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    Hang printer - Print stops with mesh leveling

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    • Phaedruxundefined
      Phaedrux Moderator @Shinomori
      last edited by

      @shinomori said in Print stops with mesh leveling:

      May need to update to 3.3. Are there mayor syntax changes that would require rewrite of all the system files?

      No, based on your config.g there isn't anything that would need to change.

      Z-Bot CoreXY Build | Thingiverse Profile

      Shinomoriundefined 1 Reply Last reply Reply Quote 0
      • Shinomoriundefined
        Shinomori @Phaedrux
        last edited by

        @phaedrux
        I keep getting a "Post content was flagged as spam by Akismet.com" when I try to post a reply.

        1 Reply Last reply Reply Quote 2
        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          I've upvoted a few posts. Please wait a few minutes and try again.

          Z-Bot CoreXY Build | Thingiverse Profile

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          • Shinomoriundefined
            Shinomori @Phaedrux
            last edited by

            @phaedrux
            The last one was just an output of the m122 and it refused it. I had a big post prepared with lots of details. I'll see if I take the M122 out if it works.

            Shinomoriundefined 1 Reply Last reply Reply Quote 1
            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              Yes it might have hit the length limit as well.

              Z-Bot CoreXY Build | Thingiverse Profile

              Shinomoriundefined 2 Replies Last reply Reply Quote 0
              • Shinomoriundefined
                Shinomori @Phaedrux
                last edited by

                @phaedrux
                I wrote this up while at the machine.

                Top of M122:
                === Diagnostics ===
                RepRapFirmware for Duet 3 MB6HC v0.6 or 1.0 version 3.0 running on Duet 3 MB6HC
                Board ID: 08DJM-956L2-G43S4-6J1F8-3SN6P-9V6QG

                Now I will tighten the lines with g1 s2 commands: to center it over the dot on the tape.

                Then I run my set home macro:
                G92 X0 Y0 Z0 E0
                G90

                Use movement keys to position in start location.

                Run set home macro again.

                Now I run a G29 and get a mesh with a shim.
                1623450150245-40df07a7-0b9d-40b3-923a-51f5cceec253-image.png

                X0 Y0 is in the middle high one is +.9. Some of this I'm sure is a tramming issue and some jankiness on the printer itself.

                Print is only 20mm diameter and first layer is .8mm should be fine for test.

                Here it is frozen up timers are jumping around like it thinks it's printing but it is not moving or extruding:

                1623450670856-ff2b12ab-277b-42de-b4c0-edb83ee817af-image.png

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                • Shinomoriundefined
                  Shinomori @Phaedrux
                  last edited by

                  @phaedrux
                  Here is the gcode with the approximate stop line highlighted It ran for less than 2 secs after heat up:
                  ; generated by PrusaSlicer 2.3.1+win64 on 2021-05-06 at 23:24:46 UTC

                  ;

                  ; external perimeters extrusion width = 1.35mm
                  ; perimeters extrusion width = 1.35mm
                  ; infill extrusion width = 1.35mm
                  ; solid infill extrusion width = 1.35mm
                  ; top infill extrusion width = 1.20mm
                  ; first layer extrusion width = 1.40mm

                  M107
                  M104 S230 ; set temperature
                  ;TYPE:Custom
                  G90
                  G29 S1

                  M109 S230 ; set temperature and wait for it to be reached
                  G21 ; set units to millimeters
                  G90 ; use absolute coordinates
                  M83 ; use relative distances for extrusion
                  ; Filament gcode
                  ;LAYER_CHANGE
                  ;Z:0.8
                  ;HEIGHT:0.8
                  G1 Z0.800 F4800.000
                  G1 E-0.60000 F2400.000
                  G1 X-12.321 Y4.326 F4800.000
                  G1 E0.60000 F2400.000
                  ;TYPE:Skirt
                  ;WIDTH:1.4
                  G1 F600.000
                  G1 X-12.509 Y3.790 E0.23191
                  G1 X-12.692 Y3.125 E0.28169
                  G1 X-12.840 Y2.442 E0.28564
                  G1 X-12.993 Y1.419 E0.42261
                  G1 X-13.051 Y0.710 E0.29038
                  G1 X-13.071 Y0.026 E0.27972
                  G1 X-13.054 Y-0.657 E0.27927
                  G1 X-12.993 Y-1.419 E0.31226
                  G1 X-12.840 Y-2.442 E0.42231
                  G1 X-12.673 Y-3.200 E0.31738
                  G1 X-12.497 Y-3.828 E0.26631
                  G1 X-12.284 Y-4.466 E0.27498
                  G1 X-12.046 Y-5.072 E0.26592
                  G1 X-11.765 Y-5.695 E0.27901
                  G1 X-11.405 Y-6.383 E0.31725
                  G1 X-10.865 Y-7.265 E0.42246
                  G1 X-10.462 Y-7.835 E0.28541
                  G1 X-9.978 Y-8.442 E0.31710
                  G1 X-9.279 Y-9.205 E0.42251
                  G1 X-8.765 Y-9.696 E0.29038
                  G1 X-8.246 Y-10.141 E0.27965
                  G1 X-7.714 Y-10.552 E0.27459
                  G1 X-7.074 Y-10.990 E0.31694
                  G1 X-6.183 Y-11.515 E0.42252
                  G1 X-5.548 Y-11.835 E0.29033

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                  • Shinomoriundefined
                    Shinomori @Shinomori
                    last edited by

                    @shinomori Pause print button responds but it never actually pauses since it seems to think it is running a command:

                    M122 after pause but before emergency stop:
                    M122
                    === Diagnostics ===
                    RepRapFirmware for Duet 3 MB6HC v0.6 or 1.0 version 3.0 running on Duet 3 MB6HC
                    Board ID: 08DJM-956L2-G43S4-6J1F8-3SN6P-9V6QG
                    Used output buffers: 1 of 32 (12 max)
                    === RTOS ===
                    Static ram: 152720
                    Dynamic ram: 148572 of which 80 recycled
                    Exception stack ram used: 396
                    Never used ram: 91448
                    Tasks: NETWORK(ready,1984) HEAT(blocked,1200) CanReceiv(suspended,3808) CanSender(suspended,1476) CanClock(blocked,1424) TMC(blocked,76) MAIN(running,3660) IDLE(ready,160)
                    Owned mutexes:
                    === Platform ===
                    Last reset 00:23:47 ago, cause: power up
                    Last software reset at 2021-06-09 23:35, reason: User, spinning module LinuxInterface, available RAM 91628 bytes (slot 2)
                    Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task 0x4e49414d
                    Error status: 0
                    Free file entries: 10
                    SD card 0 not detected, interface speed: 37.5MBytes/sec
                    SD card longest block write time: 0.0ms, max retries 0
                    MCU temperature: min 45.9, current 50.1, max 50.2
                    Supply voltage: min 23.9, current 24.0, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                    12V rail voltage: min 12.2, current 12.3, max 12.3, under voltage events: 0
                    Driver 0: standstill, reads 58670, writes 17 timeouts 0, SG min/max 0/763
                    Driver 1: standstill, reads 58671, writes 17 timeouts 0, SG min/max 0/1023
                    Driver 2: standstill, reads 58674, writes 13 timeouts 0, SG min/max 0/643
                    Driver 3: standstill, reads 58683, writes 5 timeouts 0, SG min/max 0/64
                    Driver 4: standstill, reads 58670, writes 17 timeouts 0, SG min/max 0/773
                    Driver 5: standstill, reads 58688, writes 0 timeouts 0, SG min/max not available
                    Date/time: 2021-06-11 23:34:59
                    Slowest loop: 2.32ms; fastest: 0.08ms
                    === Move ===
                    Hiccups: 0(0), FreeDm: 375, MinFreeDm: 347, MaxWait: 475680ms
                    Bed compensation in use: none, comp offset 0.000
                    === MainDDARing ===
                    Scheduled moves: 103, completed moves: 103, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                    === AuxDDARing ===
                    Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                    === Heat ===
                    Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                    Heater 0 is on, I-accum = 0.4
                    === GCodes ===
                    Segments left: 0
                    Stack records: 2 allocated, 0 in use
                    Movement lock held by file
                    http* is doing "M25" in state(s) 0
                    telnet is idle in state(s) 0
                    file* is idle in state(s) 0
                    serial is idle in state(s) 0
                    aux is idle in state(s) 0
                    daemon* is ready with "M122" in state(s) 0
                    queue is idle in state(s) 0
                    lcd is idle in state(s) 0
                    spi is idle in state(s) 0
                    autopause is idle in state(s) 0
                    Code queue is empty.
                    === Network ===
                    Slowest loop: 1.01ms; fastest: 0.01ms
                    Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                    HTTP sessions: 0 of 8

                    • Ethernet -
                      State: 0
                      Error counts: 0 0 0 0 0
                      Socket states: 0 0 0 0 0 0 0 0
                      === CAN ===
                      Messages sent 5100, longest wait 0ms for type 0
                      === Linux interface ===
                      State: 0, failed transfers: 0
                      Last transfer: 14ms ago
                      RX/TX seq numbers: 45924/45925
                      SPI underruns 0, overruns 0
                      Number of disconnects: 0
                      Buffer RX/TX: 0/0-0
                      === Duet Control Server ===
                      Duet Control Server v1.1.0.5
                      HTTP:
                      Buffered code: M25
                      => 20 bytes
                      File:
                      Number of lock/unlock requests: 1/0
                      Code buffer space: 4096
                      Configured SPI speed: 2000000 Hz
                      Full transfers per second: 32.61
                      Processing print job /opt/dsf/sd/gcodes/Shape-Cylinder.gcode
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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Running sudo apt update and sudo apt upgrade on the Pi should get you updated to 3.2.2 and might give you better results. Much has changed since 3.0

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Shinomoriundefined 1 Reply Last reply Reply Quote 0
                      • Shinomoriundefined
                        Shinomori @Phaedrux
                        last edited by

                        @phaedrux Emergency stopped the machine rehomed and ran again. Stopped in the same place, but this time says: M25
                        Error: Code has been cancelled Think that may be because of attempted pause because it didn't do it the first time.

                        Video of it trying to print.

                        https://drive.google.com/file/d/1LZMMEUyWGRScdTSb7rXbOwDcd-6Qup9i/view?usp=sharing

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                        • Shinomoriundefined
                          Shinomori @Phaedrux
                          last edited by

                          @phaedrux Got it. Will run that update when I am at the machine again and see if it fixes anything.

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                          • Shinomoriundefined
                            Shinomori @Shinomori
                            last edited by Shinomori

                            @shinomori
                            Ok we ran the update and upgrade on the pi till it showed nothing left to update.

                            Looks like I messed up something somewhere.

                            Can't connect to duet3.local anymore, but the ip address works.

                            Showing duet webcontrol 3.3.0 now.

                            And we're getting this now.
                            23d29bdc-e5a5-4f73-9044-39cf146e163b-image.png

                            Also getting an "Warning: Incompatible firmware, please upgrade as soon as possible" error on boot.

                            Does format of the config need to be changed?

                            When trying to send console commands now the machine keeps getting stuck with the send button spinning and have to restart it to be able to send commands again. Usually get 1 or 2 before it freezes.

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                            • Shinomoriundefined
                              Shinomori
                              last edited by

                              Ok I was able to get it approximately homed using the console. The freezing started happening less. I tried to simulate the gcode file from before by right clicking on the file in the jobs tab and got:
                              M37 P"0:/gcodes/Shape-Cylinder.gcode"
                              Error: GCode file "0:/gcodes/Shape-Cylinder.gcode" not found

                              I tried just running it with the g29 s1 left in. The screen never changed from above picture so i have no idea what the printer is doing and no control apart from console commands. It did seem to get past the first part of the circle and the height map is still showing so it appears the update fixed the stopping with mesh enabled. Not just to figure out why i have no print control and can't connect via hostname.

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by Phaedrux

                                Please send M122 and post the output. We're looking to see what firmware is reported and what version DSF is reported for the Pi.

                                Z-Bot CoreXY Build | Thingiverse Profile

                                o_lampeundefined Shinomoriundefined 2 Replies Last reply Reply Quote 0
                                • o_lampeundefined
                                  o_lampe @Phaedrux
                                  last edited by

                                  @phaedrux
                                  A bit OT, but you mentioned 'self levelling concrete' in another thread and I thought, this machine is a pretty good candidate to try?

                                  @dc42
                                  definitely OT: in this thread I asked a question about a hangprinter, but I had a different machine in mind. Now that I see this machine, I understand your reply better. I will refine my question and I hope you find the time to answer...

                                  Shinomoriundefined 1 Reply Last reply Reply Quote 1
                                  • Shinomoriundefined
                                    Shinomori @o_lampe
                                    last edited by

                                    @o_lampe
                                    I could see that working to make a build platform for a hangprinter.

                                    For our application it's not something we're even looking at. The next version of ours is to have a high volume pellet extruder and print directly on the ground. Figuring out a mesh level or heavy raft compensation for uneven build surface is going to be essential. The prints we would like to attempt with our v2 won't even fit through the door that the current test platform is in. The only part that will stay the same is the duet board.

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                                    • Shinomoriundefined
                                      Shinomori @Phaedrux
                                      last edited by

                                      @phaedrux
                                      Do you think it would be good to just flash the whole thing to the newest version of the duet pi and just copy over the current config files so I know it is the newest version?

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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by Phaedrux

                                        Yes that's an option if sudo apt update sudo apt upgrade isn't able to update the board.

                                        Using USB to flash the board to the latest and then using a fresh download of Duet PI to burn a new Pi SD card and then updating would get you up to date.

                                        https://duet3d.dozuki.com/Wiki/Installing_and_Updating_Firmware

                                        To backup the config either download your files from DWC, or pull them off the Pi virtual SD card in /opt/dsf/sd

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • Shinomoriundefined
                                          Shinomori @Phaedrux
                                          last edited by Shinomori

                                          @phaedrux
                                          The update seemed to work and the print continued past the hold up spot, but the UI was completely messed up.

                                          If i just copy all the system files from the web ui and then copy them back. That should work?
                                          I have limited time at the printer and it is a 20 minute drive to get to it so doing a fresh install and copy over config seems like more sure fire way to get up and going. I'll give it a shot when I get over to the printer later today.

                                          Thanks

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                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Did you verify with M122 or M115 that the firmware was updated?

                                            How was the UI messed up?

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            Shinomoriundefined 1 Reply Last reply Reply Quote 0
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