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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • dhusoloundefined
      dhusolo
      last edited by

      Started a print a few hours ago. This time got I got these error's but the heater wasn't in a fault state.

      11/4/2020, 10:04:23 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:04:21 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:04:21 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:04:21 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:04:07 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:04:03 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:03:59 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:03:55 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 10:03:52 PM	Warning: Tool 0 was not driven because its heater temperatures were not high enough or it has a heater fault
      11/4/2020, 7:56:35 PM	Height map saved to file heightmap.csv
      

      The PI became unresponsive before I could get the logs for DWC
      This is from DWS

      DWS.txt

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Is it possible there was an extrusion command issued while the heater wasn't at the min temp?

        Z-Bot CoreXY Build | Thingiverse Profile

        dhusoloundefined 1 Reply Last reply Reply Quote 0
        • dhusoloundefined
          dhusolo @Phaedrux
          last edited by

          @Phaedrux I highly doubt it. That was in the middle of a print. I had to restart the printer to get it to respond so I couldn't take a screenshot but the temp was stable until those errors started showing and it wasn't in a fault state.

          1 Reply Last reply Reply Quote 0
          • dhusoloundefined
            dhusolo
            last edited by

            Capture.PNG

            I tried with a different raspberry pi but same outcome. I was able to connect a monitor but was unable to copy the full output. This was the best I could get

            1 Reply Last reply Reply Quote 0
            • dhusoloundefined
              dhusolo
              last edited by

              So it happened again. I swapped to a Raspberry Pi 4 with new firmware.

              11/6/2020, 12:04:08 AM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 20m
              11/6/2020, 12:04:08 AM	Warning: Controller has been reset
              11/5/2020, 11:48:41 PM	Height map saved to file heightmap.csv
              11/5/2020, 11:48:41 PM	16 points probed, min error -0.018, max error 0.070, mean 0.034, deviation 0.027
              11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.027 -0.025 -0.033, points used 3, (mean, deviation) before (-0.028, 0.003) after (-0.000, 0.000)
              11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.059 -0.023 -0.016, points used 3, (mean, deviation) before (-0.031, 0.014) after (0.000, 0.000)
              11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.022 -0.039 -0.054, points used 3, (mean, deviation) before (-0.039, 0.010) after (0.000, 0.000)
              11/5/2020, 11:46:07 PM	Height map loaded from file heightmap.csv
              11/5/2020, 11:44:01 PM	M32 "0:/gcodes/a1.gcode"
              File 0:/gcodes/a1.gcode selected for printing
              
              11/6/2020, 12:12:01 AM	M122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
              Used output buffers: 1 of 40 (13 max)
              === RTOS ===
              Static ram: 154604
              Dynamic ram: 163392 of which 64 recycled
              Exception stack ram used: 544
              Never used ram: 74612
              Tasks: ETHERNET(blocked,824) NETWORK(ready,1960) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
              Owned mutexes:
              === Platform ===
              Last reset 03:23:27 ago, cause: power up
              Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 39.7, current 39.9, max 41.4
              Supply voltage: min 24.3, current 24.6, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
              Driver 0: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/160
              Driver 1: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/400
              Driver 2: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/384
              Driver 3: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
              Driver 4: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
              Driver 5: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1019
              Date/time: 2020-11-06 00:12:00
              Slowest loop: 9.38ms; fastest: 0.21ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 322, MaxWait: 302820ms
              Bed compensation in use: mesh, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 3599, completed moves: 3599, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is ready with "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon* is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 0.77ms; fastest: 0.03ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
              HTTP sessions: 0 of 8
              - Ethernet -
              State: establishingLink
              Error counts: 0 0 0 0 0
              Socket states: 0 0 0 0 0 0 0 0
              === Filament sensors ===
              Extruder 0 sensor: ok
              === CAN ===
              Messages sent 7459, longest wait 0ms for type 0
              === Linux interface ===
              State: 0, failed transfers: 8
              Last transfer: 19ms ago
              RX/TX seq numbers: 2795/56430
              SPI underruns 13, overruns 11
              Number of disconnects: 3
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.1.1
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 32.12
              

              DWS2.txt
              DCS.txt

              1 Reply Last reply Reply Quote 1
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Hi, please keep an eye out for RRF 3.2 Beta 3 which may have a fix for you. Not sure on the ETA other than.. soon.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • dhusoloundefined
                  dhusolo
                  last edited by

                  This is mostly to maintain tracking

                  Errored out a few times during printing but it didn't stop printing until 4:54:48

                  11/6/2020, 4:59:19 PM	Connection established
                  11/6/2020, 4:58:54 PM	Connection interrupted, attempting to reconnect...
                  Network error
                  11/6/2020, 4:54:57 PM	Connection established
                  11/6/2020, 4:54:48 PM	Connection interrupted, attempting to reconnect...
                  DCS has been stopped
                  11/6/2020, 4:19:04 PM	Connection to Duet established
                  11/6/2020, 4:19:04 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                  11/6/2020, 4:08:08 PM	Connection to Duet established
                  11/6/2020, 4:08:08 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                  11/6/2020, 3:50:15 PM	Connection to Duet established
                  11/6/2020, 3:50:15 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                  11/6/2020, 2:44:36 PM	Connection to Duet established
                  11/6/2020, 2:44:36 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                  11/6/2020, 1:39:53 PM	Height map saved to file heightmap.csv
                  
                  	M98 P"config.g"
                  HTTP is enabled on port 80
                  FTP is disabled
                  TELNET is disabled
                  Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
                  
                  11/6/2020, 5:01:05 PM	m122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                  Used output buffers: 1 of 40 (10 max)
                  === RTOS ===
                  Static ram: 154604
                  Dynamic ram: 163184 of which 64 recycled
                  Exception stack ram used: 528
                  Never used ram: 74836
                  Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
                  Owned mutexes:
                  === Platform ===
                  Last reset 03:27:54 ago, cause: power up
                  Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                  Error status: 0
                  MCU temperature: min 36.5, current 40.1, max 40.9
                  Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                  Driver 0: standstill, reads 30653, writes 19 timeouts 0, SG min/max 0/227
                  Driver 1: standstill, reads 30649, writes 23 timeouts 0, SG min/max 0/1023
                  Driver 2: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
                  Driver 3: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
                  Driver 4: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/1023
                  Driver 5: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/708
                  Date/time: 2020-11-06 17:01:05
                  Slowest loop: 9.23ms; fastest: 0.14ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 187934ms
                  Bed compensation in use: mesh, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves: 270437, completed moves: 270437, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === AuxDDARing ===
                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is ready with "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon* is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === Network ===
                  Slowest loop: 0.94ms; fastest: 0.01ms
                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                  HTTP sessions: 0 of 8
                  - Ethernet -
                  State: establishingLink
                  Error counts: 0 0 0 0 0
                  Socket states: 0 0 0 0 0 0 0 0
                  === Filament sensors ===
                  Extruder 0 sensor: ok
                  === CAN ===
                  Messages sent 49847, longest wait 0ms for type 0
                  === Linux interface ===
                  State: 0, failed transfers: 22
                  Last transfer: 20ms ago
                  RX/TX seq numbers: 3664/7222
                  SPI underruns 35, overruns 14
                  Number of disconnects: 1
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.1.1
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.07
                  
                  1 Reply Last reply Reply Quote 0
                  • dhusoloundefined
                    dhusolo
                    last edited by

                    Disconnected panel due

                    11/6/2020, 5:23:22 PM	Connection established
                    11/6/2020, 5:21:46 PM	Connection interrupted, attempting to reconnect...
                    DCS has been stopped
                    11/6/2020, 5:21:16 PM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 19m
                    11/6/2020, 5:21:15 PM	Warning: Controller has been reset
                    11/6/2020, 5:06:52 PM	Height map saved to file heightmap.csv
                    
                    11/6/2020, 5:23:59 PM	M122
                    === Diagnostics ===
                    RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                    Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                    Used output buffers: 1 of 40 (13 max)
                    === RTOS ===
                    Static ram: 154604
                    Dynamic ram: 163392 of which 140 recycled
                    Exception stack ram used: 544
                    Never used ram: 74536
                    Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
                    Owned mutexes:
                    === Platform ===
                    Last reset 03:50:47 ago, cause: power up
                    Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
                    Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                    Error status: 0
                    MCU temperature: min 39.5, current 39.8, max 40.3
                    Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                    12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
                    Driver 0: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                    Driver 1: standstill, reads 32787, writes 8 timeouts 0, SG min/max 0/226
                    Driver 2: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                    Driver 3: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/179
                    Driver 4: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/175
                    Driver 5: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/127
                    Date/time: 2020-11-06 17:23:58
                    Slowest loop: 9.29ms; fastest: 0.21ms
                    === Storage ===
                    Free file entries: 10
                    SD card 0 not detected, interface speed: 37.5MBytes/sec
                    SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                    === Move ===
                    Hiccups: 0(0), FreeDm: 375, MinFreeDm: 323, MaxWait: 541330ms
                    Bed compensation in use: mesh, comp offset 0.000
                    === MainDDARing ===
                    Scheduled moves: 3364, completed moves: 3364, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                    === AuxDDARing ===
                    Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                    === Heat ===
                    Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                    === GCodes ===
                    Segments left: 0
                    Movement lock held by null
                    HTTP* is ready with "M122" in state(s) 0
                    Telnet is idle in state(s) 0
                    File is idle in state(s) 0
                    USB is idle in state(s) 0
                    Aux is idle in state(s) 0
                    Trigger is idle in state(s) 0
                    Queue is idle in state(s) 0
                    LCD is idle in state(s) 0
                    SBC is idle in state(s) 0
                    Daemon* is idle in state(s) 0
                    Aux2 is idle in state(s) 0
                    Autopause is idle in state(s) 0
                    Code queue is empty.
                    === Network ===
                    Slowest loop: 0.76ms; fastest: 0.03ms
                    Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                    HTTP sessions: 0 of 8
                    - Ethernet -
                    State: establishingLink
                    Error counts: 0 0 0 0 0
                    Socket states: 0 0 0 0 0 0 0 0
                    === Filament sensors ===
                    Extruder 0 sensor: ok
                    === CAN ===
                    Messages sent 5531, longest wait 0ms for type 0
                    === Linux interface ===
                    State: 0, failed transfers: 22
                    Last transfer: 20ms ago
                    RX/TX seq numbers: 1766/48405
                    SPI underruns 38, overruns 14
                    Number of disconnects: 2
                    Buffer RX/TX: 0/0-0
                    === Duet Control Server ===
                    Duet Control Server v3.1.1
                    Code buffer space: 4096
                    Configured SPI speed: 8000000 Hz
                    Full transfers per second: 32.03
                    
                    11/6/2020, 5:24:21 PM	M98 P"config.g"
                    HTTP is enabled on port 80
                    FTP is disabled
                    TELNET is disabled
                    Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
                    

                    DWS3.txt
                    DCS3.txt

                    1 Reply Last reply Reply Quote 1
                    • dhusoloundefined
                      dhusolo
                      last edited by

                      So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                      I'm going to try the beta 3.2.3 with SBC and try again.

                      dc42undefined A Former User? 2 Replies Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @dhusolo
                        last edited by

                        @dhusolo said in Duet 3 SBC DCS has stopped:

                        So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                        I'm going to try the beta 3.2.3 with SBC and try again.

                        Sounds like a good plan to me. As with any beta, exercise caution - I suggest you baby-sit the print, at least for a while.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        1 Reply Last reply Reply Quote 0
                        • A Former User?
                          A Former User @dhusolo
                          last edited by A Former User

                          @dhusolo said in Duet 3 SBC DCS has stopped:

                          So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                          I'm going to try the beta 3.2.3 with SBC and try again.

                          I did try to tell you a few days ago.....

                          Nice to be proven correct again....

                          It must be noted that I had the same problem on 3.1.1 firmware too

                          dhusoloundefined 1 Reply Last reply Reply Quote 0
                          • dhusoloundefined
                            dhusolo @A Former User
                            last edited by

                            @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                            A Former User? 1 Reply Last reply Reply Quote 0
                            • dhusoloundefined
                              dhusolo
                              last edited by

                              After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                              The error exists even after swapping back to the original 3.1.1 pi.

                              3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                              Phaedruxundefined 1 Reply Last reply Reply Quote 0
                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by Phaedrux

                                What version is on the Duet itself?

                                See this thread for downgrading instructions.

                                https://forum.duet3d.com/topic/19257/downgrade-from-3-2beta2-to-3-1-1/

                                Z-Bot CoreXY Build | Thingiverse Profile

                                dhusoloundefined 1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo @Phaedrux
                                  last edited by dhusolo

                                  @Phaedrux thanks. I ran

                                  sudo wget -O /opt/dsf/sd/sys/Duet3Firmware_MB6HC.bin https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet3Firmware_MB6HC.bin
                                  
                                  sudo apt -y --allow-downgrades install duetsoftwareframework=3.1.1 duetcontrolserver=3.1.1 duetruntime=3.1.1 duetsd=1.0.6 duettools=3.1.1 duetwebcontrol=3.1.1 duetwebserver=3.1.0 reprapfirmware=3.1.1-1
                                  
                                  Unpacking duetruntime (3.1.1) over (3.2.0-beta3) ...
                                  Setting up duetruntime (3.1.1) ...
                                  Setting up duetwebcontrol (3.1.1) ...
                                  Setting up duetcontrolserver (3.1.1) ...
                                  Installing new version of config file /opt/dsf/conf/config.json ...
                                  Setting up duettools (3.1.1) ...
                                  Setting up duetwebserver (3.1.0) ...
                                  Setting up duetsd (1.0.6) ...
                                  Setting up reprapfirmware (3.1.1-1) ...
                                  [fatal] Could not connect to Duet (Board is not available (no header))
                                  Setting up duetsoftwareframework (3.1.1) ...
                                  
                                  
                                  1 Reply Last reply Reply Quote 0
                                  • dhusoloundefined
                                    dhusolo
                                    last edited by

                                    The cable is good. I used a continuity tester to check each pin from the duet board to the pi. Every pin had a connection to it's corresponding one. I'm starting to suspect there's an issue with the board

                                    1 Reply Last reply Reply Quote 0
                                    • dhusoloundefined
                                      dhusolo
                                      last edited by

                                      @dc42 any ideas? everything i've tried has failed. The board will work in standalone but the reason I bought it is for the benefits of with the SBC

                                      1 Reply Last reply Reply Quote 0
                                      • A Former User?
                                        A Former User @dhusolo
                                        last edited by

                                        @dhusolo said in Duet 3 SBC DCS has stopped:

                                        @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                        I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                        • Phaedruxundefined
                                          Phaedrux Moderator @A Former User
                                          last edited by

                                          @CaLviNx said in Duet 3 SBC DCS has stopped:

                                          @dhusolo said in Duet 3 SBC DCS has stopped:

                                          @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                          I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                          How bout you save us all some time and just exit the thread please.

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          A Former User? 1 Reply Last reply Reply Quote 1
                                          • Phaedruxundefined
                                            Phaedrux Moderator @dhusolo
                                            last edited by

                                            @dhusolo said in Duet 3 SBC DCS has stopped:

                                            After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                                            The error exists even after swapping back to the original 3.1.1 pi.

                                            3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                                            Can you try beta 3 again? It seems like something might have gone wrong on the update.

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