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    Extruder motor gets crazy.

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    • droftartsundefined
      droftarts administrators @dutti
      last edited by

      @barbarossa-cologne said in Extruder motor gets crazy.:

      M584 X0.0 Y0.1 Z0.2:0.3:0.4:0.5 E1.0:1.1:1.2 ; set drive mapping
      M350 X16 Y16 Z16 E16:16:16:16:16:16 I1 ; configure microstepping with interpolation
      M92 X80.00 Y80.00 Z1600.00 E1600.00:1600.00:1600.00:92.70:92.70:92.70 ; set steps per mm ; set steps per mm
      M566 X900.00 Y900.00 Z12.00 E120.00:120.00:120.00:120.00:120.00:120.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X6000.00 Y6000.00 Z180.00 E3600.00:3600.00:3600.00:1200.00:1200.00:1200.00 ; set maximum speeds (mm/min)
      M201 X500.00 Y500.00 Z40.00 E250.00:250.00:250.00:250.00:250.00:250.00 ; set accelerations (mm/s^2)
      M906 X1200 Y1200 Z3000 E3000:3000:3000:1200:1200:1200 I30 ; set motor currents (mA) and motor idle factor in per cent

      Yes, configured wrong. You have defined 3 extruder axes, so the 'E' parameter on all of the above should only have 3 values. X, Y and Z parameters can only have one parameter (except in M584). Try:

      M584 X0.0 Y0.1 Z0.2:0.3:0.4:0.5 E1.0:1.1:1.2 ; set drive mapping
      M350 X16 Y16 Z16 E16:16:16 I1 ; configure microstepping with interpolation
      M92 X80.00 Y80.00 Z1600.00 E92.70:92.70:92.70 ; set steps per mm ; set steps per mm
      M566 X900.00 Y900.00 Z12.00 E120.00:120.00:120.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X6000.00 Y6000.00 Z180.00 E1200.00:1200.00:1200.00 ; set maximum speeds (mm/min)
      M201 X500.00 Y500.00 Z40.00 E250.00:250.00:250.00 ; set accelerations (mm/s^2)
      M906 X1200 Y1200 Z3000 E1200:1200:1200 I30 ; set motor currents (mA) and motor idle factor in per cent
      

      It will have been using the first 3 values for E, so I expect your extruder motors got hot getting 3A when they should have been getting 1.2A!

      Ian

      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

      duttiundefined 2 Replies Last reply Reply Quote 0
      • duttiundefined
        dutti @droftarts
        last edited by

        @droftarts
        Ok thanks...
        I´ll try it out!
        KR
        Richard

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        • duttiundefined
          dutti @droftarts
          last edited by

          @droftarts
          Different code, same problem 😕
          Any other options to solve the problem?
          thanks to all
          Richard

          
          ; Configuration file for Duet 3 (firmware version 3)
          ; executed by the firmware on start-up
          ;
          ; generated by RepRapFirmware Configuration Tool v3.1.3 on Tue Jun 23 2020 22:36:44 GMT+0200 (Mitteleuropäische Sommerzeit)
          
          ; General preferences
          G90 ; send absolute coordinates...
          M83 ; ...but relative extruder moves
          M550 P"Duet 3" ; set printer name
          
          ; Drives
          M569 P0.0 S1 ; physical drive 0.0 goes forwards
          M569 P0.1 S1 ; physical drive 0.1 goes forwards
          M569 P0.2 S1 ; physical drive 0.2 goes forwards
          M569 P0.3 S1 ; physical drive 0.3 goes forwards
          M569 P0.4 S1 ; physical drive 0.4 goes forwards
          M569 P0.5 S1 ; physical drive 0.5 goes forwards
          M569 P1.0 S0 ; physical drive 1.0 goes forwards
          M569 P1.1 S1 ; physical drive 1.1 goes forwards
          M569 P1.2 S1 ; physical drive 1.2 goes forwards
          M584 X0.0 Y0.1 Z0.2:0.3:0.4:0.5 E1.0:1.1:1.2 ; set drive mapping
          M350 X16 Y16 Z16 E16:16:16 I1 ; configure microstepping with interpolation
          M92 X80.00 Y80.00 Z1600.00 E92.70:92.70:92.70 ; set steps per mm ; set steps per mm
          M566 X900.00 Y900.00 Z12.00 E120.00:120.00:120.00 ; set maximum instantaneous speed changes (mm/min)
          M203 X6000.00 Y6000.00 Z180.00 E1200.00:1200.00:1200.00 ; set maximum speeds (mm/min)
          M201 X500.00 Y500.00 Z40.00 E250.00:250.00:250.00 ; set accelerations (mm/s^2)
          M906 X1200 Y1200 Z3000 E1200:1200:1200 I30 ; set motor currents (mA) and motor idle factor in per cent
          M84 S30 ; Set idle timeout
          
          ; Axis Limits
          M208 X0 Y0 Z0 S1 ; set axis minima
          M208 X700 Y700 Z800 S0 ; set axis maxima
          
          ; Endstops
          M574 X2 S1 P"!io3.in" ; configure active-high endstop for high end on X via pin !io3.in
          M574 Y2 S1 P"!io0.in" ; configure active-high endstop for high end on Y via pin !io0.in
          
          ; Z-Probe
          M558 P9 C"io4.in" H10 F200 T1800 ; set Z probe type to bltouch and the dive height + speeds
          M950 S0 C"io4.out" ; create servo pin 0 for BLTouch
          G31 P25 X-20 Y-20 Z2.5 ; set Z probe trigger value, offset and trigger height
          M557 X10:600 Y10:600 S200 ; define mesh grid
          
          ; Heaters
          M308 S0 P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp0
          M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
          M307 H1 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit
          M140 H0 ; map heated bed to heater 0
          M143 H0 S90 ; set temperature limit for heater 0 to 90C
          M308 S1 P"temp1" Y"thermistor" T100000 B4138                                     ; configure sensor 1 as thermistor on pin temp1
          M950 H1 C"out1" T1                                                               ; create nozzle heater output on out1 and map it to sensor 1
          M307 H1 B0 S1.00                                                                 ; disable bang-bang mode for heater  and set PWM limit
          
          ; Fans
          M950 F0 C"out3" Q500 ; create fan 0 on pin out3 and set its frequency
          M106 P0 S0.8 H-1  ; set fan 0 value. Thermostatic control is turned off
          M950 F1 C"out7" Q500 ; create fan 1 on pin out7 and set its frequency
          M106 P1 S1 H-1 ; set fan 1 value. Thermostatic control is turned off
          M950 F2 C"out8" Q500 ; create fan 2 on pin out8 and set its frequency
          M106 P2 S1 H T45 ; set fan 2 value. Thermostatic control is turned on
          
          ; Tools
          M563 P0 D0 H1 F0 ; define tool 0
          G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
          G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
          
          ; Custom settings are not defined
          M671 X-19.5:99.5:99.5:-19.5 Y110:110:540:540 S2.5
          
          ; Miscellaneous
          M501 ; load saved parameters from non-volatile memory
          M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power
          
          
          
          
          
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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            Have you calibrated the extruder yet?

            Z-Bot CoreXY Build | Thingiverse Profile

            duttiundefined 1 Reply Last reply Reply Quote 0
            • duttiundefined
              dutti @Phaedrux
              last edited by

              @Phaedrux
              No, but the seller told me that I need 92.7 steps per mm. This amount I had on a different machine and it was working perfectly.
              I have the same motor on the x + y axis and there are not hot when working.
              I think the motor still gets 3a instead of 1.2a.
              thanks a lot
              Richard

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                If you send M906 by itself, what does it report?

                You should try this extruder calibration to see if your steps per mm is correct.

                https://duet3d.dozuki.com/Guide/Ender+3+Pro+and+Duet+Maestro+Guide+Part+4:+Calibration/40#s165

                If it's extruding the right amount of filament, but the amount of filament during a print is still wrong, then there is something wrong with the slicer config.

                Z-Bot CoreXY Build | Thingiverse Profile

                duttiundefined 1 Reply Last reply Reply Quote 0
                • duttiundefined
                  dutti @Phaedrux
                  last edited by dutti

                  @Phaedrux
                  @Phaedrux said in Extruder motor gets crazy.:

                  M906

                  M906
                  Motor current (mA) - X:1200, Y:1200, Z:3000, E:1200:1200:1200, idle factor 30%

                  I think it´s correct.

                  I just extruded manually on the dwc to test the new config.g.
                  I´ll try to print.... but the motor was much faster than excepted. It´s like freaking out!

                  duttiundefined 1 Reply Last reply Reply Quote 0
                  • duttiundefined
                    dutti @dutti
                    last edited by

                    This post is deleted!
                    duttiundefined 1 Reply Last reply Reply Quote 0
                    • duttiundefined
                      dutti @dutti
                      last edited by dutti

                      @barbarossa-cologne
                      and in this situation it´s not possible to calibrate anyways. because it´s just not possible to extrude something.
                      The extruder just makes one step and jumps that step back. Problem with extruding to fast is solved!!
                      Extruder isn´t hot anymore! 🙂 --> solved
                      Maybe the motor is broken, now.
                      I´ll check that!
                      KR
                      Richard

                      Phaedruxundefined dc42undefined 2 Replies Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator @dutti
                        last edited by

                        @barbarossa-cologne said in Extruder motor gets crazy.:

                        Maybe the motor is broken, now.

                        I guess that could be possible if it was getting 3A for a long time when it's rated for 1.2A.

                        Z-Bot CoreXY Build | Thingiverse Profile

                        duttiundefined 1 Reply Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @dutti
                          last edited by

                          @barbarossa-cologne said in Extruder motor gets crazy.:

                          Maybe the motor is broken, now.
                          I´ll check that!

                          Measure the resistance of each phase. Compare them with each other and with the datasheet.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

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                          • duttiundefined
                            dutti @Phaedrux
                            last edited by

                            @Phaedrux
                            Motor wasn´t working correct after having 3a instead of 1.2a.
                            Thanks
                            Problem solved!

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