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    Tips to mitigate vertical artifacting Duet 2 Wifi

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    Tuning and tweaking
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    • brotherchrisundefined
      brotherchris @Phaedrux
      last edited by

      @Phaedrux I thought about crossing the belt's I might try that. Config and slicer profile attached. I will print a ringing test. slicer settiongs.gcode config.g

      Phaedruxundefined 1 Reply Last reply Reply Quote 0
      • brotherchrisundefined
        brotherchris
        last edited by

        @theruttmeister Great info, this is 15mm/s. 20201002_204849.jpg

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        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          That's looking a bit cleaner. Is that a faint diagonal I see or is that an artifact of the image?

          A good way to test what @theruttmeister is talking about would be to reprint that object sliced at 100mm/s and then using the speed factor to change the speed by 10mm/s every 10 layers or so.

          Z-Bot CoreXY Build | Thingiverse Profile

          brotherchrisundefined 1 Reply Last reply Reply Quote 0
          • brotherchrisundefined
            brotherchris @Phaedrux
            last edited by

            @Phaedrux Yeah, it's 45 degree striping. I will try it faster.

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            • brotherchrisundefined
              brotherchris
              last edited by brotherchris

              More pic of the stripes. Reminds me of old school A4988 candy strips. 20201002_211118.jpg 20201002_211128.jpg

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                For the sake of completeness can you provide your config.g, the results of M122 and M98 P"config.g". Maybe some more details on the printer.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • brotherchrisundefined
                  brotherchris @Phaedrux
                  last edited by

                  @Phaedrux Sure, I posted config.g above, but I can do it again. config.g m122.txt 10/2/2020, 9:23:33 PM M98 P"config.g"
                  Warning: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 265C

                  The printer is an EXO cube, almost just like this one.
                  https://www.exoslide.com/exocube-printer

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                  • Phaedruxundefined
                    Phaedrux Moderator @brotherchris
                    last edited by Phaedrux

                    @brotherchris said in Tips to mitigate vertical artifacting Duet 2 Wifi:

                    @Phaedrux I thought about crossing the belt's I might try that. Config and slicer profile attached. I will print a ringing test. slicer settiongs.gcode config.g

                    Sorry I missed those before.

                    Nothing stands out as obvious in the config.

                    Which leaves us with mechanics and the minutiae of stepper drivers.

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • brotherchrisundefined
                      brotherchris @Phaedrux
                      last edited by

                      @Phaedrux said in Tips to mitigate vertical artifacting Duet 2 Wifi:

                      minutiae

                      Totally agree, I am pretty used to troubleshooting these types of things. I have seen this before, but never on a 2660 driver. This post was mainly to see if any other Duet users were seeing this. Great discussion by the way, enjoying it.

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        You might find this interesting: https://duet3d.dozuki.com/Wiki/Tuning_Stepper_Motor_Drivers

                        Not sure how applicable or helpful it would be in this case though.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • brotherchrisundefined
                          brotherchris @fcwilt
                          last edited by

                          @fcwilt Thanks for the reply, 20201002_221416.jpg Left is normal, right is super tight belts.

                          fcwiltundefined 1 Reply Last reply Reply Quote 0
                          • brotherchrisundefined
                            brotherchris @Phaedrux
                            last edited by

                            @Phaedrux Ringing test. 20201002_225434.jpg

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by Phaedrux

                              Might be able to reduce the ringing a bit with a drop of jerk from 1200 to 700.

                              Hard to say if that would be enough to fix the benchy artifacts.

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • fcwiltundefined
                                fcwilt @brotherchris
                                last edited by

                                @brotherchris said in Tips to mitigate vertical artifacting Duet 2 Wifi:

                                @fcwilt Thanks for the reply, 20201002_221416.jpg Left is normal, right is super tight belts.

                                I wish I could remember exactly what I did to fix the problem. It was awhile ago when I had a CoreXY of my own design.

                                Frederick

                                Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

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                                • Vetiundefined
                                  Veti
                                  last edited by Veti

                                  i switched to 0.9 degrees stepper and 16 tooth pulleys.

                                  see
                                  https://forum.prusaprinters.org/forum/original-prusa-i3-mk3s-mk3-user-mods-octoprint-enclosures-nozzles-.../stepper-motor-upgrades-to-eliminate-vfa-s-vertical-fine-artifacts/

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                                  • brotherchrisundefined
                                    brotherchris
                                    last edited by

                                    Latest print, the 0.9 degree steppers are my last resort. I think I have exhausted most of my other ideas. I will switch them out today and report back.20201003_094351.jpg

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                                    • NexxCatundefined
                                      NexxCat
                                      last edited by

                                      Sorry, kinda off topic, but just put 2+2 together and realised @brotherchris was Chris Riley. Love your videos, keep up the fab work 🙂

                                      brotherchrisundefined 1 Reply Last reply Reply Quote 1
                                      • brotherchrisundefined
                                        brotherchris @NexxCat
                                        last edited by

                                        @NexxCat lol, thank you!

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                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          Yeah definitely looking like VFA. Upping your natural steps per mm on XY would be a good next step.

                                          Z-Bot CoreXY Build | Thingiverse Profile

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                                          • brotherchrisundefined
                                            brotherchris
                                            last edited by

                                            The 0.9 motors might have helped a bit, but I think this is as good as it's going to get. 1.8 on the right 0.9 on the left.20201003_145945.jpg

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