2 Z0.3:0.4:0.5 E1.0				; set drive mapping
                                    M671 X-31.5:437.4:198.5 Y63:63:440 S30.0        ; Z-Level leadscrews at left (connected to E6(9)) and right (connected to E2) of X axis (S=MaxCorrection)
                                    
                                    
                                    M350 X16 Y16 Z16 E16 I1							; configure microstepping with interpolation
                                    M92 X80.00 Y80.00 Z400.00 E420.00				; set steps per mm
                                    M566 X900.00 Y900.00 Z12.00 E120.00				; set maximum instantaneous speed changes (mm/min)
                                    M203 X30000.00 Y30000.00 Z300.00 E1200.00		; set maximum speeds (mm/min) Z180
                                    M201 X500.00 Y500.00 Z20.00 E250.00				; set accelerations (mm/s^2)
                                    M906 X2000 Y2000 Z1000 E600 I30					; set motor currents (mA) and motor idle factor in per cent
                                    M84 S30                                         ; Set idle timeout
                                    
                                    ; Axis Limits
                                    M208 X0 Y0 Z0 S1                                ; set axis minima
                                    M208 X380 Y360 Z400 S0                          ; set axis maxima
                                    
                                    ;; Endstops         ##################### TODO
                                    M574 X1 S1 P"!0.io1.in"		;Induktions geber X1=low end   ; configure active-high endstop for low end on X via pin io2.in
                                    M574 Y2 S1 P"!0.io2.in"		;Induktions geber Y2=High end   ; configure active-high endstop for high end on Y via pin io1.in
                                    M574 Z1 S2													; Configure Z-probe endstop for low end on Z
                                    
                                    
                                    
                                    ;; Z-Probe
                                    ; BL Touch:
                                    M950 S0 C"0.io4.out"                         ; create servo pin 0 for BLTouch
                                    M558 P9 C"0.io4.in" H5 F120 T6000          	; set Z probe type to bltouch and the dive height + speeds
                                    G31 P500 X0 Y30 Z2.12		                ; set Z probe trigger value, offset and trigger heigh
                                    
                                    ; IR Probe:
                                    ;M558 P8 C"0.io0.in" H5 F120 T6000			; set Z probe type to unmodulated and the dive height + speeds
                                    ;G31 P500 X0 Y25 Z1.45                       ; set Z probe trigger value, offset and trigger height
                                    ; M564 S0 to disable axis limits.
                                    
                                    ;M557 X10:380 Y40:380 P10:10                     ; Chriss - define mesh grid
                                    M557 X50:350 Y50:350 P3:3
                                    	                                     ; https://duet3d.dozuki.com/Wiki/Gcode#Section_M557_Set_Z_probe_point_or_define_probing_grid
                                    
                                    
                                    ;; Heaters
                                    ; Bed
                                    ; Tune in with:  M303 H0 S70       (60=Temp) (M500 to save) 
                                    ; Show curren tsettings M307 H0
                                    M308 S0 P"0.temp2" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp2
                                    M950 H0 C"0.out2" T0 Q10                       ; create bed heater output on 0.out2 and map it to sensor 0 and Frequency (Q) 10Hz
                                    ; MOVED to  override M307 H0 A340 C140.0 D5.5 S1.0 V0.0 B0          ; disable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0                                        ; map heated bed to heater 0
                                    M143 H0 S120                                   ; set temperature limit for heater 0 to 120C
                                    
                                    
                                    ; Hotend
                                    ; Tune in with:  M303 H1 S270       (60=Temp) (M500 to save) 
                                    ; Show current settings M307 H1
                                    M308 S1 P"0.temp3" Y"thermistor" T500000 B4723 C1.196220e-7  ; configure sensor 1 
                                    M950 H1 C"0.out3" T1                         ; create nozzle heater output on 0.out3 and map it to sensor 1
                                    M143 H1 S280                                   	; set temperature limit for heater 1 to 280C
                                    ; MOVED to  override M307 H1 A340 C140.0 D5.5 S1.0 V0.0 B0        ; disable bang-bang mode for heater  and set PWM limit
                                    
                                    ;; Fans         ##################### TODO
                                    ; Fan for the printed part:
                                    M950 F0 C"0.out9" Q500                       ; create fan 0 on pin 1.out4 and set its frequency
                                    M106 P0 S0 H-1 C"Part"                       ; set fan 0 value. Thermostatic control is turned off
                                    ; Fan for the Hotend:
                                    M950 F1 C"0.out8" Q500                       ; create fan 1 on pin 1.out5 and set its frequency
                                    M106 P1 S1 H1 T45 C"Hotend"                  ; P="set fan 1" S="value" H="Thermostatic control Heater No." T=" is turned on at 45°C"
                                    
                                    ; Fan for expansion case Alwas on
                                    ;M950 F9 C"1.out8" Q500
                                    ;M106 P9 S1 H-1
                                    
                                    
                                    ; Tools
                                    M563 P0 S"TooL0" D0 H1 F0		                 ; define tool 0
                                    G10 P0 X0 Y0 Z0                              ; set tool 0 axis offsets
                                    G10 P0 R0 S0                                   ; set initial tool 0 active and standby temperatures to 0C
                                    
                                    ;; Filament Sensor          ##################### TODO
                                    M591 D0 P5 C"0.io3.in" R40:120 E3.0 S0  ; Duet3D laser sensor for extruder drive 0, connected to endstop input 3 (E0), tolerance 40 to 120%, 3mm comparison length, disabled
                                    
                                    
                                    ; Custom settings are not defined
                                    
                                    ; Miscellaneous
                                    M575 P1 B57600 S1							; Enable PanelDue
                                    M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                                    
                                    
                                    ; Configure the case fan:
                                    M308 S9 P"mcu-temp" Y"mcu-temp" A"mcu"        ; define sensor 9 to be mcu temperature
                                    M950 F2 C"0.out7" Q500
                                    ;M106 P2 S100 C"Case"
                                    ;M106 P2 S0 C"Case"				; Keep it off for now
                                    M106 P2 S1 L0.25 B0.5 H9 T40:60 C"Case"      ; cooling electronics space thermostatic on sensor 9 35 to 50C
                                    
                                    
                                    
                                    
                                    
                                    
                                    ; Enable the LED stripe and turn it off
                                    M950 F3 C"0.out6" Q500   ; LED on out6 ground on top pin, plus on 3rd pin from top (V_OUTLC1)
                                    M106 P3 C"LED" S0
                                    
                                    
                                    M501                                               ; load saved parameters from non-volatile memory (config-override.g)
                                    
                                    
                                    
                                    
                                    
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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by

                                      Can you test if you can reliably extrude at 195c? That might be too cold and it clogged?

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      Chrissundefined 1 Reply Last reply Reply Quote 0
                                      • Chrissundefined
                                        Chriss @Phaedrux
                                        last edited by

                                        @Phaedrux

                                        Good point.. I will finish the current print first. ... do you expect that PLA will fail already at 195?

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                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          Depends on the PLA. Depends on how much volume you're trying to flow. Depends on how accurate your thermistor values are.

                                          You could do a volumetric flow rate calibration at that temp to see if your speed height width combination was more than the hotend could handle at that temp.

                                          Did you try to print it again?

                                          Z-Bot CoreXY Build | Thingiverse Profile

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                                          • deckingmanundefined
                                            deckingman @Chriss
                                            last edited by

                                            @Chriss Just try using an extrusion multiplier of 95%. Parts are surprisingly very tolerant of under extrusion, but very intolerant of over extrusion.

                                            Ian
                                            https://somei3deas.wordpress.com/
                                            https://www.youtube.com/@deckingman

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