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    Duet 3. ? faulty Driver0. Post requested by Duet

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    • DavidSimcockundefined
      DavidSimcock @T3P3Tony
      last edited by

      @t3p3tony said in Duet 3. ? faulty Driver0. Post requested by Duet:

      @davidsimcock I would rename the current homey.g to homey.g.backup then make a new homey.g with the contents above. then yes G28 X, then G28 Y

      OK...I've done that. The result is that the x axis motor is de-energised at the end of the process.

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        After homing is complete can you send M906 and M913 by itself and report back what it says?

        Another thing to try is to completely backup your current config, remove it all, and start with a fresh basic config from the online tool.

        https://configtool.reprapfirmware.org/Start

        Z-Bot CoreXY Build | Thingiverse Profile

        DavidSimcockundefined 1 Reply Last reply Reply Quote 1
        • DavidSimcockundefined
          DavidSimcock @Phaedrux
          last edited by

          @phaedrux said in Duet 3. ? faulty Driver0. Post requested by Duet:

          After homing is complete can you send M906 and M913 by itself and report back what it says?

          Another thing to try is to completely backup your current config, remove it all, and start with a fresh basic config from the online tool.

          https://configtool.reprapfirmware.org/Start

          Thanks. Here are the M906 and M913

          M906.txt

          M913.txt

          dc42undefined 1 Reply Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators @DavidSimcock
            last edited by

            @davidsimcock from your config-axes.g file:

            ; Axes configuration executed by config.g
            M584 X0.0 Y0.1:0.3 Z0.2:0.4
            ...
            M669 K0 X1:0:0:0 Y0:1:0:1 Z0:0:1:0

            You are defining 3 physical axes but your M669 command assumes 4. Try changing the M669 command to this:

            M669 K0 X1:0:0 Y0:1:0 Z0:0:1

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            DavidSimcockundefined 1 Reply Last reply Reply Quote 0
            • DavidSimcockundefined
              DavidSimcock @dc42
              last edited by

              @dc42 said in Duet 3. ? faulty Driver0. Post requested by Duet:

              @davidsimcock from your config-axes.g file:

              ; Axes configuration executed by config.g
              M584 X0.0 Y0.1:0.3 Z0.2:0.4
              ...
              M669 K0 X1:0:0:0 Y0:1:0:1 Z0:0:1:0

              You are defining 3 physical axes but your M669 command assumes 4. Try changing the M669 command to this:

              M669 K0 X1:0:0 Y0:1:0 Z0:0:1

              Right...I've revised the M669 as suggested. Homing now functions as it should, with the x axis motor holding torque. Thanks for the suggestion!

              DavidSimcockundefined 1 Reply Last reply Reply Quote 1
              • DavidSimcockundefined
                DavidSimcock @DavidSimcock
                last edited by

                @davidsimcock The issue does seem to be resolved with changing the kinematics M669 command.
                A BIG THANKS to all who have made suggestions to resolve the issue. It is much appreciated.

                T3P3Tonyundefined 1 Reply Last reply Reply Quote 1
                • dc42undefined dc42 marked this topic as a question
                • dc42undefined dc42 has marked this topic as solved
                • T3P3Tonyundefined
                  T3P3Tony administrators @DavidSimcock
                  last edited by

                  @davidsimcock thanks for confirming this. May I ask where the config came from?

                  www.duet3d.com

                  DavidSimcockundefined 1 Reply Last reply Reply Quote 0
                  • DavidSimcockundefined
                    DavidSimcock @T3P3Tony
                    last edited by

                    @t3p3tony I took it from the Ooznest Workbee configuration that I had on a duet 2 wifi, and adapted it for the parameters of my machine. Why there should have been those kinematis commands I don't know. And I confess to not really understanding why there were 4 entry's...

                    T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
                    • T3P3Tonyundefined
                      T3P3Tony administrators @DavidSimcock
                      last edited by

                      @davidsimcock thanks, I will follow up with Ooznest. Thanks agin with your patience as we worked through this.

                      www.duet3d.com

                      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                      • jay_s_ukundefined
                        jay_s_uk @T3P3Tony
                        last edited by

                        @t3p3tony M669 was also a feature of this workbee config https://forum.duet3d.com/topic/27923/x-axis-stops-working-after-moving-y

                        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                        T3P3Tonyundefined 1 Reply Last reply Reply Quote 1
                        • T3P3Tonyundefined
                          T3P3Tony administrators @jay_s_uk
                          last edited by

                          @jay_s_uk thank you for linking these two together I did not see that post.

                          We have captured the issue with M669 to review.

                          www.duet3d.com

                          dc42undefined 1 Reply Last reply Reply Quote 1
                          • dc42undefined
                            dc42 administrators @T3P3Tony
                            last edited by

                            I've added the behaviour when M669 has too many entries per matrix row to the bug list.

                            Duet WiFi hardware designer and firmware engineer
                            Please do not ask me for Duet support via PM or email, use the forum
                            http://www.escher3d.com, https://miscsolutions.wordpress.com

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