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Bl-Touch self extended

Scheduled Pinned Locked Moved
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  • undefined
    Heartleander81
    last edited by 15 Dec 2020, 18:18

    This screw is on max high. The pin is not fall from alone. I stand by the printer and the bl touch make "klick"

    This make the pl touch to when i heat the hotend and bed at same time.

    1 Reply Last reply Reply Quote 0
    • undefined
      Veti
      last edited by 15 Dec 2020, 19:53

      does your voltage drop when your heat both?

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      • undefined
        Heartleander81
        last edited by 15 Dec 2020, 23:34

        No, 24.3v and 12.1v constant. But when I heat the hotend and bed together, it says Toolchange for a long time at the top of DCW. DCW then takes a very long time to react to a setting, such as changing the temperature.

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        • undefined
          Veti
          last edited by 16 Dec 2020, 05:05

          post your M122 of both the duet and the toolchanger when that happens

          1 Reply Last reply Reply Quote 0
          • undefined
            Heartleander81
            last edited by Heartleander81 16 Dec 2020, 07:58

            M122
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-956L2-G43S8-6JTDG-3SJ6P-KB0UG
            Used output buffers: 1 of 40 (10 max)
            === RTOS ===
            Static ram: 154604
            Dynamic ram: 163292 of which 136 recycled
            Exception stack ram used: 224
            Never used ram: 74960
            Tasks: NETWORK(ready,1972) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4944) IDLE(ready,76)
            Owned mutexes:
            === Platform ===
            Last reset 00:50:37 ago, cause: software
            Last software reset at 2020-12-20 06:24, reason: User, spinning module LinuxInterface, available RAM 75036 bytes (slot 2)
            Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
            Error status: 0
            MCU temperature: min 28.9, current 29.5, max 29.8
            Supply voltage: min 24.7, current 24.7, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
            12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
            Driver 0: standstill, reads 24546, writes 21 timeouts 0, SG min/max 0/0
            Driver 1: standstill, reads 24546, writes 21 timeouts 0, SG min/max 0/0
            Driver 2: standstill, reads 24547, writes 21 timeouts 0, SG min/max 0/0
            Driver 3: standstill, reads 24547, writes 21 timeouts 0, SG min/max 0/0
            Driver 4: standstill, reads 24547, writes 21 timeouts 0, SG min/max 0/0
            Driver 5: standstill, reads 24548, writes 21 timeouts 0, SG min/max 0/0
            Date/time: 2020-12-20 07:15:34
            Slowest loop: 3.99ms; fastest: 0.14ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
            Bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = 2 -1 -1 -1
            Heater 1 is on, I-accum = 0.0
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is ready with "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon* is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 0.88ms; fastest: 0.01ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
            HTTP sessions: 0 of 8
            - Ethernet -
            State: disabled
            Error counts: 0 0 0 0 0
            Socket states: 0 0 0 0 0 0 0 0
            === CAN ===
            Messages sent 12121, longest wait 0ms for type 0
            === Linux interface ===
            State: 0, failed transfers: 0
            Last transfer: 16ms ago
            RX/TX seq numbers: 31465/31467
            SPI underruns 0, overruns 0
            Number of disconnects: 0
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.1.1
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 32.00
            undefined 1 Reply Last reply 16 Dec 2020, 08:06 Reply Quote 0
            • undefined
              Veti @Heartleander81
              last edited by 16 Dec 2020, 08:06

              @Heartleander81

              are you using usb to connect to your duet?
              see https://duet3d.dozuki.com/Wiki/USB_ground_loops

              1 Reply Last reply Reply Quote 0
              • undefined
                Heartleander81
                last edited by 16 Dec 2020, 08:10

                Only raspberry with spi. I doun't use Usb

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                • undefined
                  Heartleander81
                  last edited by 16 Dec 2020, 08:15

                  20201216_091452.jpg

                  This is my wiring

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                  • undefined
                    Veti
                    last edited by 16 Dec 2020, 08:44

                    normally when someone post the diagnostics without newlines, its because it was not copied from the web console and they used usb.

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                    • undefined
                      Heartleander81
                      last edited by 16 Dec 2020, 09:37

                      I have copy with my smartphone. 😅

                      But I think now my bl-touch is damaged. I have make a g32 and the bed drive in the nozzel. Bl-touch was red but nothing stop

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                      • undefined
                        Veti
                        last edited by 16 Dec 2020, 09:49

                        check the extension wire, that is know to make bad contact and cause issues.

                        undefined 1 Reply Last reply 18 Dec 2020, 08:13 Reply Quote 0
                        • undefined
                          Heartleander81
                          last edited by Heartleander81 16 Dec 2020, 10:18

                          Have make new connections last week bevor i have it install in the HevORT

                          20201216_111916.jpg

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                          • undefined
                            Heartleander81 @Veti
                            last edited by 18 Dec 2020, 08:13

                            @Veti

                            Found the bug. It was due to the contact resistance at the on-board connection. I thank you for the help and patience

                            1 Reply Last reply Reply Quote 1
                            • undefined
                              Heartleander81
                              last edited by 19 Dec 2020, 18:39

                              ok now i'm confused. Since I no longer trusted the old Bl-touch, I installed a new one. It's the same problem that it just goes in and out without me triggering it. The connection on the board is new. That happens when you print or afterwards. If I had the printer off, that didn't happen for days.

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                Heartleander81
                                last edited by 20 Dec 2020, 00:22

                                The Bl-Touch doesn't seem to be the problem, nor does the wiring. If the pin is inside or outside, DCW says "not stopped" When I have the BL-Touch off, the board tells me "at min stop" I measure 4-10mV at pin outside with pin inside 3.3V on the white cable to ground

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                                • undefined
                                  Phaedrux Moderator
                                  last edited by 20 Dec 2020, 03:24

                                  Please post your full config.g and homeall.g as well as the results of M98 P"config.g"

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  undefined 1 Reply Last reply 20 Dec 2020, 06:28 Reply Quote 0
                                  • undefined
                                    Heartleander81
                                    last edited by 20 Dec 2020, 06:27

                                    ; Configuration file for Duet 3 (firmware version 3)
                                    ; executed by the firmware on start-up
                                    ;
                                    ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit)
                                    ; General preferences
                                    G90 ; send absolute coordinates...
                                    M83 ; ...but relative extruder moves
                                    M550 P"Duet3" ; set printer name
                                    M912 P0 S-5 ; sstzt CPU Temp korrektur
                                    M669 K1 ;switch to core X/Y mode
                                    ; Drives
                                    M569 P0.0 S0 V30 D3 ; X physical drive 0.0 goes forwards
                                    M569 P0.1 S0 V30 D3 ; Y physical drive 0.1 goes forwards
                                    M569 P0.2 S1 V30 D3 ; Z1 physical drive 0.2 goes forwards
                                    M569 P0.3 S1 V30 D3 ; Z2 physical drive 0.3 goes forwards
                                    M569 P0.4 S1 V30 D3 ; Z3 physical drive 0.4 goes forwards
                                    M569 P0.5 S0 V30 D3 ; E physical drive 0.5 goes backwards
                                    M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5 ; set drive mapping
                                    M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                                    M92 X80.00 Y80.00 Z800.00 E419.00 ; set steps per mm
                                    M566 X1000.00 Y1000.00 Z300.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
                                    M203 X18000.00 Y18000.00 Z600.00 E3000.00 ; set maximum speeds (mm/min)
                                    M201 X500.00 Y500.00 Z200.00 E450.00 ; set accelerations (mm/s^2)
                                    M906 X800 Y800 Z900 E800 I30 ; set motor currents (mA) and motor idle factor in per cent
                                    M84 S120 ; Set idle timeout
                                    ; Axis Limits
                                    M208 X0 Y0 Z0 S1 ; set axis minima
                                    M208 X300 Y300 Z295 S0 ; set axis maxima
                                    ; Endstops
                                    M574 X1 S1 P"io2.in" ; configure active-high endstop for low end on X via pin io2.in
                                    M574 Y1 S1 P"io1.in" ; configure active-high endstop for low end on Y via pin io1.in
                                    M574 Z1 S2
                                    ; Z-Probe
                                    M950 S0 C"io7.out" ; create servo pin 0 for BLTouch
                                    M558 P9 C"^io7.in" H5 F400 T5000 ; set Z probe type to bltouch and the dive height + speeds
                                    G31 P500 X38.884 Y-6.578 Z2.21 ; set Z probe trigger value, offset and trigger height
                                    M557 X40:260 Y40:260 S40 ; define mesh grid
                                    M671 X-33.985:142.224:318.433 Y-16.206:312.004:-16.206 S50 ;Z lift Point Position
                                    ; Heaters
                                    M308 S0 A"Bett" P"temp0" Y"thermistor" T100000 B4100 ; configure sensor 0 as thermistor on pin temp0
                                    M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
                                    M307 H0 A176.1 C1192.2 D31.2 S1.0 V24.3 B0 ; disable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0 ; qmap heated bed to heater 0
                                    M143 H0 S120 ; set temperature limit for heater 0 to 120C
                                    M308 S1 A"Hotend" P"temp1" Y"thermistor" T100000 B4395 ; configure sensor 1 as thermistor on pin temp1
                                    M950 H1 C"out1" T1 ; create nozzle heater output on out1 and map it to sensor 1
                                    M307 H1 B0 S0.80 ; disable bang-bang mode for heater and set PWM limit
                                    M308 S2 A"Elektro" P"temp3" Y"thermistor" T100000 B4100 ; configure sensor 1 as thermistor on pin temp1
                                    M141 H2
                                    M308 S3 Y"drivers" A"Stepper" ; configure sensor 3 as temperature warning and overheat flags on the TMC2660 on Duet
                                    M308 S4 Y"mcu-temp" A"MCU" ; configure sensor 4 as thermistor on pin e1temp
                                    ; Fans
                                    M950 F1 C"out7" Q500 ; create fan 1 on pin out7 and set its frequency
                                    M106 P1 C"Hotend" S1 H1 T50 ; set fan 1 name and value. Thermostatic control is turned on
                                    M950 F0 C"out4" Q1000 ; create fan 0 on pin out4 and set its frequency
                                    M106 P0 C"Bauteil1" S0 H-1 ; set fan 0 name and value. Thermostatic control is turned off
                                    M950 F2 C"out9" Q500 ; create Light on pin out9 and set its frequency
                                    M106 P2 C"Licht" S0 H-1
                                    M950 F3 C"out8" Q500 ; create fan 3 on pin out8 and set its frequency
                                    M106 P3 H3:4 T33 ; set fan 3 value
                                    ; Tools
                                    M563 P0 S"Hotend" D0 H1 F0 ; define tool 0
                                    G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                                    G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
                                    ; Custom settings are not defined
                                    M564 S1 H0
                                    T0
                                    ; Miscellaneous
                                    ;M575 P1 S1 B57600 ; enable support for PanelDue
                                    M501 ; load saved parameters from non-volatile memory
                                    M911 S21 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                                    ; homeall file for use with dc42 Duet firmware on CoreXY printers
                                    ; This file assumes the endstop switches are at the low end of each axis.
                                    ; Reverse the X and Y movement for high-end switches.
                                    ; Adjust the bed upper and lower limits in config.g (M208 commands) to get the correct homing positions
                                    T0
                                    G91 ; relative mode
                                    G1 Z5 F400
                                    G1 H1 X-240 Y-240 F6000 ; course home X or Y
                                    G1 H1 X-240 ; course home X
                                    G1 H1 Y-240 ; course home Y
                                    G1 X4 Y4 F6000 ; move away from the endstops
                                    G1 H1 X-10 ; fine home X
                                    G1 H1 Y-10 ; fine home Y
                                    G90 ; back to absolute mode
                                    ; The following code assumes you are using a Z probe to do Z homing.
                                    ; Adjust the XY coordinates in the following to place the Z probe over a suitable spot,
                                    ; preferably near the centre of the bed if your Z probe supports that
                                    G1 X112 Y156.8 F6000
                                    G30
                                    ; This file leaves the head at the zprobe trigger height so that you can slip a piece of paper under it and then do G0 Z0 to check the height.
                                    ; If you prefer to send the printer to X0Y0Z0, un-comment the following lines
                                    ;G1 X0 Y0 F6000
                                    ;G1 Z5 F400
                                    M98 P"config.g"
                                    Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 201C
                                    Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 201C
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                                    • undefined
                                      Heartleander81 @Phaedrux
                                      last edited by Heartleander81 20 Dec 2020, 06:28

                                      @Phaedrux ok I hope that help.

                                      When I measure from ground to white I have 3.3V when retracted, <20mV when extended. DWC always says "not stopped"
                                      If I measure 5V pin to ground I have 4.94V.

                                      1 Reply Last reply Reply Quote 0
                                      • undefined
                                        Heartleander81
                                        last edited by Heartleander81 20 Dec 2020, 06:40

                                        Startcode

                                        T0
                                        G32 ; True Bed Leveling und Meshbedleveling
                                        G29 S1 P"heightmap.csv" ; Load Mesh
                                        G1 X5 Y5 Z15 F6000 ; Move the platform down 15mm
                                        ;M117 Prime the extruder
                                        G92 E0 ; reset extruder
                                        G1 E3 F200 ; Extrude 3mm
                                        ;M117 Purge Extruder
                                        G92 E0 ; reset extruder
                                        G1 Z1 F1000 ; move z up to prevent scratching of surface
                                        G1 X10 Y10 Z0.3 F5000 ; move to start-line position
                                        G1 X10 Y200 E15 F1500 ; draw 1st line
                                        G1 X10.8 Y200 F5000 ; move to side a little
                                        G1 X11.6 Y2 E30 F1500 ; draw 2nd line
                                        G1 Z17 F3000 ; Move Bed 17mm down
                                        G1 E15 F300 ; Extrude 15mm
                                        G92 E0 ; reset extruder
                                        G4 S5 ; Wait 5 second

                                        Endcode

                                        M104 S0
                                        M140 S0
                                        M107
                                        G92 E1
                                        G1 E-1 F300 ;Retract the filament
                                        G1 X5 Y300 Z290 F6000
                                        undefined 1 Reply Last reply 20 Dec 2020, 14:20 Reply Quote 0
                                        • undefined
                                          BDubs @Heartleander81
                                          last edited by 20 Dec 2020, 14:20

                                          @Heartleander81 I was just reading the BLT documentation the other day and it mentioned it being susceptible to noise from the hotbend heater wires (guessing 12/24v pwm stepping on the BLT 3.3/5v signal) Wondering if this is your issue...

                                          Of course I can't find it now to link...

                                          undefined 1 Reply Last reply 20 Dec 2020, 15:20 Reply Quote 0
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