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    Need help diagnosing bad stepper output signal on Duet 3

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    • Noahundefined
      Noah
      last edited by

      I just setup a brand new duet 3 board with a Pi.
      I have X,Y,Z1,Z2,Z3 on drivers 0,1,2,3,4 and the extruder on the last driver #5. I have tried 3 different motors and then switched the extruder motor around with a Z motor by just swapping connectors from one of the 3 Z motors at the board. When the extruder motor is plugged into driver #4 it runs perfectly, and on the same cable just plugged into a Z motors driver when I manual raise or lower the bed.
      So the motor and cable is definitely working fine. I am wondering if the brand new board I have just happened to come with a bad driver or something?
      I have tried many many amp settings and accel and step settings... not matter what any motor I connect to driver #5 just makes a faint hummm and rarely will even start to rotate. If I help the shaft along while it humming it will go.

      basic config:
      G90 ; send absolute coordinates...
      M83 ; ...but relative extruder moves
      M550 P"Duet 3" ; set printer name
      M669 K1 ; select CoreXY mode

      ; Drives
      M569 P0.0 S1 ; physical drive 0.0 goes forwards
      M569 P0.1 S1 ; physical drive 0.1 goes forwards
      M569 P0.2 S1 ; physical drive 0.2 goes forwards
      M569 P0.3 S1 ; physical drive 0.3 goes forwards
      M569 P0.4 S1 ; physical drive 0.4 goes forwards
      M569 P0.5 S1 ; physical drive 0.5 goes forwards
      M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5 ; set drive mapping
      M671 X-30.109:146.1:322.309 Y-10.413:317.797:-10.413 S50
      M350 X16 Y16 Z16 E16:16:16 I1 ; configure microstepping with interpolation
      M92 X160.00 Y160.00 Z1600.00 E1600.00:1600.00:873.00 ; set steps per mm
      M566 X1200.00 Y1200.00 Z30.00 E30.00:30.00:1800.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X18000.00 Y18000.00 Z1800.00 E1800.00:1800.00:3000.00 ; set maximum speeds (mm/min)
      M201 X1600.00 Y1600.00 Z100.00 E100.00:100.00:2000.00 ; set accelerations (mm/s^2)
      M906 X1200 Y1200 Z800 E800:800:950 I30 ; set motor currents (mA) and motor idle factor in per cent
      M84 S30 ; Set idle timeout

      ; Axis Limits
      M208 X0 Y0 Z0 S1 ; set axis minima
      M208 X315 Y315 Z400 S0 ; set axis maxima

      ; Endstops
      M574 X1 S1 P"io1.in" ; configure active-high endstop for low end on X via pin io1.in
      M574 Y1 S1 P"io0.in" ; configure active-high endstop for low end on Y via pin io0.in
      M574 Z1 S2 ; configure Z-probe endstop for low end on Z

      ; Z-Probe
      M950 S0 C"io7.out" ; create servo pin 0 for BLTouch
      M558 P9 C"^io7.in" H15 F120 T9000 ; set Z probe type to bltouch and the dive height + speeds
      G31 P500 X26.5 Y-37 Z1.44 ; set Z probe trigger value, offset and trigger height
      M557 X40:190 Y15:195 S40 ; define mesh grid

      ; Heaters
      M308 S0 P"temp0" Y"pt1000" R2200 ; configure sensor 0 as PT1000 on pin temp0
      M950 H0 C"out0" T0 ; create nozzle heater output on out0 and map it to sensor 0
      M307 H0 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
      M143 H0 S460 ; set temperature limit for heater 0 to 460C
      M308 S1 P"temp1" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin temp1
      M950 H1 C"out1" T1 ; create bed heater output on out1 and map it to sensor 1
      M307 H1 B0 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit
      M140 H1 ; map heated bed to heater 1
      M143 H1 S160 ; set temperature limit for heater 1 to 160C
      M308 S2 P"temp2" Y"thermistor" T100000 B4138 ; configure sensor 2 as thermistor on pin temp2
      M950 H2 C"out2" T2 ; create chamber heater output on out2 and map it to sensor 2
      M307 H2 B0 S1.00 ; disable bang-bang mode for the chamber heater and set PWM limit
      M141 H2 ; map chamber to heater 2
      M143 H2 S150 ; set temperature limit for heater 2 to 150C

      ; Fans
      M950 F0 C"out4" Q500 ; create fan 0 on pin out4 and set its frequency
      M106 P0 S0.5 H-1 ; set fan 0 value. Thermostatic control is turned off
      M950 F1 C"out5" Q500 ; create fan 1 on pin out5 and set its frequency
      M106 P1 S0.5 H-1 ; set fan 1 value. Thermostatic control is turned off

      ; Tools
      M563 P0 D0 H0 F0 ; define tool 0
      G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

      ; Custom settings

      ; Miscellaneous
      M501 ; load saved parameters from non-volatile memory
      M911 S22 R23.5 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
      T0 ; select first tool

      M122 RESULTS

      2/13/2021, 1:57:52 PM M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.2.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
      Board ID: 08DJM-956BA-NA3TJ-6JTD2-3SD6M-9B9YT
      Used output buffers: 1 of 40 (20 max)
      === RTOS ===
      Static ram: 149788
      Dynamic ram: 62956 of which 40 recycled
      Never used RAM 146048, free system stack 126 words
      Tasks: Linux(ready,95) HEAT(blocked,297) CanReceiv(blocked,927) CanSender(blocked,348) CanClock(blocked,352) TMC(blocked,19) MAIN(running,1069) IDLE(ready,19)
      Owned mutexes: Telnet(MAIN)
      === Platform ===
      Last reset 00:18:28 ago, cause: power up
      Last software reset at 2021-02-13 12:38, reason: User, none spinning, available RAM 146048, slot 1
      Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
      Error status: 0x00
      Aux0 errors 0,0,0
      Aux1 errors 0,0,0
      MCU temperature: min 40.1, current 40.4, max 40.6
      Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
      Driver 0: position 10480, standstill, reads 23950, writes 4 timeouts 0, SG min/max 0/149
      Driver 1: position -6160, standstill, reads 23950, writes 4 timeouts 0, SG min/max 0/163
      Driver 2: position 50304, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/111
      Driver 3: position 0, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/111
      Driver 4: position 0, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/112
      Driver 5: position 0, standstill, reads 23954, writes 0 timeouts 0, SG min/max not available
      Date/time: 2021-02-13 13:57:53
      Slowest loop: 173.93ms; fastest: 0.03ms
      === Storage ===
      Free file entries: 10
      SD card 0 not detected, interface speed: 37.5MBytes/sec
      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, maxWait 49750ms, bed compensation in use: none, comp offset 0.000
      === MainDDARing ===
      Scheduled moves 29, completed moves 28, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3
      === AuxDDARing ===
      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters = 1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = 2 -1 -1 -1
      Heater 0 is on, I-accum = 0.0
      === GCodes ===
      Segments left: 0
      Movement lock held by HTTP
      HTTP* is idle in state(s) 47 8, running macro
      Telnet* is doing "M122" in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger* is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is idle in state(s) 0
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty.
      === CAN ===
      Messages queued 254, send timeouts 566, received 0, lost 0, longest wait 0ms for reply type 0, free buffers 48
      === SBC interface ===
      State: 4, failed transfers: 0
      Last transfer: 1ms ago
      RX/TX seq numbers: 39110/39110
      SPI underruns 0, overruns 0
      Number of disconnects: 0, IAP RAM available 0x2c8a8
      Buffer RX/TX: 0/0-0
      === Duet Control Server ===
      Duet Control Server v3.2.2
      HTTP:
      Buffered code: G30 ; home Z by probing the bed
      ==> 24 bytes
      Executing macro homeall.g, started by G28

      Next stack level
      Code buffer space: 4096
      Configured SPI speed: 8000000 Hz
      Full transfers per second: 36.46
      Maximum length of RX/TX data transfers: 4924/860
      ok

      Rushmere3Dundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
      • Noahundefined
        Noah
        last edited by

        This stands out to me a little... I have no clue what any of it means. I just notice irregularities on driver 5 compared to the others

        Driver 0: position 10480, standstill, reads 23950, writes 4 timeouts 0, SG min/max 0/149
        Driver 1: position -6160, standstill, reads 23950, writes 4 timeouts 0, SG min/max 0/163
        Driver 2: position 50304, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/111
        Driver 3: position 0, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/111
        Driver 4: position 0, ok, reads 23950, writes 4 timeouts 0, SG min/max 0/112
        Driver 5: position 0, standstill, reads 23954, writes 0 timeouts 0, SG min/max not available

        1 Reply Last reply Reply Quote 0
        • Rushmere3Dundefined
          Rushmere3D @Noah
          last edited by

          @Noah

          The first thing that stands out is you have defined multiple E factors in your config but you only have one Extruder, I think you meant to set multiple Z factors.

          Ie

          M350 X16 Y16 Z16 E16:16:16 I1 ; configure microstepping with interpolation
          

          Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

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          • Phaedruxundefined
            Phaedrux Moderator @Noah
            last edited by

            @Noah said in Need help diagnosing bad stepper output signal on Duet 3:

            M350 X16 Y16 Z16 E16:16:16 I1 ; configure microstepping with interpolation
            M92 X160.00 Y160.00 Z1600.00 E1600.00:1600.00:873.00 ; set steps per mm
            M566 X1200.00 Y1200.00 Z30.00 E30.00:30.00:1800.00 ; set maximum instantaneous speed changes (mm/min)
            M203 X18000.00 Y18000.00 Z1800.00 E1800.00:1800.00:3000.00 ; set maximum speeds (mm/min)
            M201 X1600.00 Y1600.00 Z100.00 E100.00:100.00:2000.00 ; set accelerations (mm/s^2)
            M906 X1200 Y1200 Z800 E800:800:950 I30 ; set motor currents (mA) and motor idle factor in per cent

            Can you remove the multiple E values from this section? You only have a single extruder, so there should only be a single E value.

            Z-Bot CoreXY Build | Thingiverse Profile

            1 Reply Last reply Reply Quote 1
            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              Can you send M98 P"config.g" and report the results?

              Z-Bot CoreXY Build | Thingiverse Profile

              Noahundefined 1 Reply Last reply Reply Quote 0
              • Noahundefined
                Noah
                last edited by

                The rrf config tool originally gave me that setup
                When I manually moved things from
                M350 X16 Y16 Z16 E16:16:16 I1 to M350 X16 Y16 Z16:16:16 E16 I1
                and so on for all the motor settings the bed would no longer home and the printer wouldn't function so I had to switch everything back

                Phaedruxundefined 1 Reply Last reply Reply Quote 0
                • Noahundefined
                  Noah @Phaedrux
                  last edited by

                  @Phaedrux said in Need help diagnosing bad stepper output signal on Duet 3:

                  P"config.g"

                  M98 P"config.g"
                  Error: in file macro line 21: M350: array too long, max length = 1
                  Error: in file macro line 22: M92: array too long, max length = 1
                  Error: in file macro line 23: M566: array too long, max length = 1
                  Error: in file macro line 24: M203: array too long, max length = 1
                  Error: in file macro line 25: M201: array too long, max length = 1
                  Error: in file macro line 26: M906: array too long, max length = 1
                  Warning: Macro file config-override.g not found

                  1 Reply Last reply Reply Quote 0
                  • Noahundefined
                    Noah
                    last edited by Noah

                    I just tried putting back these settings

                    ; Drives
                    M569 P0.0 S1 ; physical drive 0.0 goes forwards
                    M569 P0.1 S1 ; physical drive 0.1 goes forwards
                    M569 P0.2 S1 ; physical drive 0.2 goes forwards
                    M569 P0.3 S1 ; physical drive 0.3 goes forwards
                    M569 P0.4 S1 ; physical drive 0.4 goes forwards
                    M569 P0.5 S1 ; physical drive 0.5 goes forwards
                    M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5
                    M671 X-30.109:146.1:322.309 Y-10.413:317.797:-10.413 S50
                    M350 X16 Y16 Z16 E16:16:16 I1
                    M92 X160.00 Y160.00 Z1600.00:1600.00:1600.00 E873.00
                    M566 X1200.00 Y1200.00 Z30.00:30.00:30.00 E1800.00
                    M203 X18000.00 Y18000.00 Z1800.00:1800.00:1800.00 E3000.00
                    M201 X1600.00 Y1600.00 Z100.00:100.00:100.00 E2000.00
                    M906 X1200 Y1200 Z800:800:800 E950 I30
                    M84 S30

                    Same result again. The triple Z bed no longer homes or responds to G32

                    Rushmere3Dundefined 1 Reply Last reply Reply Quote 0
                    • Rushmere3Dundefined
                      Rushmere3D @Noah
                      last edited by

                      @Noah

                      If you run M98 P"config.g" again and it gives the same result as before, I think it's because you have multiple factors when you don't need them. If you tell the firmware the Z is 0.2:0.3:0.4 it knows to use one setting for all 3 steppers.

                      Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

                      Phaedruxundefined 1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator @Noah
                        last edited by

                        @Noah said in Need help diagnosing bad stepper output signal on Duet 3:

                        M350 X16 Y16 Z16 E16:16:16 I1 to M350 X16 Y16 Z16:16:16 E16 I1

                        The Z axis only needs a single entry as well. It's only when you have multiple extruder axis that each axis needs to be defined. The other axis with multiple motors all use the same settings since they aren't independent.

                        So remove the multiple Z values as well.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • Phaedruxundefined
                          Phaedrux Moderator @Rushmere3D
                          last edited by

                          @Rushmere3D JYNX again!

                          Z-Bot CoreXY Build | Thingiverse Profile

                          Rushmere3Dundefined 1 Reply Last reply Reply Quote 0
                          • Rushmere3Dundefined
                            Rushmere3D @Phaedrux
                            last edited by

                            @Phaedrux haha

                            Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

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                            • Noahundefined
                              Noah
                              last edited by

                              ok, haha
                              thank you so much for dealing with the noob over here. I corrected all of the lines after m671 to show only one value for X,Y,Z,E
                              I was just copying what the RRF config tool gave me for the multiple E motors since it did not have any option to add extra Z motors.
                              Z homing and G32 working perfect again, and I only have one data point for motor 5 now
                              Fingers crossed.

                              Phaedruxundefined 1 Reply Last reply Reply Quote 0
                              • Noahundefined
                                Noah
                                last edited by

                                as soon as the hotend heats up and it will let me send extrude and retract commands, I'll let you know if the ext motor is behaving any differently now

                                1 Reply Last reply Reply Quote 0
                                • Noahundefined
                                  Noah
                                  last edited by

                                  Hahahaha Phaedrux & Rushmere You guy are amazing!!!
                                  wish I had asked a little sooner for someone to review my code... I really caused myself a couple of days of grief over here... I have good motor function on all motors now.
                                  Now, I am off to tune my extrusion steps and try a print!|

                                  Thank You both soooooo much

                                  Noah

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                                  • Noahundefined
                                    Noah
                                    last edited by Noah

                                    Proper config for others refernce

                                    ; Drives
                                    M569 P0.0 S1 ; physical drive 0.0 goes forwards
                                    M569 P0.1 S1 ; physical drive 0.1 goes forwards
                                    M569 P0.2 S1 ; physical drive 0.2 goes forwards
                                    M569 P0.3 S1 ; physical drive 0.3 goes forwards
                                    M569 P0.4 S1 ; physical drive 0.4 goes forwards
                                    M569 P0.5 S1 ; physical drive 0.5 goes forwards
                                    M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5
                                    M671 X-30.109:146.1:322.309 Y-10.413:317.797:-10.413 S50
                                    M350 X16 Y16 Z16 E16 I1
                                    M92 X160.00 Y160.00 Z1600.00 E873.00
                                    M566 X1200.00 Y1200.00 Z30.00 E1800.00
                                    M203 X18000.00 Y18000.00 Z1800.00 E3000.00
                                    M201 X1600.00 Y1600.00 Z100.00 E2000.00
                                    M906 X1200 Y1200 Z800 E950 I30
                                    M84 S30

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                                    • Phaedruxundefined
                                      Phaedrux Moderator @Noah
                                      last edited by

                                      Glad you got it sorted.

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • Noahundefined
                                        Noah
                                        last edited by

                                        I still do have the
                                        Error: in file macro line 21: M350: array too long, max length = 1

                                        but only for the M350 line

                                        That's strange... what doesn't it like about my M350 X16 Y16 Z16 E16 I1

                                        1 Reply Last reply Reply Quote 0
                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          Please upload your actual config.g file

                                          Z-Bot CoreXY Build | Thingiverse Profile

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