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    Homing issues on 2 delta printers after upgrading to 3.1.1

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    • mhackneyundefined
      mhackney
      last edited by

      But it did not work for my friend's machine. IO asked him to post here.

      My 3D Printing blog: http://www.sublimelayers.com
      Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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      • sLpFhaWKundefined
        sLpFhaWK
        last edited by sLpFhaWK

        Hi David, I am also having this issue which is why I got help from Michael, it seems even after changing the lines you recommend I am still getting that error.

        Config.g

        ; Configuration file for UltiBots D300 V-Slot 3D Printer
        ; version 1.0 for firmware version 3.0
        
        ; Communication and general
        M111 S0                         		; Debug off
        M550 PVader  				    	    ; Machine name and Netbios name (can be anything you like)
        M551 XXXXX				                ; Machine password (used for FTP)
        ;*** If you have more than one Duet on your network, they must all have different MAC addresses, so change the last digits
        ;*** Wifi Networking
        M552 S1					                ; Enable WiFi
        ;M587 S"Epcot" I"192.168.1.102"
        M555 P2                         		; Set output to look like Marlin
        
        M575 P1 S1 B57600		    		    ; Communication parameters for the PanelDue
        
        G21                           		 	; Work in millimetres
        G90                          		 	; Send absolute coordinates...
        M83                           		 	; ...but relative extruder moves
        
        ; Axis and motor configuration
        M569 P0 S0			        	       ; Drive 0 goes forwards (X tower)
        M569 P1 S0			        	       ; Drive 1 goes forwards (Y tower)
        M569 P2 S0			        	       ; Drive 2 goes forwards (Z tower)
        M569 P3 S0				               ; Drive 3 goes forwards (extruder 1)
        
        ;M574 X2 Y2 Z2 S1			    	   ; set endstop configuration (all endstops at high end, active high)
        M574 X1 S1 P"xstop"   ; X min active high endstop switch
        M574 Y1 S1 P"ystop"   ; Y min active high endstop switch
        M574 Z1 S1 P"zstop"   ; Z min active high endstop switch
        
        ;*** The homed height is deliberately set too high in the following - you will adjust it during calibration
        M665 L376.890 R209.421 H448 B140.0 X1.000 Y0.329 Z0.000	; set delta radius, diagonal rod length L380.31, printable radius and homed height
        M666 X-0.44 Y-1.37 Z1.81			   ; put your endstop adjustments here, or let auto calibration find them
        
        M350 X64 Y64 Z64 E16 I1			; Set microstepping to 32 for X, Y and Z and 16 for extruder stepper with interpolation
        M92 X640 Y640 Z640			; Set axis steps/mm
        M906 X1000 Y1000 Z1000 E500		; Set motor currents (mA)
        M201 X1000 Y1000 Z1000 E1000		; Accelerations (mm/s^2)
        M203 X20000 Y20000 Z20000 E3600		; Maximum speeds (mm/min)
        M566 X1200 Y1200 Z1200 E300		; Maximum instant speed changes mm/minute
        
        ; Fans
        M950 F2 C"fan2"
        M950 F1 C"fan1"                        ; This fan is the Heatsink Fan
        M106 P1 T50 S255 H1			    	   ; Set hotend heatsink FAN1 thermostatic control at 50°C
        
        ; Thermistors
        M308 S0 P"bed_temp" Y"thermistor" T100000 B3950 ; define bed temperature sensor
        M308 S1 P"e0_temp" Y"thermistor" T100000 B4725 C7.06e-8 ; define E0 temperature sensor
        M950 H0 C"bed_heat" T0 ; heater 0 uses the bed_heat pin, sensor 0
        M950 H1 C"e0_heat" T1 ; heater 1 uses the e0_heat pin and sensor 1
        
        ; Heater configuration
        M140 H0
        
        ; Tool definitions
        M563 P0 D0 H1                          ; Define tool 0, the extruder
        G10 P0 S0 R0                           ; Set tool 0 operating and standby temperatures
        ;M92 E415					           ; Bondtech BMG steps per mm
        M92 E822	                       	   ; Titan Aero steps per mm                    	old: 837
        
        ; Z probe and compensation definition
        ; Change "H25" to "H3" AFTER commissioning your printer
        M558 P5 C"!e0stop" X0 Y0 Z0 H4 F60     ; FSRs with JohnSL board Z probe behaves as a switch and is not used for homing any axes
        ;G31 X0 Y0 Z-0.15 P500				   ; More (-) Z is less smooshed, more (+) Z is more smooshed
        G31 X0 Y0 Z-0.25 P500				   ; More (-) Z is less smooshed, more (+) Z is more smooshed
        
        T0						               ; Select tool 0, the hot end
        M501						           ; Load config-override.g
        
        

        Here is my current homedelta.g

        ; Homing file for RepRapFirmware on UltiBots D300VS
        G91							; use relative positioning
        G1 H1 X1000 Y1000 Z1000 F2500		; move all carriages up 1000mm, stopping at the endstops
        G1 H1 X6 Y6 Z6 F250			; move carriages slowly up 6mm, stopping at the endstops
        G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred
        G1 Z-10 F6000 ; move down a few mm so that the nozzle can be centred
        G90							; back to absolute positioning
        G1 X0 Y0 F2000				; center the head and set a reasonable feed rate
        

        6897d636-ad52-46ee-a831-4b8e2f8ec188-image.png

        -sLpFhaWK
        Ultibots K250v
        Rostock Max v2 Soon to be Full MetalMax
        Mini Kossel

        Phaedruxundefined droftartsundefined 2 Replies Last reply Reply Quote 0
        • mhackneyundefined
          mhackney
          last edited by

          sLpDhaWK and my config.g and other files are nearly identical. The only difference is that I have a PT100 setup on an E3D Titan Aero and he has a V67 hot end with Ultibots microstruder. Otherwise I used the exact config files that we edited together yesterday.

          My 3D Printing blog: http://www.sublimelayers.com
          Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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          • Phaedruxundefined
            Phaedrux Moderator @sLpFhaWK
            last edited by

            @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

            G1 Z-10 F6000 ; move down a few mm so that the nozzle can be centred

            Can you try more than 10mm?

            Z-Bot CoreXY Build | Thingiverse Profile

            sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
            • dc42undefined
              dc42 administrators
              last edited by

              @sLpFhaWK , your homedelta.g file is very significantly different, and wrong in at least one important respect. Please take a closer look and work out what it is doing, and what you want it to do instead.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

              sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
              • sLpFhaWKundefined
                sLpFhaWK @dc42
                last edited by

                @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                @sLpFhaWK , your homedelta.g file is very significantly different, and wrong in at least one important respect. Please take a closer look and work out what it is doing, and what you want it to do instead.

                David, I've been messing with it for a good part of the morning. I even used the configurator to see what a clean homedelta.g would look like, and I've used the exact same one as Michael and I am still getting the issue.

                Our printers are nearly identical aside from his hotend/extruder setup.

                -sLpFhaWK
                Ultibots K250v
                Rostock Max v2 Soon to be Full MetalMax
                Mini Kossel

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                • sLpFhaWKundefined
                  sLpFhaWK @Phaedrux
                  last edited by

                  @Phaedrux

                  I can, and will. This is my homedelta.g now.

                  G91                            ; relative positioning
                  G1 H1 X1200 Y1200 Z1200 F2500  ; move all towers to the high end stopping at the endstops (first pass)
                  G1 H2 X-6 Y-6 Z-6 F2500        ; go down a few mm
                  G1 H1 X7 Y7 Z7 F360         ; move all towers up once more (second pass)
                  G1 Z-5 F6000                   ; move down a few mm so that the nozzle can be centred
                  G90                            ; absolute positioning
                  G1 X0 Y0 F6000                 ; move X+Y to the centre
                  

                  -sLpFhaWK
                  Ultibots K250v
                  Rostock Max v2 Soon to be Full MetalMax
                  Mini Kossel

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                  • dc42undefined
                    dc42 administrators
                    last edited by dc42

                    That homedelta.g file looks better than the one you pstes earlier. But if you refer to my earlier post, I suggested to @mhackney that he change the line:

                    @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                    G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                    • sLpFhaWKundefined
                      sLpFhaWK @dc42
                      last edited by

                      @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                      @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                      G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                      If you refer to my earlier post, I suggested to @mhackney that he change that line.

                      David you are correct, and I did change that and even though it worked for Michael it did not work for me.

                      -sLpFhaWK
                      Ultibots K250v
                      Rostock Max v2 Soon to be Full MetalMax
                      Mini Kossel

                      dc42undefined 1 Reply Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @sLpFhaWK
                        last edited by

                        @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                        @dc42 said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                        @sLpFhaWK said in Homing issues on 2 delta printers after upgrading to 3.1.1:

                        G1 Z-5 F6000 ; move down a few mm so that the nozzle can be centred

                        If you refer to my earlier post, I suggested to @mhackney that he change that line.

                        David you are correct, and I did change that and even though it worked for Michael it did not work for me.

                        So why did you post the old homedelta.g instead of the modified one? How do you expect me to help you if it appears to me that you have ignored my suggestions?

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                        • sLpFhaWKundefined
                          sLpFhaWK @dc42
                          last edited by

                          @dc42
                          David, with all due respect I haven't ignored your suggestions. I am unsure why the homedelta.g I posted didn't have your change in it, at the time I copied and pasted what Michael had sent to me in a messenger chat.

                          But I am also confused, is that line supposed to be in the homedelta.g twice? If you look at my original code it is in there on line 5. Do I delete line 6?

                          a5333773-3c81-4fb5-9554-35f30f380351-image.png

                          This is what I have now, and even now I'm not sure it's correct.

                          G91                            ; relative positioning
                          G1 H1 X1200 Y1200 Z1200 F2500  ; move all towers to the high end stopping at the endstops (first pass)
                          G1 H2 X-6 Y-6 Z-6 F2500        ; go down a few mm
                          G1 H1 X7 Y7 Z7 F360         ; move all towers up once more (second pass)
                          G1 H2 X-5 Y-5 Z-5 F6000
                          ; G1 Z-20 F6000                   ; move down a few mm so that the nozzle can be centred
                          G90                            ; absolute positioning
                          G1 X0 Y0 F6000                 ; move X+Y to the centre
                          

                          -sLpFhaWK
                          Ultibots K250v
                          Rostock Max v2 Soon to be Full MetalMax
                          Mini Kossel

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                          • mhackneyundefined
                            mhackney
                            last edited by

                            @dc42 So, this is odd and probably related to his issue too...

                            As I reported above, when I made the one line change you suggested, homing worked fine. Then I homed, jogged down in Z by 200mm and reset the Duet. Now I am getting the same error - and even odder - even issuing G28 (or clicking home) multiple times, the printer does the home cycle and then generates the target not reached error.

                            Here is my homedelta.g after making your change:

                            ; Homing file for RepRapFirmware on UltiBots D300VS
                            G91							; use relative positioning
                            G1 H1 X1000 Y1000 Z1000 F2500		; move all carriages up 1000mm, stopping at the endstops
                            G1 H2 X-5 Y-5 Z-5			; move all carriages down 3mm
                            
                            G1 H1 X6 Y6 Z6 F250			; move carriages slowly up 6mm, stopping at the endstops
                            G1 H2 X-5 Y-5 Z-5 F6000 ; move down a few mm so that the nozzle can be centred
                            G90							; back to absolute positioning
                            G1 X0 Y0 F2000				; center the head and set a reasonable feed rate
                            

                            I have not touched my scripts and after I made your change earlier today I tested homing and jogging in Z and X-Y many (>10) times with no issues. But now after a reboot it is failing.

                            My 3D Printing blog: http://www.sublimelayers.com
                            Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                            • mhackneyundefined
                              mhackney
                              last edited by

                              And removing the last 2 G1 lines as you originally requested, the error is not generated.

                              My 3D Printing blog: http://www.sublimelayers.com
                              Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                              • mhackneyundefined
                                mhackney
                                last edited by

                                I've tried lowering 15 mm in the G1 H2 line third from the bottom to give a bit more room. That fails too.

                                If I only comment the last G1 X0 Y0 F2000 no error is generated but any jog move in Z generates this error:

                                M120 G91 G1 Z-5 F6000 G90 M121
                                Error: G0/G1: target position not reachable from current position
                                

                                My 3D Printing blog: http://www.sublimelayers.com
                                Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  I'm not really a delta guy, but from past instances of that error it was usually enough to drop all carriages in Z to resolve the error, which from what I understand means that the requested move would require one of the carriages to raise above the endstop to be reached.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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                                  • mhackneyundefined
                                    mhackney
                                    last edited by mhackney

                                    Thanks Phaedrux. Mechanically, nothing has changed on these printers and mine are workhorses. The error message seems logical and your first post above made sense so I tried -15mm drop in Z on my machine but still getting this error.

                                    It is true that a movement in XY on a delta causes at least 1 carriage to move up the tower and that does seem to be what this error message is telling us. But at 15mm down from the home switches there should be enough room for small X-Y movements. So as a test I did the final downward move to:

                                    G1 H2 X-100 Y-100 Z-100 F6000 ; move down a few mm so that the nozzle can be centred

                                    So now I see the home sequence, the slow descent of 100mm, then a final X-Y adjustment presumably for the M666 endstop offset adjustments and THEN the error is raised.

                                    David, you asked about my M665 and M666 before, they are copied from my 2.x config.g. They seem correct. Hmm, this got me thinking, maybe my config-override.g has some bad stuff in it. I commented out the M665 and M666 in it and now homing seems to be working again. Here is what I commented out in config-override:

                                    ;M665 L376.890:376.890:376.890 R209.670 H450.462 B140.0 X0.114 Y0.283 Z0.000
                                    ;M666 X0.107 Y-0.648 Z0.542 A0.00 B0.00
                                    

                                    My 3D Printing blog: http://www.sublimelayers.com
                                    Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                    • mhackneyundefined
                                      mhackney
                                      last edited by

                                      Well, nope, I am still getting the error when I change the final move from 100 back to 5mm.

                                      My 3D Printing blog: http://www.sublimelayers.com
                                      Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                      • mhackneyundefined
                                        mhackney
                                        last edited by mhackney

                                        Ok, maybe this will help narrow it down...

                                        When I home and get this error, take a look at X Y and Z in DWC. X and Y should be 0 and Z 450.32mm.

                                        Screen Shot 2020-07-14 at 4.49.00 PM.png

                                        If I reset and home when the printer is "near" the home position, I get no error and the correct tool position. However, if I jog down 100mm (for example) and reset, I get this error when trying to home.

                                        This is certainly an odd situation.

                                        If I then do a G92 X0 Y0 Z-450 after I get the error and see the odd tool position then I can home with no errors.

                                        My 3D Printing blog: http://www.sublimelayers.com
                                        Coming this summer: "3D Printing Strategies - the art of perfecting your designs and prints"

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                                        • dc42undefined
                                          dc42 administrators
                                          last edited by dc42

                                          @mhackney, after resetting, please run just these commands:

                                          G91
                                          G1 H1 X1000 Y1000 Z1000 F2500

                                          and then report what XYZ coordinates are reported.

                                          Also, please post the contents of config-override.g.

                                          PS - you could also try deleting config-override.g to see if that fixes the problem, then recreate it (using M500) after running auto calibration.

                                          Duet WiFi hardware designer and firmware engineer
                                          Please do not ask me for Duet support via PM or email, use the forum
                                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                                          sLpFhaWKundefined 1 Reply Last reply Reply Quote 0
                                          • sLpFhaWKundefined
                                            sLpFhaWK @dc42
                                            last edited by

                                            @dc42

                                            So I tried this, I homed normal near my home position dropped 150mm and then reset the printer, my max home height is 452mm drops 15mm after home so everytime I reset the printer it thinks its at 437mm. After I run your commands, it stayed at the top and read 602mm and I had deleted the override file and I still got that error, without the override I got the same error even homing normally with it at it's correct height.

                                            ; This is a system-generated file - do not edit
                                            ; Delta parameters
                                            M665 L377.470 R206.427 H451.666 B140.0 X0.252 Y0.460 Z0.000
                                            M666 X0.578 Y-1.992 Z1.414 A-1.07 B-0.18
                                            ; Heater model parameters
                                            M307 H0 A90.0 C700.0 D10.0 S1.00 V0.0 B1
                                            M307 H1 A512.9 C267.0 D9.0 S1.00 V0.0 B0
                                            M307 H2 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            M307 H3 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            M307 H4 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            M307 H5 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            M307 H6 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            M307 H7 A340.0 C140.0 D5.5 S1.00 V0.0 B0
                                            
                                            

                                            -sLpFhaWK
                                            Ultibots K250v
                                            Rostock Max v2 Soon to be Full MetalMax
                                            Mini Kossel

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