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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Is it possible there was an extrusion command issued while the heater wasn't at the min temp?

      Z-Bot CoreXY Build | Thingiverse Profile

      dhusoloundefined 1 Reply Last reply Reply Quote 0
      • dhusoloundefined
        dhusolo @Phaedrux
        last edited by

        @Phaedrux I highly doubt it. That was in the middle of a print. I had to restart the printer to get it to respond so I couldn't take a screenshot but the temp was stable until those errors started showing and it wasn't in a fault state.

        1 Reply Last reply Reply Quote 0
        • dhusoloundefined
          dhusolo
          last edited by

          Capture.PNG

          I tried with a different raspberry pi but same outcome. I was able to connect a monitor but was unable to copy the full output. This was the best I could get

          1 Reply Last reply Reply Quote 0
          • dhusoloundefined
            dhusolo
            last edited by

            So it happened again. I swapped to a Raspberry Pi 4 with new firmware.

            11/6/2020, 12:04:08 AM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 20m
            11/6/2020, 12:04:08 AM	Warning: Controller has been reset
            11/5/2020, 11:48:41 PM	Height map saved to file heightmap.csv
            11/5/2020, 11:48:41 PM	16 points probed, min error -0.018, max error 0.070, mean 0.034, deviation 0.027
            11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.027 -0.025 -0.033, points used 3, (mean, deviation) before (-0.028, 0.003) after (-0.000, 0.000)
            11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.059 -0.023 -0.016, points used 3, (mean, deviation) before (-0.031, 0.014) after (0.000, 0.000)
            11/5/2020, 11:48:41 PM	Leadscrew adjustments made: -0.022 -0.039 -0.054, points used 3, (mean, deviation) before (-0.039, 0.010) after (0.000, 0.000)
            11/5/2020, 11:46:07 PM	Height map loaded from file heightmap.csv
            11/5/2020, 11:44:01 PM	M32 "0:/gcodes/a1.gcode"
            File 0:/gcodes/a1.gcode selected for printing
            
            11/6/2020, 12:12:01 AM	M122
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
            Used output buffers: 1 of 40 (13 max)
            === RTOS ===
            Static ram: 154604
            Dynamic ram: 163392 of which 64 recycled
            Exception stack ram used: 544
            Never used ram: 74612
            Tasks: ETHERNET(blocked,824) NETWORK(ready,1960) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
            Owned mutexes:
            === Platform ===
            Last reset 03:23:27 ago, cause: power up
            Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
            Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
            Error status: 0
            MCU temperature: min 39.7, current 39.9, max 41.4
            Supply voltage: min 24.3, current 24.6, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
            12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
            Driver 0: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/160
            Driver 1: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/400
            Driver 2: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/384
            Driver 3: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
            Driver 4: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1023
            Driver 5: standstill, reads 17162, writes 4 timeouts 0, SG min/max 0/1019
            Date/time: 2020-11-06 00:12:00
            Slowest loop: 9.38ms; fastest: 0.21ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 375, MinFreeDm: 322, MaxWait: 302820ms
            Bed compensation in use: mesh, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 3599, completed moves: 3599, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is ready with "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon* is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 0.77ms; fastest: 0.03ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
            HTTP sessions: 0 of 8
            - Ethernet -
            State: establishingLink
            Error counts: 0 0 0 0 0
            Socket states: 0 0 0 0 0 0 0 0
            === Filament sensors ===
            Extruder 0 sensor: ok
            === CAN ===
            Messages sent 7459, longest wait 0ms for type 0
            === Linux interface ===
            State: 0, failed transfers: 8
            Last transfer: 19ms ago
            RX/TX seq numbers: 2795/56430
            SPI underruns 13, overruns 11
            Number of disconnects: 3
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.1.1
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 32.12
            

            DWS2.txt
            DCS.txt

            1 Reply Last reply Reply Quote 1
            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              Hi, please keep an eye out for RRF 3.2 Beta 3 which may have a fix for you. Not sure on the ETA other than.. soon.

              Z-Bot CoreXY Build | Thingiverse Profile

              1 Reply Last reply Reply Quote 0
              • dhusoloundefined
                dhusolo
                last edited by

                This is mostly to maintain tracking

                Errored out a few times during printing but it didn't stop printing until 4:54:48

                11/6/2020, 4:59:19 PM	Connection established
                11/6/2020, 4:58:54 PM	Connection interrupted, attempting to reconnect...
                Network error
                11/6/2020, 4:54:57 PM	Connection established
                11/6/2020, 4:54:48 PM	Connection interrupted, attempting to reconnect...
                DCS has been stopped
                11/6/2020, 4:19:04 PM	Connection to Duet established
                11/6/2020, 4:19:04 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                11/6/2020, 4:08:08 PM	Connection to Duet established
                11/6/2020, 4:08:08 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                11/6/2020, 3:50:15 PM	Connection to Duet established
                11/6/2020, 3:50:15 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                11/6/2020, 2:44:36 PM	Connection to Duet established
                11/6/2020, 2:44:36 PM	Warning: Lost connection to Duet (Board is not available (no data response))
                11/6/2020, 1:39:53 PM	Height map saved to file heightmap.csv
                
                	M98 P"config.g"
                HTTP is enabled on port 80
                FTP is disabled
                TELNET is disabled
                Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
                
                11/6/2020, 5:01:05 PM	m122
                === Diagnostics ===
                RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                Used output buffers: 1 of 40 (10 max)
                === RTOS ===
                Static ram: 154604
                Dynamic ram: 163184 of which 64 recycled
                Exception stack ram used: 528
                Never used ram: 74836
                Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
                Owned mutexes:
                === Platform ===
                Last reset 03:27:54 ago, cause: power up
                Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
                Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                Error status: 0
                MCU temperature: min 36.5, current 40.1, max 40.9
                Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                Driver 0: standstill, reads 30653, writes 19 timeouts 0, SG min/max 0/227
                Driver 1: standstill, reads 30649, writes 23 timeouts 0, SG min/max 0/1023
                Driver 2: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
                Driver 3: standstill, reads 30650, writes 23 timeouts 0, SG min/max 0/1023
                Driver 4: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/1023
                Driver 5: standstill, reads 30651, writes 23 timeouts 0, SG min/max 0/708
                Date/time: 2020-11-06 17:01:05
                Slowest loop: 9.23ms; fastest: 0.14ms
                === Storage ===
                Free file entries: 10
                SD card 0 not detected, interface speed: 37.5MBytes/sec
                SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                === Move ===
                Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 187934ms
                Bed compensation in use: mesh, comp offset 0.000
                === MainDDARing ===
                Scheduled moves: 270437, completed moves: 270437, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === AuxDDARing ===
                Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === Heat ===
                Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP* is ready with "M122" in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                SBC is idle in state(s) 0
                Daemon* is idle in state(s) 0
                Aux2 is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty.
                === Network ===
                Slowest loop: 0.94ms; fastest: 0.01ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                HTTP sessions: 0 of 8
                - Ethernet -
                State: establishingLink
                Error counts: 0 0 0 0 0
                Socket states: 0 0 0 0 0 0 0 0
                === Filament sensors ===
                Extruder 0 sensor: ok
                === CAN ===
                Messages sent 49847, longest wait 0ms for type 0
                === Linux interface ===
                State: 0, failed transfers: 22
                Last transfer: 20ms ago
                RX/TX seq numbers: 3664/7222
                SPI underruns 35, overruns 14
                Number of disconnects: 1
                Buffer RX/TX: 0/0-0
                === Duet Control Server ===
                Duet Control Server v3.1.1
                Code buffer space: 4096
                Configured SPI speed: 8000000 Hz
                Full transfers per second: 32.07
                
                1 Reply Last reply Reply Quote 0
                • dhusoloundefined
                  dhusolo
                  last edited by

                  Disconnected panel due

                  11/6/2020, 5:23:22 PM	Connection established
                  11/6/2020, 5:21:46 PM	Connection interrupted, attempting to reconnect...
                  DCS has been stopped
                  11/6/2020, 5:21:16 PM	Cancelled printing file 0:/gcodes/a1.gcode, print time was 0h 19m
                  11/6/2020, 5:21:15 PM	Warning: Controller has been reset
                  11/6/2020, 5:06:52 PM	Height map saved to file heightmap.csv
                  
                  11/6/2020, 5:23:59 PM	M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                  Used output buffers: 1 of 40 (13 max)
                  === RTOS ===
                  Static ram: 154604
                  Dynamic ram: 163392 of which 140 recycled
                  Exception stack ram used: 544
                  Never used ram: 74536
                  Tasks: ETHERNET(blocked,832) NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2672) IDLE(ready,76)
                  Owned mutexes:
                  === Platform ===
                  Last reset 03:50:47 ago, cause: power up
                  Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                  Error status: 0
                  MCU temperature: min 39.5, current 39.8, max 40.3
                  Supply voltage: min 24.3, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
                  Driver 0: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                  Driver 1: standstill, reads 32787, writes 8 timeouts 0, SG min/max 0/226
                  Driver 2: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/1023
                  Driver 3: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/179
                  Driver 4: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/175
                  Driver 5: standstill, reads 32788, writes 7 timeouts 0, SG min/max 0/127
                  Date/time: 2020-11-06 17:23:58
                  Slowest loop: 9.29ms; fastest: 0.21ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 323, MaxWait: 541330ms
                  Bed compensation in use: mesh, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves: 3364, completed moves: 3364, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === AuxDDARing ===
                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is ready with "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon* is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === Network ===
                  Slowest loop: 0.76ms; fastest: 0.03ms
                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                  HTTP sessions: 0 of 8
                  - Ethernet -
                  State: establishingLink
                  Error counts: 0 0 0 0 0
                  Socket states: 0 0 0 0 0 0 0 0
                  === Filament sensors ===
                  Extruder 0 sensor: ok
                  === CAN ===
                  Messages sent 5531, longest wait 0ms for type 0
                  === Linux interface ===
                  State: 0, failed transfers: 22
                  Last transfer: 20ms ago
                  RX/TX seq numbers: 1766/48405
                  SPI underruns 38, overruns 14
                  Number of disconnects: 2
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.1.1
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.03
                  
                  11/6/2020, 5:24:21 PM	M98 P"config.g"
                  HTTP is enabled on port 80
                  FTP is disabled
                  TELNET is disabled
                  Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 351C
                  

                  DWS3.txt
                  DCS3.txt

                  1 Reply Last reply Reply Quote 1
                  • dhusoloundefined
                    dhusolo
                    last edited by

                    So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                    I'm going to try the beta 3.2.3 with SBC and try again.

                    dc42undefined A Former User? 2 Replies Last reply Reply Quote 0
                    • dc42undefined
                      dc42 administrators @dhusolo
                      last edited by

                      @dhusolo said in Duet 3 SBC DCS has stopped:

                      So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                      I'm going to try the beta 3.2.3 with SBC and try again.

                      Sounds like a good plan to me. As with any beta, exercise caution - I suggest you baby-sit the print, at least for a while.

                      Duet WiFi hardware designer and firmware engineer
                      Please do not ask me for Duet support via PM or email, use the forum
                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                      1 Reply Last reply Reply Quote 0
                      • A Former User?
                        A Former User @dhusolo
                        last edited by A Former User

                        @dhusolo said in Duet 3 SBC DCS has stopped:

                        So last night I swapped to standalone mode completely disconnecting the pi. I was able to print the same file I had issues with. So sounds like the issue is with the communication between the Pi and the Duet 3.

                        I'm going to try the beta 3.2.3 with SBC and try again.

                        I did try to tell you a few days ago.....

                        Nice to be proven correct again....

                        It must be noted that I had the same problem on 3.1.1 firmware too

                        dhusoloundefined 1 Reply Last reply Reply Quote 0
                        • dhusoloundefined
                          dhusolo @A Former User
                          last edited by

                          @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                          A Former User? 1 Reply Last reply Reply Quote 0
                          • dhusoloundefined
                            dhusolo
                            last edited by

                            After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                            The error exists even after swapping back to the original 3.1.1 pi.

                            3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                            Phaedruxundefined 1 Reply Last reply Reply Quote 0
                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by Phaedrux

                              What version is on the Duet itself?

                              See this thread for downgrading instructions.

                              https://forum.duet3d.com/topic/19257/downgrade-from-3-2beta2-to-3-1-1/

                              Z-Bot CoreXY Build | Thingiverse Profile

                              dhusoloundefined 1 Reply Last reply Reply Quote 0
                              • dhusoloundefined
                                dhusolo @Phaedrux
                                last edited by dhusolo

                                @Phaedrux thanks. I ran

                                sudo wget -O /opt/dsf/sd/sys/Duet3Firmware_MB6HC.bin https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet3Firmware_MB6HC.bin
                                
                                sudo apt -y --allow-downgrades install duetsoftwareframework=3.1.1 duetcontrolserver=3.1.1 duetruntime=3.1.1 duetsd=1.0.6 duettools=3.1.1 duetwebcontrol=3.1.1 duetwebserver=3.1.0 reprapfirmware=3.1.1-1
                                
                                Unpacking duetruntime (3.1.1) over (3.2.0-beta3) ...
                                Setting up duetruntime (3.1.1) ...
                                Setting up duetwebcontrol (3.1.1) ...
                                Setting up duetcontrolserver (3.1.1) ...
                                Installing new version of config file /opt/dsf/conf/config.json ...
                                Setting up duettools (3.1.1) ...
                                Setting up duetwebserver (3.1.0) ...
                                Setting up duetsd (1.0.6) ...
                                Setting up reprapfirmware (3.1.1-1) ...
                                [fatal] Could not connect to Duet (Board is not available (no header))
                                Setting up duetsoftwareframework (3.1.1) ...
                                
                                
                                1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo
                                  last edited by

                                  The cable is good. I used a continuity tester to check each pin from the duet board to the pi. Every pin had a connection to it's corresponding one. I'm starting to suspect there's an issue with the board

                                  1 Reply Last reply Reply Quote 0
                                  • dhusoloundefined
                                    dhusolo
                                    last edited by

                                    @dc42 any ideas? everything i've tried has failed. The board will work in standalone but the reason I bought it is for the benefits of with the SBC

                                    1 Reply Last reply Reply Quote 0
                                    • A Former User?
                                      A Former User @dhusolo
                                      last edited by

                                      @dhusolo said in Duet 3 SBC DCS has stopped:

                                      @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                      I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                      Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                      • Phaedruxundefined
                                        Phaedrux Moderator @A Former User
                                        last edited by

                                        @CaLviNx said in Duet 3 SBC DCS has stopped:

                                        @dhusolo said in Duet 3 SBC DCS has stopped:

                                        @CaLviNx Yea you're correct but why did you feel the need to say it like that? I was troubleshooting. I started focusing on the firmware side. When all options were exhausted i eliminated the Pi

                                        I was trying to help you and save you time, instead of listening to reason you blew it off and acted like I was speaking out of my ass

                                        How bout you save us all some time and just exit the thread please.

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        A Former User? 1 Reply Last reply Reply Quote 1
                                        • Phaedruxundefined
                                          Phaedrux Moderator @dhusolo
                                          last edited by

                                          @dhusolo said in Duet 3 SBC DCS has stopped:

                                          After upgrading to the latest beta 3.2.3 I get the error Could not connect to duet (Board is not available (no header))

                                          The error exists even after swapping back to the original 3.1.1 pi.

                                          3a65705c-3346-4f96-b84d-536c57fff93e-image.png

                                          Can you try beta 3 again? It seems like something might have gone wrong on the update.

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          dhusoloundefined 1 Reply Last reply Reply Quote 0
                                          • A Former User?
                                            A Former User @Phaedrux
                                            last edited by

                                            @Phaedrux said in Duet 3 SBC DCS has stopped

                                            How bout you save us all some time and just exit the thread please.

                                            What why? Don't you don't like the fact that I pointed out the problem days ago, a problem that has been proven to be true, just because you don't like the fact its still a fact none the less.

                                            Phaedruxundefined dhusoloundefined 2 Replies Last reply Reply Quote 0
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