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    Bl-Touch self extended

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    • Heartleander81undefined
      Heartleander81
      last edited by

      Only raspberry with spi. I doun't use Usb

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      • Heartleander81undefined
        Heartleander81
        last edited by

        20201216_091452.jpg

        This is my wiring

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        • Vetiundefined
          Veti
          last edited by

          normally when someone post the diagnostics without newlines, its because it was not copied from the web console and they used usb.

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          • Heartleander81undefined
            Heartleander81
            last edited by

            I have copy with my smartphone. 😅

            But I think now my bl-touch is damaged. I have make a g32 and the bed drive in the nozzel. Bl-touch was red but nothing stop

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            • Vetiundefined
              Veti
              last edited by

              check the extension wire, that is know to make bad contact and cause issues.

              Heartleander81undefined 1 Reply Last reply Reply Quote 0
              • Heartleander81undefined
                Heartleander81
                last edited by Heartleander81

                Have make new connections last week bevor i have it install in the HevORT

                20201216_111916.jpg

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                • Heartleander81undefined
                  Heartleander81 @Veti
                  last edited by

                  @Veti

                  Found the bug. It was due to the contact resistance at the on-board connection. I thank you for the help and patience

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                  • Heartleander81undefined
                    Heartleander81
                    last edited by

                    ok now i'm confused. Since I no longer trusted the old Bl-touch, I installed a new one. It's the same problem that it just goes in and out without me triggering it. The connection on the board is new. That happens when you print or afterwards. If I had the printer off, that didn't happen for days.

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                    • Heartleander81undefined
                      Heartleander81
                      last edited by

                      The Bl-Touch doesn't seem to be the problem, nor does the wiring. If the pin is inside or outside, DCW says "not stopped" When I have the BL-Touch off, the board tells me "at min stop" I measure 4-10mV at pin outside with pin inside 3.3V on the white cable to ground

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        Please post your full config.g and homeall.g as well as the results of M98 P"config.g"

                        Z-Bot CoreXY Build | Thingiverse Profile

                        Heartleander81undefined 1 Reply Last reply Reply Quote 0
                        • Heartleander81undefined
                          Heartleander81
                          last edited by

                          ; Configuration file for Duet 3 (firmware version 3)
                          ; executed by the firmware on start-up
                          ;
                          ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit)
                          
                          ; General preferences
                          G90                                                ; send absolute coordinates...
                          M83                                                ; ...but relative extruder moves
                          M550 P"Duet3"                                      ; set printer name
                          M912 P0 S-5                                        ; sstzt CPU Temp korrektur
                          
                          
                          M669 K1                                            ;switch to core X/Y mode
                          
                          ; Drives
                          M569 P0.0 S0 V30 D3                                ; X physical drive 0.0 goes forwards
                          M569 P0.1 S0 V30 D3                                ; Y physical drive 0.1 goes forwards
                          M569 P0.2 S1 V30 D3                                ; Z1 physical drive 0.2 goes forwards
                          M569 P0.3 S1 V30 D3                                ; Z2 physical drive 0.3 goes forwards
                          M569 P0.4 S1 V30 D3                                ; Z3 physical drive 0.4 goes forwards
                          M569 P0.5 S0 V30 D3                                ; E physical drive 0.5 goes backwards
                          
                          M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5                   ; set drive mapping
                          M350 X16 Y16 Z16 E16 I1                            ; configure microstepping with interpolation
                          M92 X80.00 Y80.00 Z800.00 E419.00                  ; set steps per mm
                          M566 X1000.00 Y1000.00 Z300.00 E120.00             ; set maximum instantaneous speed changes (mm/min)
                          M203 X18000.00 Y18000.00 Z600.00 E3000.00          ; set maximum speeds (mm/min)
                          M201 X500.00 Y500.00 Z200.00 E450.00               ; set accelerations (mm/s^2)
                          M906 X800 Y800 Z900 E800 I30                       ; set motor currents (mA) and motor idle factor in per cent
                          M84 S120                                           ; Set idle timeout
                          
                          ; Axis Limits
                          M208 X0 Y0 Z0 S1                                   ; set axis minima
                          M208 X300 Y300 Z295 S0                             ; set axis maxima
                          
                          ; Endstops
                          M574 X1 S1 P"io2.in"                               ; configure active-high endstop for low end on X via pin io2.in
                          M574 Y1 S1 P"io1.in"                               ; configure active-high endstop for low end on Y via pin io1.in
                          M574 Z1 S2
                          
                          ; Z-Probe
                          M950 S0 C"io7.out"                                          ; create servo pin 0 for BLTouch
                          M558 P9 C"^io7.in" H5 F400 T5000                            ; set Z probe type to bltouch and the dive height + speeds
                          G31 P500 X38.884 Y-6.578 Z2.21                              ; set Z probe trigger value, offset and trigger height
                          M557 X40:260 Y40:260 S40                                    ; define mesh grid
                          M671 X-33.985:142.224:318.433 Y-16.206:312.004:-16.206 S50  ;Z lift Point Position
                          
                          ; Heaters
                          M308 S0 A"Bett" P"temp0" Y"thermistor" T100000 B4100       ; configure sensor 0 as thermistor on pin temp0
                          M950 H0 C"out0" T0                                         ; create bed heater output on out0 and map it to sensor 0
                          M307 H0 A176.1 C1192.2 D31.2 S1.0 V24.3 B0                 ; disable bang-bang mode for the bed heater and set PWM limit
                          M140 H0                                                    ; qmap heated bed to heater 0
                          M143 H0 S120                                               ; set temperature limit for heater 0 to 120C
                          M308 S1 A"Hotend" P"temp1" Y"thermistor" T100000 B4395     ; configure sensor 1 as thermistor on pin temp1
                          M950 H1 C"out1" T1                                         ; create nozzle heater output on out1 and map it to sensor 1
                          M307 H1 B0 S0.80                                           ; disable bang-bang mode for heater  and set PWM limit
                          M308 S2 A"Elektro" P"temp3" Y"thermistor" T100000 B4100    ; configure sensor 1 as thermistor on pin temp1
                          M141 H2
                          M308 S3 Y"drivers" A"Stepper"  ; configure sensor 3 as temperature warning and overheat flags on the TMC2660 on Duet
                          M308 S4 Y"mcu-temp" A"MCU" ; configure sensor 4 as thermistor on pin e1temp
                          
                          ; Fans
                          M950 F1 C"out7" Q500                               ; create fan 1 on pin out7 and set its frequency
                          M106 P1 C"Hotend" S1 H1 T50                        ; set fan 1 name and value. Thermostatic control is turned on
                          M950 F0 C"out4" Q1000                              ; create fan 0 on pin out4 and set its frequency
                          M106 P0 C"Bauteil1" S0 H-1                         ; set fan 0 name and value. Thermostatic control is turned off
                          M950 F2 C"out9" Q500                               ; create Light on pin out9 and set its frequency
                          M106 P2 C"Licht" S0 H-1
                          M950 F3 C"out8" Q500                               ; create fan 3 on pin out8 and set its frequency                        
                          M106 P3 H3:4 T33                                   ; set fan 3 value
                          
                          ; Tools
                          M563 P0 S"Hotend" D0 H1 F0                         ; define tool 0
                          G10 P0 X0 Y0 Z0                                    ; set tool 0 axis offsets
                          G10 P0 R0 S0                                       ; set initial tool 0 active and standby temperatures to 0C
                          
                          ; Custom settings are not defined
                          M564 S1 H0
                          T0
                          
                          ; Miscellaneous
                          ;M575 P1 S1 B57600                                  ; enable support for PanelDue
                          M501                                               ; load saved parameters from non-volatile memory
                          M911 S21 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                          
                          
                          
                          ; homeall file for use with dc42 Duet firmware on CoreXY printers
                          ; This file assumes the endstop switches are at the low end of each axis.
                          ; Reverse the X and Y movement for high-end switches.
                          ; Adjust the bed upper and lower limits in config.g (M208 commands) to get the correct homing positions
                          T0
                          G91                       ; relative mode
                          G1 Z5 F400
                          G1 H1 X-240 Y-240 F6000   ; course home X or Y
                          G1 H1 X-240               ; course home X
                          G1 H1 Y-240               ; course home Y
                          G1 X4 Y4 F6000             ; move away from the endstops
                          G1 H1 X-10                ; fine home X
                          G1 H1 Y-10                ; fine home Y
                          G90                       ; back to absolute mode
                          
                          ; The following code assumes you are using a Z probe to do Z homing.
                          ; Adjust the XY coordinates in the following to place the Z probe over a suitable spot,
                          ; preferably near the centre of the bed if your Z probe supports that
                          
                          G1 X112 Y156.8 F6000
                          G30
                          ; This file leaves the head at the zprobe trigger height so that you can slip a piece of paper under it and then do G0 Z0 to check the height.
                          ; If you prefer to send the printer to X0Y0Z0, un-comment the following lines
                          ;G1 X0 Y0 F6000
                          ;G1 Z5 F400
                          
                          
                          
                          M98 P"config.g"
                          Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 201C
                          Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 201C
                          
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                          • Heartleander81undefined
                            Heartleander81 @Phaedrux
                            last edited by Heartleander81

                            @Phaedrux ok I hope that help.

                            When I measure from ground to white I have 3.3V when retracted, <20mV when extended. DWC always says "not stopped"
                            If I measure 5V pin to ground I have 4.94V.

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                            • Heartleander81undefined
                              Heartleander81
                              last edited by Heartleander81

                              Startcode

                              T0 
                              G32 		                   ; True Bed Leveling und Meshbedleveling
                              G29 S1 P"heightmap.csv"         ; Load Mesh
                              G1 X5 Y5 Z15 F6000 	           ; Move the platform down 15mm 
                              ;M117 Prime the extruder 
                              G92 E0                         ; reset extruder
                              G1 E3 F200                     ; Extrude 3mm
                              ;M117 Purge Extruder 
                              G92 E0                         ; reset extruder 
                              G1 Z1 F1000 	               ; move z up to prevent scratching of surface 
                              G1 X10 Y10 Z0.3 F5000          ; move to start-line position 
                              G1 X10 Y200 E15 F1500          ; draw 1st line 
                              G1 X10.8 Y200 F5000            ; move to side a little 
                              G1 X11.6 Y2 E30 F1500          ; draw 2nd line 
                              G1 Z17 F3000                   ; Move Bed 17mm down
                              G1 E15 F300                    ; Extrude 15mm
                              G92 E0                         ; reset extruder
                              G4 S5                          ; Wait 5 second
                              
                              
                              

                              Endcode

                              M104 S0
                              M140 S0
                              M107
                              G92 E1
                              G1 E-1 F300						;Retract the filament
                              G1 X5 Y300 Z290 F6000
                              
                              BDubsundefined 1 Reply Last reply Reply Quote 0
                              • BDubsundefined
                                BDubs @Heartleander81
                                last edited by

                                @Heartleander81 I was just reading the BLT documentation the other day and it mentioned it being susceptible to noise from the hotbend heater wires (guessing 12/24v pwm stepping on the BLT 3.3/5v signal) Wondering if this is your issue...

                                Of course I can't find it now to link...

                                Heartleander81undefined 1 Reply Last reply Reply Quote 0
                                • Heartleander81undefined
                                  Heartleander81 @BDubs
                                  last edited by

                                  @BDubs That would be an explanation. Was the fault on the board or was it from the cables? is the best way to shield the Bl-Touch?

                                  BDubsundefined 1 Reply Last reply Reply Quote 0
                                  • BDubsundefined
                                    BDubs @Heartleander81
                                    last edited by

                                    @Heartleander81 said in Bl-Touch self extended:

                                    @BDubs That would be an explanation. Was the fault on the board or was it from the cables? is the best way to shield the Bl-Touch?

                                    Still can't find it...arrg...

                                    They mentioned turning off the nozzle heater (to effectively kill the PWM signal) when probing to prevent it from being susceptible to noise.

                                    In terms of shielding, I'd try using shielded cable and be sure to properly connect the ground/drain to your chassis in such a way as to avoid a ground loop.

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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by

                                      M558 B1 will turn off the heaters during the probing move.

                                      https://duet3d.dozuki.com/Wiki/Gcode?revisionid=HEAD#Section_M558_Set_Z_probe_type

                                      @Heartleander81 said in Bl-Touch self extended:

                                      DWC always says "not stopped"

                                      Where are you seeing not stopped?
                                      How are you testing the BLTouch?

                                      If you send M401 and M402 does the pin deploy and retract?
                                      If you send G30 does the pin deploy and start to move the z axis?
                                      Does triggering the pin by hand stop movement?

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • Heartleander81undefined
                                        Heartleander81 @Phaedrux
                                        last edited by

                                        @Heartleander81 said in Bl-Touch self extended:

                                        DWC always says "not stopped"

                                        Where are you seeing not stopped?
                                        How are you testing the BLTouch?

                                        If you send M401 and M402 does the pin deploy and retract?
                                        If you send G30 does the pin deploy and start to move the z axis?
                                        Does triggering the pin by hand stop movement?

                                        On the DWC ore with M119 Z not stopped and Z-Probe not stopped

                                        M401 and M402 do the deploy and retract.
                                        G30 do it all. Deploy and start when i push the pin axes stop.

                                        But why deploy the pin when I print ore after print deploy and retract from self?

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                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          Ok, so the BLTouch is otherwise working correctly, it's just occasionally deploying the pin when it doesn't?

                                          Interference on the servo wire could be possible. Can you separate the BLtouch wires from the rest in the bundle?

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          Heartleander81undefined 2 Replies Last reply Reply Quote 0
                                          • Heartleander81undefined
                                            Heartleander81 @Phaedrux
                                            last edited by

                                            @Phaedrux I can test it. But take some time. 2-4h. When my child is go to bed, i have more time.

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