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    RRF Config Mapping

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    • JoergS5undefined
      JoergS5 @printthatthing
      last edited by JoergS5

      @printthatthing the
      G1 H1 Z-355 F360
      should be a replacement for what I proposed (the G30 proposal), but 355 is less than the 500 height of M208, so 0 may not be reached, I would set it higher to Z-600.
      And the G92 Z0 is not needed, because the G1 H1 Z... already sets Z to the M208 minimum for Z, ie 0.
      The sensitivity setting G31 P is probably wrong, please set P25 instead.

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        ; Z-Probe
        M950 S0 C"duex.pwm5"                          ; create servo pin 0 for BLTouch
        M558 P9 C"^zprobe.in" H5 F120 T6000            ; set Z probe type to bltouch and the dive height + speeds
        G31 P25 X66 Y33 Z2.5                          ; set Z probe trigger value, offset and trigger height
        

        Remove the ! from duex.pwm5
        Change G31 P500 to P25

        in homeall change

        G1 H1 Z-355 F360        ; move Z down stopping at the endstop
        G90                     ; absolute positioning
        G92 Z0                  ; set Z position to axis minimum (you may want to adjust this)
        

        To

        G90                     ; absolute positioning
        G1 X150 Y150 F6000        ; move Z down stopping at the endstop
        G30 ; probe the bed
        

        Z-Bot CoreXY Build | Thingiverse Profile

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        • printthatthingundefined
          printthatthing
          last edited by

          Thank you all again. I think I have it running now.
          I had to keep ! for duex.pwm5 else it does not probe.
          config.g

          ; Configuration file for Duet WiFi (firmware version 3)
          ; executed by the firmware on start-up
          ;
          ; generated by RepRapFirmware Configuration Tool v3.1.3 on Wed Jul 08 2020 21:18:31 GMT+0200 (centraleuropeisk sommartid)
          
          ; General preferences
          G90                                            ; send absolute coordinates...
          M83                                            ; ...but relative extruder moves
          M550 P"Formbot Raptor 2"                       ; set printer name
          
          ; Network
          M552 S1                                        ; enable network
          M586 P0 S1                                     ; enable HTTP
          M586 P1 S0                                     ; disable FTP
          M586 P2 S0                                     ; disable Telnet
          
          ; Drives
          M569 P0 S1                                     ; physical drive 0 goes forwards
          M569 P1 S1                                     ; physical drive 1 goes forwards
          M569 P2 S1                                     ; physical drive 2 goes forwards
          M569 P3 S1                                     ; physical drive 3 goes forwards
          M584 X0 Y1 Z2 E3                               ; set drive mapping
          M350 X16 Y16 Z16 E16 I1                        ; configure microstepping with interpolation
          M92 X80.00 Y80.00 Z640.00 E415.00              ; set steps per mm
          M566 X900.00 Y900.00 Z12.00 E120.00            ; set maximum instantaneous speed changes (mm/min)
          M203 X6000.00 Y6000.00 Z180.00 E1200.00        ; set maximum speeds (mm/min)
          M201 X500.00 Y500.00 Z20.00 E250.00            ; set accelerations (mm/s^2)
          M906 X800 Y800 Z800 E800 I30                   ; set motor currents (mA) and motor idle factor in per cent
          M84 S30                                        ; Set idle timeout
          
          ; Axis Limits
          M208 X0 Y0 Z0 S1                               ; set axis minima
          M208 X400 Y400 Z350 S0                         ; set axis maxima
          
          ; Endstops
          M574 X1 S1 P"!xstop"                           ; configure active-high endstop for low end on X via pin !xstop
          M574 Y1 S1 P"!ystop"                           ; configure active-high endstop for low end on Y via pin !ystop
          M574 Z1 S2                                     ; configure Z-probe endstop for low end on Z
          
          
          ; Z-Probe
          M950 S0 C"!duex.pwm5"                           ; create servo pin 0 for BLTouch
          M558 P9 C"^zprobe.in" H5 F120 T6000            ; set Z probe type to bltouch and the dive height + speeds
          G31 P25 X-25 Y-5 Z0.489                          ; set Z probe trigger value, offset and trigger height
          M557 X5:380 Y5:380 S20                       ; define mesh grid
          
          ; Heaters
          M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp
          M950 H0 C"bedheat" T0                          ; create bed heater output on bedheat and map it to sensor 0
          M307 H0 B1 S1.00                               ; enable bang-bang mode for the bed heater and set PWM limit
          M140 H0                                        ; map heated bed to heater 0
          M143 H0 S120                                   ; set temperature limit for heater 0 to 120C
          M308 S1 P"e0temp" Y"thermistor" T100000 B4138  ; configure sensor 1 as thermistor on pin e0temp
          M950 H1 C"e0heat" T1                           ; create nozzle heater output on e0heat and map it to sensor 1
          M307 H1 B0 S1.00                               ; disable bang-bang mode for heater  and set PWM limit
          
          ; Fans
          M950 F0 C"fan0" Q500                           ; create fan 0 on pin fan0 and set its frequency
          M106 P0 S0 H-1                                 ; set fan 0 value. Thermostatic control is turned off
          M950 F1 C"fan1" Q500                           ; create fan 1 on pin fan1 and set its frequency
          M106 P1 S1 H1 T45                              ; set fan 1 value. Thermostatic control is turned on
          
          ; Tools
          M563 P0 D0 H1 F0                               ; define tool 0
          G10 P0 X0 Y0 Z0                                ; set tool 0 axis offsets
          G10 P0 R0 S0                                   ; set initial tool 0 active and standby temperatures to 0C
          
          ; Custom settings are not defined
          
          

          homeall.g

          ; homeall.g
          ; called to home all axes
          ;
          ; generated by RepRapFirmware Configuration Tool v3.1.3 on Wed Jul 08 2020 20:58:26 GMT+0200 (centraleuropeisk sommartid)
          G91                     ; relative positioning
          G1 H2 Z5 F6000          ; lift Z relative to current position
          G1 H1 X-405 Y-405 F1800 ; move quickly to X and Y axis endstops and stop there (first pass)
          G1 H2 X5 Y5 F6000       ; go back a few mm
          G1 H1 X-405 Y-405 F360  ; move slowly to X and Y axis endstops once more (second pass)
          
          
          G90                     ; absolute positioning
          G1 X150 Y150 F6000        ; move Z down stopping at the endstop
          G30                     ; home Z by probing the bed
          
          
          ; Uncomment the following lines to lift Z after probing
          G91                    ; relative positioning
          G1 Z5 F100             ; lift Z relative to current position
          G90                    ; absolute positioning
          

          Is the heatmap very bad or ok to use without adjustments?
          heat.png

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators
            last edited by dc42

            As you have no DueX, you are not connecting the servo pin of the BLTouch duex.pwm5, so you should not use that selection in configtool or config.g. Use the name of the actual pin that you have connected it to, which is exp.heater7, and don't invert it. Although as it happens, using duex.pwm5 and inverting it will work.

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            printthatthingundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
            • printthatthingundefined
              printthatthing @dc42
              last edited by

              @dc42 Aha, okay that make sense.

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              • Phaedruxundefined
                Phaedrux Moderator @dc42
                last edited by

                @dc42 said in RRF Config Mapping:

                so you should not use that selection in configtool

                Unfortunately the config tool currently doesn't show the expansion pins right now, just duex pins.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • Phaedruxundefined
                  Phaedrux Moderator @printthatthing
                  last edited by

                  @printthatthing said in RRF Config Mapping:

                  Is the heatmap very bad or ok to use without adjustments?

                  That's a bit of a saddle shape for sure. You may or may not be able to fix that physically. You can test the effect of the compensation by printing a bed test like this: bedlevel_nozzle_0.4_200x200-0.3-0.8.stl

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • printthatthingundefined
                    printthatthing @Phaedrux
                    last edited by

                    @Phaedrux Ok thanks.

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                    • printthatthingundefined
                      printthatthing
                      last edited by

                      Now I'm stuck with error at bed heating.
                      Error: Heater 0 fault: temperature rising much more slowly than the expected 1.7°C/sec
                      Duet 2 Wifi power a solid state relay for a 220v heater.

                      I executed M307 H0 S90
                      M307 H0 results in below.
                      Heater 0 model: gain 340.0, time constant 140.0, dead time 5.5, max PWM 1.00, calibration voltage 0.0, mode bang-bang

                      Then I tried to save the value
                      M307 H0 A340 C140 D5.5 V0 B0
                      But it result in
                      Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        That's expected. The warning is letting you know what the max uncontrolled temp could be.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • printthatthingundefined
                          printthatthing @Phaedrux
                          last edited by

                          @Phaedrux Ok, but I still not able to heat the bed. It start heating but halt after few seconds. Error: Heater 0 fault: temperature rising much more slowly than the expected 1.7°C/sec

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                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            Are you sure you saved the PID tuning results with M500? Do you also have an M501 at the end of config.g to load the saved results?

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • printthatthingundefined
                              printthatthing @Phaedrux
                              last edited by printthatthing

                              @Phaedrux i was missing M501 in config.g
                              Restarted boad but getting same error when trying to heat bed.
                              Tried to run M307 H0 S90 again but it fails with Error: M307: bad model parameters

                              ; config-override.g file generated in response to M500 at 2020-07-10 23:02
                              ; This is a system-generated file - do not edit
                              ; Heater model parameters
                              M307 H0 A340.0 C140.0 D5.5 S1.00 V0.0 B1
                              M307 H1 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                              ; Workplace coordinates
                              G10 L2 P1 X0.00 Y0.00 Z0.00
                              G10 L2 P2 X0.00 Y0.00 Z0.00
                              G10 L2 P3 X0.00 Y0.00 Z0.00
                              G10 L2 P4 X0.00 Y0.00 Z0.00
                              G10 L2 P5 X0.00 Y0.00 Z0.00
                              G10 L2 P6 X0.00 Y0.00 Z0.00
                              G10 L2 P7 X0.00 Y0.00 Z0.00
                              G10 L2 P8 X0.00 Y0.00 Z0.00
                              G10 L2 P9 X0.00 Y0.00 Z0.00
                              
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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                In config.g change M307 H0 B1 S1.00 to B0

                                Then delete your config-override.g and run M307 H0 S90 again after a reboot. Then save with M500.

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  Also make sure you're starting from a cold bed state.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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                                  • printthatthingundefined
                                    printthatthing @Phaedrux
                                    last edited by printthatthing

                                    @Phaedrux said in RRF Config Mapping:

                                    Executed M307 H0 S90 after the suggested changes.
                                    Error: M307: bad model parameters

                                    Update:
                                    My bad, it might be M303 H0 S90

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • Phaedruxundefined
                                      Phaedrux Moderator @printthatthing
                                      last edited by

                                      @printthatthing said in RRF Config Mapping:

                                      Update:
                                      My bad, it might be M303 H0 S90

                                      😑 Yes of course.

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      printthatthingundefined 1 Reply Last reply Reply Quote 0
                                      • printthatthingundefined
                                        printthatthing @Phaedrux
                                        last edited by

                                        @Phaedrux said in RRF Config Mapping:

                                        @printthatthing said in RRF Config Mapping:

                                        Update:
                                        My bad, it might be M303 H0 S90

                                        😑 Yes of course.

                                        Now it works fine:) Thank you so much for all support.

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