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    Printing too high.

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    Tuning and tweaking
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    • Phaedruxundefined
      Phaedrux Moderator @evilfknpotato
      last edited by

      @evilfknpotato said in Printing too high.:

      but the motor noise doesn't sound healthy

      Which motor? All of them? What moves are you doing?

      Can you record a video to show it?

      Z-Bot CoreXY Build | Thingiverse Profile

      evilfknpotatoundefined 1 Reply Last reply Reply Quote 0
      • evilfknpotatoundefined
        evilfknpotato @Phaedrux
        last edited by

        @Phaedrux yes that seems correct its a stock creality metal mount and re measured and the trigger height is correct at 3.2mm

        Phaedruxundefined 1 Reply Last reply Reply Quote 0
        • evilfknpotatoundefined
          evilfknpotato @Phaedrux
          last edited by

          @Phaedrux all of them on homing and g1 moves
          How do I upload a video?

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          • Phaedruxundefined
            Phaedrux Moderator @evilfknpotato
            last edited by

            @evilfknpotato said in Printing too high.:

            @Phaedrux yes that seems correct its a stock creality metal mount and re measured and the trigger height is correct at 3.2mm

            Alright, so with that G92 Z0 removed from the homeall.g file does the nozzle touch the bed when you tell it to move to the Z0?

            @evilfknpotato said in Printing too high.:

            How do I upload a video?

            On a desktop you can drag and drop a file onto the post text box to upload it, or you can put it on dropbox or google drive if it's too big and share a link.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • evilfknpotatoundefined
              evilfknpotato
              last edited by

              yes it always did move to Z0 before printing and now it prints at correct height thank you so much!
              Now its just the strange motor problems, if it were my wiring it would have done this before updating firmware. uploading video

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              • evilfknpotatoundefined
                evilfknpotato
                last edited by

                IMG_9326.MOV.mp4

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                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  Maybe if have to compare to how it sounded before but that doesn't sound too bad to me.

                  You can try reducing the motor current a bit. Try 600 or 700 instead of 800.

                  Z-Bot CoreXY Build | Thingiverse Profile

                  evilfknpotatoundefined 1 Reply Last reply Reply Quote 0
                  • evilfknpotatoundefined
                    evilfknpotato @Phaedrux
                    last edited by

                    @Phaedrux it was silent before this sounds like back emf or something

                    evilfknpotatoundefined 1 Reply Last reply Reply Quote 0
                    • evilfknpotatoundefined
                      evilfknpotato @evilfknpotato
                      last edited by

                      @evilfknpotato reduced current to 600 and still the same

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                      • evilfknpotatoundefined
                        evilfknpotato
                        last edited by

                        is it worth upgrading to v3.0?

                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator @evilfknpotato
                          last edited by

                          @evilfknpotato said in Printing too high.:

                          is it worth upgrading to v3.0?

                          I wouldn't think it would make a difference but I also wouldn't have thought moving from 2.0 to 2.05 would have changed anything either.

                          Going to rrf3 would require changes to your config file. If you wanted to test it you should back up your current config files and then generate a new config from the online tool for rrf3 to test with.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          evilfknpotatoundefined 1 Reply Last reply Reply Quote 0
                          • evilfknpotatoundefined
                            evilfknpotato @Phaedrux
                            last edited by

                            @Phaedrux exactly my thoughts but something must have changed, voltages?

                            Vetiundefined 1 Reply Last reply Reply Quote 0
                            • Vetiundefined
                              Veti @evilfknpotato
                              last edited by

                              @evilfknpotato

                              try changing the M569

                              M569 P0 S1 D3 V40 ; physical drive 0 goes backwards
                              M569 P1 S1 D3 V40; physical drive 1 goes backwards
                              M569 P2 S0 D3 V40; physical drive 2 goes forwards
                              M569 P3 S1 D3 V40 ; physical drive 3 goes backwards

                              print the output of
                              M569 P0 afterwards

                              evilfknpotatoundefined 2 Replies Last reply Reply Quote 1
                              • evilfknpotatoundefined
                                evilfknpotato @Veti
                                last edited by

                                @Veti you sir are very helpful, that worked like a treat, what did this do?

                                Vetiundefined 1 Reply Last reply Reply Quote 0
                                • evilfknpotatoundefined
                                  evilfknpotato @Veti
                                  last edited by

                                  @Veti M569 P0
                                  Drive 0 runs forwards, active low enable, step timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, tpwmthrs 40 (234.4 mm/sec)

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                                  • Vetiundefined
                                    Veti @evilfknpotato
                                    last edited by

                                    @evilfknpotato

                                    in newer version of the firmware the switchover from stealthchop to spreadcycle was implemented.

                                    spreadcycle is louder

                                    above like 10mm it will switch to spreadcycle by default.

                                    this increases the limit.

                                    however stealthchop is weaker, so it might cause layer shifts.
                                    if your extruder is skipping, i would suggest that you switch that over to spreadcycle
                                    by just changing
                                    M569 P3 S1 D2

                                    evilfknpotatoundefined 1 Reply Last reply Reply Quote 1
                                    • evilfknpotatoundefined
                                      evilfknpotato @Veti
                                      last edited by

                                      @Veti very interesting as I didn’t think that sound was normal, even the stock creality board sounded whiny but not like grinding like this Spreadcycle. Thank you @Phaedrux and @Veti for your help it is now printing beautifully

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