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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • dhusoloundefined
      dhusolo @Phaedrux
      last edited by

      @Phaedrux I highly doubt it. That was in the middle of a print. I had to restart the printer to get it to respond so I couldn't take a screenshot but the temp was stable until those errors started showing and it wasn't in a fault state.

      1 Reply Last reply Reply Quote 0
      • dhusoloundefined
        dhusolo
        last edited by

        Capture.PNG

        I tried with a different raspberry pi but same outcome. I was able to connect a monitor but was unable to copy the full output. This was the best I could get

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        • dhusoloundefined
          dhusolo
          last edited by

          So it happened again. I swapped to a Raspberry Pi 4 with new firmware.

          11/6/2020, 12:04:08 AM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 20m
          11/6/2020, 12:04:08 AM	Warning: Controller has been reset
          11/5/2020, 11:48:41 PM	Height map saved to file heightmap.csv
          11/5/2020, 11:48:41 PM	16 points probed, min error -0.018, max error 0.070, mean 0.034, deviation 0.027
          11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.027 -0.025 -0.033, points used 3, (mean, deviation) before (-0.028, 0.003) after (-0.000, 0.000)
          11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.059 -0.023 -0.016, points used 3, (mean, deviation) before (-0.031, 0.014) after (0.000, 0.000)
          11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.022 -0.039 -0.054, points used 3, (mean, deviation) before (-0.039, 0.010) after (0.000, 0.000)
          11/5/2020, 11:46:07 PM	Height map loaded from file heightmap.csv
          11/5/2020, 11:44:01 PM	M32 "0:/gcodes/a1.gcode"
          File 0:/gcodes/a1.gcode selected for printing
          
          11/6/2020, 12:12:01 AM	M122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
          Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
          Used output buffers: 1 of 40 (13 max)
          === RTOS ===
          Static ram: 154604
          Dynamic ram: 163392 of which 64 recycled
          Exception stack ram used: 544
          Never used ram: 74612
          Tasks: ETHERNET(blocked,824) NETWORK(ready,1960) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
          Owned mutexes:
          === Platform ===
          Last reset 03:23:27 ago, cause: power up
          Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
          Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
          Error status: 0
          MCU temperature: min 39.7, current 39.9, max 41.4
          Supply voltage: min 24.3, current 24.6, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
          Driver 0: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/160
          Driver 1: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/400
          Driver 2: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/384
          Driver 3: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
          Driver 4: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
          Driver 5: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1019
          Date/time: 2020-11-06 00:12:00
          Slowest loop: 9.38ms; fastest: 0.21ms
          === Storage ===
          Free file entries: 10
          SD card 0 not detected, interface speed: 37.5MBytes/sec
          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
          === Move ===
          Hiccups: 0(0), FreeDm: 375, MinFreeDm: 322, MaxWait: 302820ms
          Bed compensation in use: mesh, comp offset 0.000
          === MainDDARing ===
          Scheduled moves: 3599, completed moves: 3599, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
          === AuxDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
          === Heat ===
          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP* is ready with "M122" in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon* is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty.
          === Network ===
          Slowest loop: 0.77ms; fastest: 0.03ms
          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
          HTTP sessions: 0 of 8
          - Ethernet -
          State: establishingLink
          Error counts: 0 0 0 0 0
          Socket states: 0 0 0 0 0 0 0 0
          === Filament sensors ===
          Extruder 0 sensor: ok
          === CAN ===
          Messages sent 7459, longest wait 0ms for type 0
          === Linux interface ===
          State: 0, failed transfers: 8
          Last transfer: 19ms ago
          RX/TX seq numbers: 2795/56430
          SPI underruns 13, overruns 11
          Number of disconnects: 3
          Buffer RX/TX: 0/0-0
          === Duet Control Server ===
          Duet Control Server v3.1.1
          Code buffer space: 4096
          Configured SPI speed: 8000000 Hz
          Full transfers per second: 32.12
          

          DWS2.txt
          DCS.txt

          1 Reply Last reply Reply Quote 1
          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            Hi, please keep an eye out for RRF 3.2 Beta 3 which may have a fix for you. Not sure on the ETA other than.. soon.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • dhusoloundefined
              dhusolo
              last edited by

              This is mostly to maintain tracking

              Errored out a few times during printing but it didn't stop printing until 4:54:48

              11/6/2020, 4:59:19 PM	Connection established
              11/6/2020, 4:58:54 PM	Connection interrupted, attempting to reconnect...
              Network error
              11/6/2020, 4:54:57 PM	Connection established
              11/6/2020, 4:54:48 PM	Connection interrupted, attempting to reconnect...
              DCS has been stopped
              11/6/2020, 4:19:04 PM	Connection to Duet established
              11/6/2020, 4:19:04 PM	Warning: Lost connection to Duet (Board is not available (no data response))
              11/6/2020, 4:08:08 PM	Connection to Duet established
              11/6/2020, 4:08:08 PM	Warning: Lost connection to Duet (Board is not available (no data response))
              11/6/2020, 3:50:15 PM	Connection to Duet established
              11/6/2020, 3:50:15 PM	Warning: Lost connection to Duet (Board is not available (no data response))
              11/6/2020, 2:44:36 PM	Connection to Duet established
              11/6/2020, 2:44:36 PM	Warning: Lost connection to Duet (Board is not available (no data response))
              11/6/2020, 1:39:53 PM	Height map saved to file heightmap.csv
              
              	M98 P"config.g"
              HTTP is enabled on port 80
              FTP is disabled
              TELNET is disabled
              Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
              
              11/6/2020, 5:01:05 PM	m122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 154604
              Dynamic ram: 163184 of which 64 recycled
              Exception stack ram used: 528
              Never used ram: 74836
              Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
              Owned mutexes:
              === Platform ===
              Last reset 03:27:54 ago, cause: power up
              Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 36.5, current 40.1, max 40.9
              Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
              Driver 0: standstill, reads 30653, writes 19 timeouts 0, SG min/max 0/227
              Driver 1: standstill, reads 30649, writes 23 timeouts 0, SG min/max 0/1023
              Driver 2: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
              Driver 3: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
              Driver 4: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/1023
              Driver 5: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/708
              Date/time: 2020-11-06 17:01:05
              Slowest loop: 9.23ms; fastest: 0.14ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 187934ms
              Bed compensation in use: mesh, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 270437, completed moves: 270437, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is ready with "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon* is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 0.94ms; fastest: 0.01ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
              HTTP sessions: 0 of 8
              - Ethernet -
              State: establishingLink
              Error counts: 0 0 0 0 0
              Socket states: 0 0 0 0 0 0 0 0
              === Filament sensors ===
              Extruder 0 sensor: ok
              === CAN ===
              Messages sent 49847, longest wait 0ms for type 0
              === Linux interface ===
              State: 0, failed transfers: 22
              Last transfer: 20ms ago
              RX/TX seq numbers: 3664/7222
              SPI underruns 35, overruns 14
              Number of disconnects: 1
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.1.1
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 32.07
              
              1 Reply Last reply Reply Quote 0
              • dhusoloundefined
                dhusolo
                last edited by

                Disconnected panel due

                11/6/2020, 5:23:22 PM	Connection established
                11/6/2020, 5:21:46 PM	Connection interrupted, attempting to reconnect...
                DCS has been stopped
                11/6/2020, 5:21:16 PM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 19m
                11/6/2020, 5:21:15 PM	Warning: Controller has been reset
                11/6/2020, 5:06:52 PM	Height map saved to file heightmap.csv
                
                11/6/2020, 5:23:59 PM	M122
                === Diagnostics ===
                RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                Used output buffers: 1 of 40 (13 max)
                === RTOS ===
                Static ram: 154604
                Dynamic ram: 163392 of which 140 recycled
                Exception stack ram used: 544
                Never used ram: 74536
                Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
                Owned mutexes:
                === Platform ===
                Last reset 03:50:47 ago, cause: power up
                Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
                Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                Error status: 0
                MCU temperature: min 39.5, current 39.8, max 40.3
                Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
                Driver 0: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                Driver 1: standstill, reads 32787, writes 8 timeouts 0, SG min/max 0/226
                Driver 2: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                Driver 3: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/179
                Driver 4: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/175
                Driver 5: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/127
                Date/time: 2020-11-06 17:23:58
                Slowest loop: 9.29ms; fastest: 0.21ms
                === Storage ===
                Free file entries: 10
                SD card 0 not detected, interface speed: 37.5MBytes/sec
                SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                === Move ===
                Hiccups: 0(0), FreeDm: 375, MinFreeDm: 323, MaxWait: 541330ms
                Bed compensation in use: mesh, comp offset 0.000
                === MainDDARing ===
                Scheduled moves: 3364, completed moves: 3364, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === AuxDDARing ===
                Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === Heat ===
                Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP* is ready with "M122" in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                SBC is idle in state(s) 0
                Daemon* is idle in state(s) 0
                Aux2 is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty.
                === Network ===
                Slowest loop: 0.76ms; fastest: 0.03ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                HTTP sessions: 0 of 8
                - Ethernet -
                State: establishingLink
                Error counts: 0 0 0 0 0
                Socket states: 0 0 0 0 0 0 0 0
                === Filament sensors ===
                Extruder 0 sensor: ok
                === CAN ===
                Messages sent 5531, longest wait 0ms for type 0
                === Linux interface ===
                State: 0, failed transfers: 22
                Last transfer: 20ms ago
                RX/TX seq numbers: 1766/48405
                SPI underruns 38, overruns 14
                Number of disconnects: 2
                Buffer RX/TX: 0/0-0
                === Duet Control Server ===
                Duet Control Server v3.1.1
                Code buffer space: 4096
                Configured SPI speed: 8000000 Hz
                Full transfers per second: 32.03
                
                11/6/2020, 5:24:21 PM	M98 P"config.g"
                HTTP is enabled on port 80
                FTP is disabled
                TELNET is disabled
                Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
                

                DWS3.txt
                DCS3.txt

                1 Reply Last reply Reply Quote 1
                • dhusoloundefined
                  dhusolo
                  last edited by

                  So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                  I'm going to try the beta 3.2.3 with SBC and try again.

                  dc42undefined A Former User? 2 Replies Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators @dhusolo
                    last edited by

                    @dhusolo said in Duet 3 SBC DCS has stopped:

                    So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                    I'm going to try the beta 3.2.3 with SBC and try again.

                    Sounds like a good plan to me. As with any beta, exercise caution - I suggest you baby-sit the print, at least for a while.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    1 Reply Last reply Reply Quote 0
                    • A Former User?
                      A Former User @dhusolo
                      last edited by A Former User

                      @dhusolo said in Duet 3 SBC DCS has stopped:

                      So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                      I'm going to try the beta 3.2.3 with SBC and try again.

                      I did try to tell you a few days ago.....

                      Nice to be proven correct again....

                      It must be noted that I had the same problem on 3.1.1 firmware too

                      dhusoloundefined 1 Reply Last reply Reply Quote 0
                      • dhusoloundefined
                        dhusolo @A Former User
                        last edited by

                        @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                        A Former User? 1 Reply Last reply Reply Quote 0
                        • dhusoloundefined
                          dhusolo
                          last edited by

                          After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                          The error exists even after swapping back to the original 3.1.1 pi.

                          3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                          Phaedruxundefined 1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by Phaedrux

                            What version is on the Duet itself?

                            See this thread for downgrading instructions.

                            https://forum.duet3d.com/topic/19257/downgrade-from-3-2beta2-to-3-1-1/

                            Z-Bot CoreXY Build | Thingiverse Profile

                            dhusoloundefined 1 Reply Last reply Reply Quote 0
                            • dhusoloundefined
                              dhusolo @Phaedrux
                              last edited by dhusolo

                              @Phaedrux thanks. I ran

                              sudo wget -O /opt/dsf/sd/sys/Duet3Firmware_MB6HC.bin https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet3Firmware_MB6HC.bin
                              
                              sudo apt -y --allow-downgrades install duetsoftwareframework=3.1.1 duetcontrolserver=3.1.1 duetruntime=3.1.1 duetsd=1.0.6 duettools=3.1.1 duetwebcontrol=3.1.1 duetwebserver=3.1.0 reprapfirmware=3.1.1-1
                              
                              Unpacking duetruntime (3.1.1) over (3.2.0-beta3) ...
                              Setting up duetruntime (3.1.1) ...
                              Setting up duetwebcontrol (3.1.1) ...
                              Setting up duetcontrolserver (3.1.1) ...
                              Installing new version of config file /opt/dsf/conf/config.json ...
                              Setting up duettools (3.1.1) ...
                              Setting up duetwebserver (3.1.0) ...
                              Setting up duetsd (1.0.6) ...
                              Setting up reprapfirmware (3.1.1-1) ...
                              [fatal] Could not connect to Duet (Board is not available (no header))
                              Setting up duetsoftwareframework (3.1.1) ...
                              
                              
                              1 Reply Last reply Reply Quote 0
                              • dhusoloundefined
                                dhusolo
                                last edited by

                                The cable is good. I used a continuity tester to check each pin from the duet board to the pi. Every pin had a connection to it's corresponding one. I'm starting to suspect there's an issue with the board

                                1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo
                                  last edited by

                                  @dc42 any ideas? everything i've tried has failed. The board will work in standalone but the reason I bought it is for the benefits of with the SBC

                                  1 Reply Last reply Reply Quote 0
                                  • A Former User?
                                    A Former User @dhusolo
                                    last edited by

                                    @dhusolo said in Duet 3 SBC DCS has stopped:

                                    @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                    I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • Phaedruxundefined
                                      Phaedrux Moderator @A Former User
                                      last edited by

                                      @CaLviNx said in Duet 3 SBC DCS has stopped:

                                      @dhusolo said in Duet 3 SBC DCS has stopped:

                                      @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                      I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                      How bout you save us all some time and just exit the thread please.

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      A Former User? 1 Reply Last reply Reply Quote 1
                                      • Phaedruxundefined
                                        Phaedrux Moderator @dhusolo
                                        last edited by

                                        @dhusolo said in Duet 3 SBC DCS has stopped:

                                        After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                                        The error exists even after swapping back to the original 3.1.1 pi.

                                        3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                                        Can you try beta 3 again? It seems like something might have gone wrong on the update.

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        dhusoloundefined 1 Reply Last reply Reply Quote 0
                                        • A Former User?
                                          A Former User @Phaedrux
                                          last edited by

                                          @Phaedrux said in Duet 3 SBC DCS has stopped

                                          How bout you save us all some time and just exit the thread please.

                                          What why? Don't you don't like the fact that I pointed out the problem days ago, a problem that has been proven to be true, just because you don't like the fact its still a fact none the less.

                                          Phaedruxundefined dhusoloundefined 2 Replies Last reply Reply Quote 0
                                          • dhusoloundefined
                                            dhusolo @Phaedrux
                                            last edited by

                                            @Phaedrux If you're referring to the v3.1.1 in the pic that's from when I did it after switching back. when I went to the beta it showed the same error but v3.2.3

                                            I can try again to verify if you'd like

                                            1 Reply Last reply Reply Quote 0
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