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    Homing issues on 2 delta printers after upgrading to 3.1.1

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    • dc42undefined
      dc42 administrators
      last edited by dc42

      Does it work if you replace this line:

      G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

      by this:

      G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

      or alternatively by:

      G1 Z-10 F6000 ; move down a few mm so that the nozzle can be centred

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

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      • mhackneyundefined
        mhackney
        last edited by

        Thank you David. I changed to

        G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred
        

        And that did the trick.

        My 3D Printing blog: http://www.sublimelayers.com
        Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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        • mhackneyundefined
          mhackney
          last edited by

          But it did not work for my friend's machine. IO asked him to post here.

          My 3D Printing blog: http://www.sublimelayers.com
          Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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          • sLpFhaWKundefined
            sLpFhaWK
            last edited by sLpFhaWK

            Hi David, I am also having this issue which is why I got help from Michael, it seems even after changing the lines you recommend I am still getting that error.

            Config.g

            ; Configuration file for UltiBots D300 V-Slot 3D Printer
            ; version 1.0 for firmware version 3.0
            
            ; Communication and general
            M111 S0                         		; Debug off
            M550 PVader  				    	    ; Machine name and Netbios name (can be anything you like)
            M551 XXXXX				                ; Machine password (used for FTP)
            ;*** If you have more than one Duet on your network, they must all have different MAC addresses, so change the last digits
            ;*** Wifi Networking
            M552 S1					                ; Enable WiFi
            ;M587 S"Epcot" I"192.168.1.102"
            M555 P2                         		; Set output to look like Marlin
            
            M575 P1 S1 B57600		    		    ; Communication parameters for the PanelDue
            
            G21                           		 	; Work in millimetres
            G90                          		 	; Send absolute coordinates...
            M83                           		 	; ...but relative extruder moves
            
            ; Axis and motor configuration
            M569 P0 S0			        	       ; Drive 0 goes forwards (X tower)
            M569 P1 S0			        	       ; Drive 1 goes forwards (Y tower)
            M569 P2 S0			        	       ; Drive 2 goes forwards (Z tower)
            M569 P3 S0				               ; Drive 3 goes forwards (extruder 1)
            
            ;M574 X2 Y2 Z2 S1			    	   ; set endstop configuration (all endstops at high end, active high)
            M574 X1 S1 P"xstop"   ; X min active high endstop switch
            M574 Y1 S1 P"ystop"   ; Y min active high endstop switch
            M574 Z1 S1 P"zstop"   ; Z min active high endstop switch
            
            ;*** The homed height is deliberately set too high in the following - you will adjust it during calibration
            M665 L376.890 R209.421 H448 B140.0 X1.000 Y0.329 Z0.000	; set delta radius, diagonal rod length L380.31, printable radius and homed height
            M666 X-0.44 Y-1.37 Z1.81			   ; put your endstop adjustments here, or let auto calibration find them
            
            M350 X64 Y64 Z64 E16 I1			; Set microstepping to 32 for X, Y and Z and 16 for extruder stepper with interpolation
            M92 X640 Y640 Z640			; Set axis steps/mm
            M906 X1000 Y1000 Z1000 E500		; Set motor currents (mA)
            M201 X1000 Y1000 Z1000 E1000		; Accelerations (mm/s^2)
            M203 X20000 Y20000 Z20000 E3600		; Maximum speeds (mm/min)
            M566 X1200 Y1200 Z1200 E300		; Maximum instant speed changes mm/minute
            
            ; Fans
            M950 F2 C"fan2"
            M950 F1 C"fan1"                        ; This fan is the Heatsink Fan
            M106 P1 T50 S255 H1			    	   ; Set hotend heatsink FAN1 thermostatic control at 50°C
            
            ; Thermistors
            M308 S0 P"bed_temp" Y"thermistor" T100000 B3950 ; define bed temperature sensor
            M308 S1 P"e0_temp" Y"thermistor" T100000 B4725 C7.06e-8 ; define E0 temperature sensor
            M950 H0 C"bed_heat" T0 ; heater 0 uses the bed_heat pin, sensor 0
            M950 H1 C"e0_heat" T1 ; heater 1 uses the e0_heat pin and sensor 1
            
            ; Heater configuration
            M140 H0
            
            ; Tool definitions
            M563 P0 D0 H1                          ; Define tool 0, the extruder
            G10 P0 S0 R0                           ; Set tool 0 operating and standby temperatures
            ;M92 E415					           ; Bondtech BMG steps per mm
            M92 E822	                       	   ; Titan Aero steps per mm                    	old: 837
            
            ; Z probe and compensation definition
            ; Change "H25" to "H3" AFTER commissioning your printer
            M558 P5 C"!e0stop" X0 Y0 Z0 H4 F60     ; FSRs with JohnSL board Z probe behaves as a switch and is not used for homing any axes
            ;G31 X0 Y0 Z-0.15 P500				   ; More (-) Z is less smooshed, more (+) Z is more smooshed
            G31 X0 Y0 Z-0.25 P500				   ; More (-) Z is less smooshed, more (+) Z is more smooshed
            
            T0						               ; Select tool 0, the hot end
            M501						           ; Load config-override.g
            
            

            Here is my current homedelta.g

            ; Homing file for RepRapFirmware on UltiBots D300VS
            G91							; use relative positioning
            G1 H1 X1000 Y1000 Z1000 F2500		; move all carriages up 1000mm, stopping at the endstops
            G1 H1 X6 Y6 Z6 F250			; move carriages slowly up 6mm, stopping at the endstops
            G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred
            G1 Z-10 F6000 ; move down a few mm so that the nozzle can be centred
            G90							; back to absolute positioning
            G1 X0 Y0 F2000				; center the head and set a reasonable feed rate
            

            6897d636-ad52-46ee-a831-4b8e2f8ec188-image.png

            -sLpFhaWK
            Ultibots K250v
            Rostock Max v2 Soon to be Full MetalMax
            Mini Kossel

            Phaedruxundefined droftartsundefined 2 Replies Last reply Reply Quote 0
            • mhackneyundefined
              mhackney
              last edited by

              sLpDhaWK and my config.g and other files are nearly identical. The only difference is that I have a PT100 setup on an E3D Titan Aero and he has a V67 hot end with Ultibots microstruder. Otherwise I used the exact config files that we edited together yesterday.

              My 3D Printing blog: http://www.sublimelayers.com
              Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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              • Phaedruxundefined
                Phaedrux Moderator @sLpFhaWK
                last edited by

                @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                G1 Z-10 F6000 ; move down a few mm so that the nozzle can be centred

                Can you try more than 10mm?

                Z-Bot CoreXY Build | Thingiverse Profile

                sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                • dc42undefined
                  dc42 administrators
                  last edited by

                  @sLpFhaWK , your homedelta.g file is very significantly different, and wrong in at least one important respect. Please take a closer look and work out what it is doing, and what you want it to do instead.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                  • sLpFhaWKundefined
                    sLpFhaWK @dc42
                    last edited by

                    @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                    @sLpFhaWK , your homedelta.g file is very significantly different, and wrong in at least one important respect. Please take a closer look and work out what it is doing, and what you want it to do instead.

                    David, I've been messing with it for a good part of the morning. I even used the configurator to see what a clean homedelta.g would look like, and I've used the exact same one as Michael and I am still getting the issue.

                    Our printers are nearly identical aside from his hotend/extruder setup.

                    -sLpFhaWK
                    Ultibots K250v
                    Rostock Max v2 Soon to be Full MetalMax
                    Mini Kossel

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                    • sLpFhaWKundefined
                      sLpFhaWK @Phaedrux
                      last edited by

                      @Phaedrux

                      I can, and will. This is my homedelta.g now.

                      G91                            ; relative positioning
                      G1 H1 X1200 Y1200 Z1200 F2500  ; move all towers to the high end stopping at the endstops (first pass)
                      G1 H2 X-6 Y-6 Z-6 F2500        ; go down a few mm
                      G1 H1 X7 Y7 Z7 F360         ; move all towers up once more (second pass)
                      G1 Z-5 F6000                   ; move down a few mm so that the nozzle can be centred
                      G90                            ; absolute positioning
                      G1 X0 Y0 F6000                 ; move X+Y to the centre
                      

                      -sLpFhaWK
                      Ultibots K250v
                      Rostock Max v2 Soon to be Full MetalMax
                      Mini Kossel

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                      • dc42undefined
                        dc42 administrators
                        last edited by dc42

                        That homedelta.g file looks better than the one you pstes earlier. But if you refer to my earlier post, I suggested to @mhackney that he change the line:

                        @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                        G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                        • sLpFhaWKundefined
                          sLpFhaWK @dc42
                          last edited by

                          @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                          @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                          G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                          If you refer to my earlier post, I suggested to @mhackney that he change that line.

                          David you are correct, and I did change that and even though it worked for Michael it did not work for me.

                          -sLpFhaWK
                          Ultibots K250v
                          Rostock Max v2 Soon to be Full MetalMax
                          Mini Kossel

                          dc42undefined 1 Reply Last reply Reply Quote 0
                          • dc42undefined
                            dc42 administrators @sLpFhaWK
                            last edited by

                            @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                            @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                            @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                            G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                            If you refer to my earlier post, I suggested to @mhackney that he change that line.

                            David you are correct, and I did change that and even though it worked for Michael it did not work for me.

                            So why did you post the old homedelta.g instead of the modified one? How do you expect me to help you if it appears to me that you have ignored my suggestions?

                            Duet WiFi hardware designer and firmware engineer
                            Please do not ask me for Duet support via PM or email, use the forum
                            http://www.escher3d.com, https://miscsolutions.wordpress.com

                            sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                            • sLpFhaWKundefined
                              sLpFhaWK @dc42
                              last edited by

                              @dc42
                              David, with all due respect I haven't ignored your suggestions. I am unsure why the homedelta.g I posted didn't have your change in it, at the time I copied and pasted what Michael had sent to me in a messenger chat.

                              But I am also confused, is that line supposed to be in the homedelta.g twice? If you look at my original code it is in there on line 5. Do I delete line 6?

                              a5333773-3c81-4fb5-9554-35f30f380351-image.png

                              This is what I have now, and even now I'm not sure it's correct.

                              G91                            ; relative positioning
                              G1 H1 X1200 Y1200 Z1200 F2500  ; move all towers to the high end stopping at the endstops (first pass)
                              G1 H2 X-6 Y-6 Z-6 F2500        ; go down a few mm
                              G1 H1 X7 Y7 Z7 F360         ; move all towers up once more (second pass)
                              G1 H2 X-5 Y-5 Z-5 F6000
                              ; G1 Z-20 F6000                   ; move down a few mm so that the nozzle can be centred
                              G90                            ; absolute positioning
                              G1 X0 Y0 F6000                 ; move X+Y to the centre
                              

                              -sLpFhaWK
                              Ultibots K250v
                              Rostock Max v2 Soon to be Full MetalMax
                              Mini Kossel

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                              • mhackneyundefined
                                mhackney
                                last edited by

                                @dc42 So, this is odd and probably related to his issue too...

                                As I reported above, when I made the one line change you suggested, homing worked fine. Then I homed, jogged down in Z by 200mm and reset the Duet. Now I am getting the same error - and even odder - even issuing G28 (or clicking home) multiple times, the printer does the home cycle and then generates the target not reached error.

                                Here is my homedelta.g after making your change:

                                ; Homing file for RepRapFirmware on UltiBots D300VS
                                G91							; use relative positioning
                                G1 H1 X1000 Y1000 Z1000 F2500		; move all carriages up 1000mm, stopping at the endstops
                                G1 H2 X-5 Y-5 Z-5			; move all carriages down 3mm
                                
                                G1 H1 X6 Y6 Z6 F250			; move carriages slowly up 6mm, stopping at the endstops
                                G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred
                                G90							; back to absolute positioning
                                G1 X0 Y0 F2000				; center the head and set a reasonable feed rate
                                

                                I have not touched my scripts and after I made your change earlier today I tested homing and jogging in Z and X-Y many (>10) times with no issues. But now after a reboot it is failing.

                                My 3D Printing blog: http://www.sublimelayers.com
                                Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                • mhackneyundefined
                                  mhackney
                                  last edited by

                                  And removing the last 2 G1 lines as you originally requested, the error is not generated.

                                  My 3D Printing blog: http://www.sublimelayers.com
                                  Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                  • mhackneyundefined
                                    mhackney
                                    last edited by

                                    I've tried lowering 15 mm in the G1 H2 line third from the bottom to give a bit more room. That fails too.

                                    If I only comment the last G1 X0 Y0 F2000 no error is generated but any jog move in Z generates this error:

                                    M120 G91 G1 Z-5 F6000 G90 M121
                                    Error: G0/G1: target position not reachable from current position
                                    

                                    My 3D Printing blog: http://www.sublimelayers.com
                                    Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by

                                      I'm not really a delta guy, but from past instances of that error it was usually enough to drop all carriages in Z to resolve the error, which from what I understand means that the requested move would require one of the carriages to raise above the endstop to be reached.

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • mhackneyundefined
                                        mhackney
                                        last edited by mhackney

                                        Thanks Phaedrux. Mechanically, nothing has changed on these printers and mine are workhorses. The error message seems logical and your first post above made sense so I tried -15mm drop in Z on my machine but still getting this error.

                                        It is true that a movement in XY on a delta causes at least 1 carriage to move up the tower and that does seem to be what this error message is telling us. But at 15mm down from the home switches there should be enough room for small X-Y movements. So as a test I did the final downward move to:

                                        G1 H2 X-100 Y-100 Z-100 F6000 ; move down a few mm so that the nozzle can be centred

                                        So now I see the home sequence, the slow descent of 100mm, then a final X-Y adjustment presumably for the M666 endstop offset adjustments and THEN the error is raised.

                                        David, you asked about my M665 and M666 before, they are copied from my 2.x config.g. They seem correct. Hmm, this got me thinking, maybe my config-override.g has some bad stuff in it. I commented out the M665 and M666 in it and now homing seems to be working again. Here is what I commented out in config-override:

                                        ;M665 L376.890:376.890:376.890 R209.670 H450.462 B140.0 X0.114 Y0.283 Z0.000
                                        ;M666 X0.107 Y-0.648 Z0.542 A0.00 B0.00
                                        

                                        My 3D Printing blog: http://www.sublimelayers.com
                                        Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                        • mhackneyundefined
                                          mhackney
                                          last edited by

                                          Well, nope, I am still getting the error when I change the final move from 100 back to 5mm.

                                          My 3D Printing blog: http://www.sublimelayers.com
                                          Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                          • mhackneyundefined
                                            mhackney
                                            last edited by mhackney

                                            Ok, maybe this will help narrow it down...

                                            When I home and get this error, take a look at X Y and Z in DWC. X and Y should be 0 and Z 450.32mm.

                                            Screen Shot 2020-07-14 at 4.49.00 PM.png

                                            If I reset and home when the printer is "near" the home position, I get no error and the correct tool position. However, if I jog down 100mm (for example) and reset, I get this error when trying to home.

                                            This is certainly an odd situation.

                                            If I then do a G92 X0 Y0 Z-450 after I get the error and see the odd tool position then I can home with no errors.

                                            My 3D Printing blog: http://www.sublimelayers.com
                                            Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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