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    After Micro swiss DD upgrade,Extruder skips steps

    Scheduled Pinned Locked Moved Solved
    Tuning and tweaking
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    • lui2004undefined
      lui2004 @Veti
      last edited by

      @Veti

      if i activeted via console i got:

      Bed compensation in use: mesh
      
      1 Reply Last reply Reply Quote 0
      • Vetiundefined
        Veti
        last edited by

        i dont see anything in the g code that would deactivate the mesh compensation.

        lui2004undefined 1 Reply Last reply Reply Quote 0
        • lui2004undefined
          lui2004 @Veti
          last edited by

          @Veti

          Strange Things 😁

          Can i post my config and homing files to check if its all ok ?

          Vetiundefined 1 Reply Last reply Reply Quote 0
          • Vetiundefined
            Veti @lui2004
            last edited by Veti

            @lui2004
            sure

            you could also execute each line one by one from the start g code and check after each line if mesh compensation is on.

            lui2004undefined 1 Reply Last reply Reply Quote 0
            • lui2004undefined
              lui2004 @Veti
              last edited by

              @Veti

              ok thanks a lot 😉

              bed.g:

              ; bed.g
              ; called to perform automatic bed compensation via G32
              ;
              ; generated by RepRapFirmware Configuration Tool v2 on Tue May 07 2019 23:06:50 GMT+0100 (British Summer Time)
              ;M561 ; clear any bed transform
              ;G29  ; probe the bed and enable compensation
              
              M561 ; clear any bed transform
              G28 ; home
              M401 ; deploy Z probe
              G30 P0 X45 Y24 Z-99999 ; hinten rechts
              G30 P1 X198.8 Y24 Z-99999 ; hinten links
              G30 P2 X198 Y194 Z-99999 ; vorne links
              G30 P3 X45 Y194 Z-99999 S4 ; vorne rechts and report adjustments needed
              M402 ; retract probe
              

              config-override.g:

              ; config-override.g file generated in response to M500 at 2020-12-14 19:28
              ; This is a system-generated file - do not edit
              ; Heater model parameters
              M307 H0 A153.1 C665.9 D6.9 S1.00 V24.2 B0
              M307 H1 A384.5 C134.9 D2.9 S1.00 V24.3 B0
              ; Workplace coordinates
              G10 L2 P1 X0.00 Y0.00 Z0.00
              G10 L2 P2 X0.00 Y0.00 Z0.00
              G10 L2 P3 X0.00 Y0.00 Z0.00
              G10 L2 P4 X0.00 Y0.00 Z0.00
              G10 L2 P5 X0.00 Y0.00 Z0.00
              G10 L2 P6 X0.00 Y0.00 Z0.00
              G10 L2 P7 X0.00 Y0.00 Z0.00
              G10 L2 P8 X0.00 Y0.00 Z0.00
              G10 L2 P9 X0.00 Y0.00 Z0.00
              

              config.g:

              ; Configuration file for Duet WiFi (firmware version 1.21)
              ; executed by the firmware on start-up
              ;
              ; generated by RepRapFirmware Configuration Tool v2 on Tue May 07 2019 23:06:50 GMT+0100 (British Summer Time)
              
              ; General preferences
              G90                                      ; Send absolute coordinates...
              M83                                      ; ...but relative extruder moves
              
              ; Network
              M550 P"Ender 5"                          ; Set machine name
              M552 S1                                  ; Enable network
              M586 P0 S1                               ; Enable HTTP
              M586 P1 S0                               ; Disable FTP
              M586 P2 S0                               ; Disable Telnet
              
              ; Drives
              M569 P0 S1                               ; Physical drive 0 goes forwards
              M569 P1 S1                               ; Physical drive 1 goes forwards
              M569 P2 S0                               ; Physical drive 2 goes backwards
              M569 P3 S1                              ; Physical drive 3 goes forwards
              M584 X0 Y1 Z2 E3                               ; set drive mapping
              M350 X16 Y16 Z16 E16 I1							; configure microstepping with interpolation
              M92 X79.92 Y79.84 Z797.61 E277.89             ; set steps per mm
              M566 X900.00 Y900.00 Z60.00 E4000.00      ; Set maximum instantaneous speed changes (mm/min)
              M203 X30000.00 Y30000.00 Z600.00 E8000.00  ; Set maximum speeds (mm/min)
              M201 X500.00 Y500.00 Z200.00 E8000.00          ; set accelerations (mm/s^2)
              M906 X800 Y800 Z800 E1400 I30                   ; set motor currents (mA) and motor idle factor in per cent
              M84 S30                                  ; Set idle timeout
              
              
              ; Axis Limits
              M208 X0 Y0 Z0 S1                         ; Set axis minima
              M208 X235 Y235 Z300 S0                   ; Set axis maxima
              
              ; Endstops
              M574 X1 S1 P"xstop"                            ; configure active-high endstop for low end on X via pin xstop
              M574 Y1 S1 P"ystop"                            ; configure active-high endstop for low end on Y via pin ystop
              M574 Z1 S2 									   ; configure Z-probe endstop for low end on Z
              
              ;Filament Sensors
              M591 D0 P2 C"!e0_stop" S1   			   ;Extruder 1(0)
              
              
              ; Z-Probe
              M950 S0 C"exp.heater7"                         ; create servo pin 0 for BLTouch
              M558 P9 C"^zprobe.in" H5 F120 T6000           ; set Z probe type to bltouch and the dive height + speeds
              G31 P500 X41.2 Y4.5 Z2.786                  ; set Z probe trigger value, offset and trigger height
              ;M557 X41.2:221.2 Y4.5:219.5 S20                       ; define mesh grid
              M557 X41.2:219 Y15:195 S20
              M671 X28.8:198.8:198:28.8 Y24:24:194:194
              
              
              
              ; Heaters
              M308 S0 P"bedtemp" Y"thermistor" T100000 B3950 ; configure sensor 0 as thermistor on pin bedtemp
              M950 H0 C"bedheat" T0                          ; create bed heater output on bedheat and map it to sensor 0
              M307 H0 B0 S1.00                               ; disable bang-bang mode for the bed heater and set PWM limit
              M140 H0                                        ; map heated bed to heater 0
              M143 H0 S120                                   ; set temperature limit for heater 0 to 120C
              M308 S1 P"e0temp" Y"thermistor" T100000 B4725 C7.06e-8; configure sensor 1 as thermistor on pin e0temp
              M950 H1 C"e0heat" T1                           ; create nozzle heater output on e0heat and map it to sensor 1
              M143 H1 S280 								   ; set temperature limit for heater 1 to 300C
              M307 H1 B0 S1.00           
              
              ; Fans
              M950 F0 C"fan0" Q500                           ; create fan 0 on pin fan0 and set its frequency
              M106 P0 S0 H-1                                 ; set fan 0 value. Thermostatic control is turned off
              M950 F1 C"fan1" Q500                           ; create fan 1 on pin fan1 and set its frequency
              M106 P1 S1 H1 T45                              ; set fan 1 value. Thermostatic control is turned on
              
              ; Tools
              M563 P0 D0 H1                            ; Define tool 0 S3D
              G10 P0 X0 Y0 Z0                          ; Set tool 0 axis offsets
              G10 P0 R0 S0                             ; Set initial tool 0 active and standby temperatures to 0C
              
              ; Automatic saving after power loss is not enabled
              
              ; Custom settings are not configured
              M575 P1 S1 B57600 ; enable support for PanelDue
              M572 D0 S0.05 ; Pressure Advance
              M207 P0 S0.45 R0 F2100 T2100 Z0 ; Firmware Retraction
              M204 P500 T2000
              M501
              
              

              homeall.g:

              ; homeall.g
              ; called to home all axes
              ;
              ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Jul 28 2020 08:52:12 GMT+0200 (Mitteleuropäische Sommerzeit)
              G91 ; relative mode
              G1 H2 Z4 F200 ; raise head 4mm
              G1 H1 X-240 Y-240 F3000 ; move up to 240mm in the -X and -Y directions until the homing switches are triggered
              G1 H2 X4 Y4 F600; move slowly 6mm in +X and +Y directions
              G1 H1 X-10 Y-10 ; move up to 10mm in the -X and -Y directions until the homing switches are triggered
              G90 ; back to absolute mode
              G1 X73 Y106 F2000 ; put head over the centre of the bed, or wherever you want to probe
              G30 ; lower head, stop when probe triggered and set Z to trigger height
              

              homex.g:

              ; homex.g
              ; called to home the X axis
              ;
              ; generated by RepRapFirmware Configuration Tool v2 on Tue May 07 2019 23:06:50 GMT+0100 (British Summer Time)
              G91 ; relative mode
              G1 H2 Z4 F200 ; raise head to avoid dragging nozzle over the bed
              G1 H1 X-240 F3000 ; move up to 240mm in the +X direction, stopping if the homing switch is triggered
              G1 X-4 F600 ; move slowly 4mm in the -X direction
              G1 H1 X10 ; move slowly 10mm in the +X direction, stopping at the homing switch
              G1 H2 Z-4 F200 ; lower the head again
              G90 ; back to absolute mode
              

              homey.g:

              ; homey.g
              ; called to home the Y axis
              ;
              ; generated by RepRapFirmware Configuration Tool v2 on Tue May 07 2019 23:06:50 GMT+0100 (British Summer Time)
              G91 ; relative mode
              G1 H2 Z4 F200 ; raise head to avoid dragging nozzle over the bed
              G1 H1 Y-240 F3000 ; move up to 240mm in the -X direction, stopping if the homing switch is triggered
              G1 X4 F600 ; move slowly 4mm in the +X direction
              G1 H1 X-10 ; move slowly 10mm in the -X direction, stopping at the homing switch
              G1 H2 Z-4 F200 ; lower the head again
              G90 ; back to absolute mode
              

              homez.g:

              ; homez.g
              ; called to home the Z axis
              ;
              ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Jul 28 2020 08:52:37 GMT+0200 (Mitteleuropäische Sommerzeit)
              G91               ; relative positioning
              G1 H2 Z5 F6000    ; lift Z relative to current position
              G90               ; absolute positioning
              G1 X73 Y106 F6000 ; go to first probe point
              G30               ; home Z by probing the bed
              
              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Vetiundefined
                Veti
                last edited by

                remove M401 and M402 from Bed.g

                M92 X79.92 Y79.84 Z797.61 E277.89 ; set steps per mm

                are you sure those measurements are correct and backlash did not play a part in it?

                lui2004undefined 1 Reply Last reply Reply Quote 0
                • lui2004undefined
                  lui2004 @Veti
                  last edited by

                  @Veti

                  i have remove the M 401 and 402 from bed.g

                  i dont think because after a restart and start printing it will use mesh.

                  the rest of config is fine ?

                  Vetiundefined 1 Reply Last reply Reply Quote 0
                  • Vetiundefined
                    Veti @lui2004
                    last edited by

                    @lui2004

                    config otherwise looks fine.

                    as i said execture each step from the beginning of the g code file and see with M122 after each if mesh is enable, to see where it gets disabled.

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @lui2004
                      last edited by

                      @lui2004 said in After Micro swiss DD upgrade,Extruder skips steps:

                      G1 H2 X4 Y4 F600; move slowly 6mm in +X and +Y directions

                      It's a minor thing, but you should remove the H2 from that line in your homeall.

                      Were you perhaps printing an older gcode file that didn't have G29 S1 in it?

                      Z-Bot CoreXY Build | Thingiverse Profile

                      lui2004undefined 2 Replies Last reply Reply Quote 0
                      • lui2004undefined
                        lui2004 @Phaedrux
                        last edited by

                        @Phaedrux

                        how does it look ? like this:

                        G1 X4 Y4 F600; move slowly 6mm in +X and +Y directions

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                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Yes.

                          The H2 means to move without regard to endstop, which is fine for the Z axis because it hasn't been homed yet, but in the case of the X Y axis it should already be homed, so normal movement should work fine. If for some reason the homing move failed, the H2 would still allow the axis to move, which can make for a confusing error.

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • lui2004undefined
                            lui2004 @Phaedrux
                            last edited by

                            @Phaedrux said in After Micro swiss DD upgrade,Extruder skips steps:

                            Were you perhaps printing an older gcode file that didn't have G29 S1 in it?

                            after a restart it works all fine with mesh active

                            1 Reply Last reply Reply Quote 0
                            • lui2004undefined
                              lui2004
                              last edited by

                              @Veti @Phaedrux

                              After your great work to help me to solve my problem,i think i have good print results,take a look.

                              Printed with Black PLA at 200°C and Bed 50°C

                              20201218_111626.jpg

                              20201218_111644.jpg

                              20201218_111703.jpg

                              20201218_111723.jpg

                              20201218_111742.jpg

                              20201218_111806.jpg

                              20201218_111825.jpg

                              20201218_111847.jpg

                              20201218_111908.jpg

                              and here Bridge test and overhangs:

                              20201218_111922.jpg

                              20201218_111958.jpg

                              20201218_112016.jpg

                              20201218_112038.jpg

                              1 Reply Last reply Reply Quote 1
                              • Vetiundefined
                                Veti
                                last edited by

                                yes that is a very good benchy

                                1 Reply Last reply Reply Quote 0
                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  Great looking prints.

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  1 Reply Last reply Reply Quote 0
                                  • lui2004undefined
                                    lui2004
                                    last edited by lui2004

                                    i will say THANK YOU to @Phaedrux @Veti for your patience with me to solve my problems 👍 👍

                                    i have learn a lot about 3D and RepRap👍

                                    i think the post can be mark as solved 😊

                                    1 Reply Last reply Reply Quote 0
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