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    Inconsistent results with optical encoder wheel filament sensor

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    Filament Monitor
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    • arhiundefined
      arhi
      last edited by

      bouncing is 70-100ms .. that's long, but if that analog capture is any good the signal is actually pretty straightforward and just using ST as mentioned by @alankilian might solve 99% of the issues ... it will not solve them all, but if that analog part is true ST will get it to usable state.

      74LVT14

      power with 3v3, output will be 0/3v3, and input is 5V tolerable (actually survives up to 7V)

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      • arhiundefined
        arhi
        last edited by

        you are using connlcd3 or ENC_B and that's from what I see PC7 pin

        from the datasheet

        a2e8aeea-13f9-4548-a90d-9ee9163a6af6-image.png

        I think PC7 can be configured and Schmitt input directly in the firmware. I can't find here if we can configure pin as Schmitt input by addingt something to the name like we can for invert and pullup. IMHO any endstop input should be configured with Schmitt input, dunno if it is or not...

        JohnOCFIIundefined 1 Reply Last reply Reply Quote 0
        • JohnOCFIIundefined
          JohnOCFII @arhi
          last edited by JohnOCFII

          @arhi said in Inconsistent results with optical encoder wheel filament sensor:

          you are using connlcd3 or ENC_B and that's from what I see PC7 pin

          IMHO any endstop input should be configured with Schmitt input, dunno if it is or not...

          I'm thinking I should try a different end stop connection to test. I can do that tomorrow afternoon.

          In the meantime, I was winding down for bed with a little light reading: https://www.digikey.com/htmldatasheets/production/386707/0/0/1/74lvt14.html

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          • JohnOCFIIundefined
            JohnOCFII
            last edited by

            Well, this is interesting.

            I moved the filament sensor from the
            CONN_LCD connection to the E1_STOP connection. I ran a similar vase mode cylinder (no top or bottom) and my DUET M591 results were much more consistent than anything I've seen. Speed was 15mm/sec.

            Pulse-type filament monitor on pin e1stop, disabled, sensitivity 1.200mm/pulse, allowed movement 30% to 1500%, check every 5.0mm, measured sensitivity 4.054mm/pulse, measured minimum 28%, maximum 32% over 527.0mm
            

            I can update the L parameter to be 4 and try again.

            I also captured a trace, and the Saleae still sees the messy start and end of the pulse. If these tests hold up, does that imply that the Duet RRF firmware is treating the CONN_LCD connection differently the the other endstops?

            Here's a link to the Saleae capture for the above test: https://1drv.ms/u/s!ApuOkxTDmZEzgf2ue8OdskJFAV4KT9Q?e=ucEW8v

            arhiundefined 1 Reply Last reply Reply Quote 0
            • arhiundefined
              arhi @JohnOCFII
              last edited by

              @JohnOCFII maybe when pin for e1stop is configured the schmitt trigger input is turned on.. or there's input buffer with schmitt trigger input on the board already... but 28-32% seems very good

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              • JohnOCFIIundefined
                JohnOCFII @arhi
                last edited by

                @arhi said in Inconsistent results with optical encoder wheel filament sensor:

                @JohnOCFII maybe when pin for e1stop is configured the schmitt trigger input is turned on.. or there's input buffer with schmitt trigger input on the board already... but 28-32% seems very good

                Could be. Now to do a few more tests to confirm that wasn't a fluke. I'll do another vase mode test, then move on to a regular print that includes a variety of moves up to 150mm/sec. I may also try the original wheel with more, thinner spokes.

                John

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                • JohnOCFIIundefined
                  JohnOCFII
                  last edited by

                  Here's a longer vase mode cylinder. Not quite as tight as the last one, but still a reasonable range, it would seem.

                  Pulse-type filament monitor on pin e1stop, disabled, sensitivity 4.000mm/pulse, allowed movement 30% to 1500%, check every 5.0mm, measured sensitivity 4.060mm/pulse, measured minimum 86%, maximum 109% over 1023.1mm
                  
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                  • arhiundefined
                    arhi @arhi
                    last edited by

                    @arhi said in Inconsistent results with optical encoder wheel filament sensor:

                    dunno that sound really bad, maybe move the connection to the C"^e0stop" connector, dunno if it makes a difference but I'm not getting that big span on that pin

                    😄

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                    • JohnOCFIIundefined
                      JohnOCFII
                      last edited by

                      Sure - I can try e0stop. I'll do that tomorrow. I'd agree the result isn't great - but it was better than those results I had racing above 1000.

                      arhiundefined 1 Reply Last reply Reply Quote 0
                      • arhiundefined
                        arhi @JohnOCFII
                        last edited by

                        @JohnOCFII e0stop is for sure identical as e1stop 😄 no need to test e0stop if you are already found that e1stop will work ok 🙂

                        JohnOCFIIundefined 1 Reply Last reply Reply Quote 1
                        • JohnOCFIIundefined
                          JohnOCFII @arhi
                          last edited by

                          @arhi said in Inconsistent results with optical encoder wheel filament sensor:

                          @JohnOCFII e0stop is for sure identical as e1stop 😄 no need to test e0stop if you are already found that e1stop will work ok 🙂

                          Yeah, I certainly hope e1stop and e0stop are treated the same in the firmware.

                          Now to do more testing and see what sort of range I'll get. I'm sure as I move back to a normal profile with Z-hop, pressure advance, etc, the bounds will get larger. I figure I'll do a few more of these consistent 15mm/sec tests, perhaps with different encoder wheels, to see what range I'll get under ideal conditions. It is also worth watching the logic analyzer to see if I'm getting consistent patterns.

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                          • alankilianundefined
                            alankilian
                            last edited by alankilian

                            [EDIT] I got myself confused into thinking these bounces were incoming signals on this pin and tht the filter would help reduce them.

                            BUT the bounces are really just threshold-crossings due to a slowly-moving signal and so this filter will not improve it. It actually makes the situation worse (depending on how much is due to the LED/Receiver slowly changing and how much due to noise on the signal wire.)

                            So, don't listen to what I say below.

                            @JohnOCFII The schematic shows a lowpass filter on the E1_STOP input pin that is not on the ENC_B pin.

                            Stop.png

                            It's got a cutoff frequency of about 8000 Hz which would get rid of some of those bounces.

                            If you want to, you could try to probe one of C111 or R95 and you could see the signal that's actually getting to the micro controller.

                            SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                            JohnOCFIIundefined 1 Reply Last reply Reply Quote 0
                            • fractalengineerundefined
                              fractalengineer
                              last edited by

                              Wow you've gone hard at it; it's been incredibly valuable going through the thread

                              I always had wide range but fairly consistent with mine; so I settled with increased tolerances and call it a day

                              It seems that RRF 3.2 changes the way it deals with filament sensor; could any of the changes be relevant to improving sensor accuracy?

                              https://github.com/Duet3D/RepRapFirmware/blob/v3-dev/WHATS_NEW_RRF3.md

                              Railcore II ZL

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                              • JohnOCFIIundefined
                                JohnOCFII @alankilian
                                last edited by

                                @alankilian said in Inconsistent results with optical encoder wheel filament sensor:

                                [EDIT] I got myself confused into thinking these bounces were incoming signals on this pin and tht the filter would help reduce them.

                                BUT the bounces are really just threshold-crossings due to a slowly-moving signal and so this filter will not improve it. It actually makes the situation worse (depending on how much is due to the LED/Receiver slowly changing and how much due to noise on the signal wire.)

                                So, don't listen to what I say below.

                                So -- it might still be worth building the separate debouncing Schmitt trigger?

                                alankilianundefined 1 Reply Last reply Reply Quote 0
                                • alankilianundefined
                                  alankilian @JohnOCFII
                                  last edited by

                                  @JohnOCFII Yes, I think adding a Schimtt-Trigger would be the best way for you to get repeatable results.

                                  Any old Schmitt-trigger input device will work for you as long as it can deal with 3.3 Volts. You don't need a fancy high-speed one.

                                  CD40106 would work well. If you want a DIP package, here's one:
                                  https://www.digikey.com/en/products/detail/texas-instruments/CD40106BE/376602

                                  Also, I had lunch with Otto Schmitt one time. He was an interesting fellow.

                                  If you want help wiring it up, let me know.

                                  SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                                  JohnOCFIIundefined 2 Replies Last reply Reply Quote 0
                                  • JohnOCFIIundefined
                                    JohnOCFII @alankilian
                                    last edited by

                                    @alankilian said in Inconsistent results with optical encoder wheel filament sensor:

                                    @JohnOCFII Yes, I think adding a Schimtt-Trigger would be the best way for you to get repeatable results.

                                    Any old Schmitt-trigger input device will work for you as long as it can deal with 3.3 Volts. You don't need a fancy high-speed one.

                                    CD40106 would work well. If you want a DIP package, here's one:
                                    https://www.digikey.com/en/products/detail/texas-instruments/CD40106BE/376602

                                    Also, I had lunch with Otto Schmitt one time. He was an interesting fellow.

                                    If you want help wiring it up, let me know.

                                    I'll order a couple from DigiKey. Need to think up a few others things to add to the order. It just feels weird to order something for under a dollar, than pay $8 in shipping...

                                    I'll post my guess at wiring after looking at the datasheet and before I power up anything.

                                    Thanks!

                                    John

                                    arhiundefined 1 Reply Last reply Reply Quote 0
                                    • arhiundefined
                                      arhi @JohnOCFII
                                      last edited by

                                      @JohnOCFII there's lot of things useful to have around 3d printers

                                      • leds
                                      • 1k resistors 1/8W
                                      • 10k resistors 1/8W
                                      • 1000uF 36V caps
                                      • 3.3 - 5v and 5v - 3.3V level shifters
                                      • switches
                                      • connectors
                                      • crimp terminals
                                      • crimp plyers
                                      • schmitt inverter circuits
                                      • ssr's
                                      • fet's
                                        ...
                                        ...
                                        so see what's cheap that you know how to utilize that you can get there 😄 and make that $8 irrelevant 😄 😄 😄 😄 😄 ... that's how I usually go from $9 bill to $90 bill 🙂 and ton of stuff I might use in future that I never utilize 🙂
                                      A Former User? JohnOCFIIundefined 2 Replies Last reply Reply Quote 2
                                      • A Former User?
                                        A Former User @arhi
                                        last edited by

                                        @arhi said in Inconsistent results with optical encoder wheel filament sensor:

                                        that's how I usually go from $9 bill to $90 bill and ton of stuff I might use in future that I never utilize

                                        amen! 😄

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                                        • JohnOCFIIundefined
                                          JohnOCFII @arhi
                                          last edited by

                                          @arhi said in Inconsistent results with optical encoder wheel filament sensor:

                                          so see what's cheap that you know how to utilize that you can get there 😄 and make that $8 irrelevant 😄 😄 😄 😄 😄 ... that's how I usually go from $9 bill to $90 bill 🙂 and ton of stuff I might use in future that I never utilize 🙂

                                          I wasn't quite that successful, but I did get my product amount to be twice the shipping fee. 🙂

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                                          • alankilianundefined
                                            alankilian
                                            last edited by

                                            Your filament monitor travels inspired me to take the easy route and order the parts for a magnetic filament monitor from filastruder.

                                            I printed out the case parts, did a tiny bit of scraping with a hobby knife and it's all running perfectly!

                                            Unfortunately, I wasn't thinking and I mounted it to the bottom of the extruder because it's simple. But that means that when the extruder runs to the end of the filament and stops extruding there will be up to 3mm of extrusion missing on the print before the monitor says "No filament movement".

                                            So I'm going to mount it above the extruder far enough so that the filament runs out at the monitor FIRST and there will be plenty to extruse for 3mm before the monitor finally says there's no filament movement.

                                            Unfortunately, the EZStruder doesn't have a PTFE tube connector on its input-side do I'll have to hard-mount the sensor above the extruder. No big deal, but it's just something I'll have to do.

                                            Anyway, $40 well spent in my opinion.

                                            IMG_5774.jpg

                                            IMG_5773.jpg

                                            SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

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