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    Duet3 Homing failed

    Scheduled Pinned Locked Moved
    Using Duet Controllers
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    • jay_s_ukundefined
      jay_s_uk @dc42
      last edited by

      @dc42 forgot about that! Good shout

      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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      • Hammadundefined
        Hammad @dc42
        last edited by

        @dc42 Thank you so much. This was actually the Problem.

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        • Hammadundefined
          Hammad @dc42
          last edited by

          @dc42 @Phaedrux I'm still facing the original Problem with the Motors. The Board doesn't home or move the Motors. I reconfigured the RepRap firmware and still nothing. I bought the 1XD Modules to be able to use the motors I mentioned in my reply at the beginning. Can you suggest a solution to this problem?

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @Hammad
            last edited by

            @hammad said in Duet3 Homing failed:

            Can you suggest a solution to this problem?

            I'll ask again:

            Have you been able to get the motors to move at all? You can force the axis to report as homed without moving at all by sending G92 X100 Y100 Z10 and then carefully testing movement by sending G1 X1 F100

            Z-Bot CoreXY Build | Thingiverse Profile

            Hammadundefined 1 Reply Last reply Reply Quote 0
            • Hammadundefined
              Hammad @Phaedrux
              last edited by

              @phaedrux It does home. I can see the coordinates on the Touchscreen. The Motors don't move at all. I tried moving the Motor with an external driver and it worked. Just to make sure that the Motors aren't the issue here.

              deckingmanundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                I am confused by your response. Is homing working or not?

                Can you give a more detailed restatement of the current problem situation?

                Perhaps it would even be a good idea to start a new thread since this one has gone on for quite some time and we've gone through a number of things.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • deckingmanundefined
                  deckingman @Hammad
                  last edited by

                  @hammad Are you saying that the homing status changes from "unhomed" to homed but the motors don't move? If so, then it means that the homing switch is triggered at the start of the move. The usual cause of that is either the configuration does not match the physical NO/NC of the switch, or there is a wiring fault.

                  Ian
                  https://somei3deas.wordpress.com/
                  https://www.youtube.com/@deckingman

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                  • Hammadundefined
                    Hammad @deckingman
                    last edited by

                    @deckingman The Homing status changed to the coordinates I entered with G92 X100 Y100 Z10. The Touchscreen showed X 100 Y 100 and Z 10. When I try to move the motors using the Touchscreen they don't move at all but the coordinates on the screen change. The wiring isn't the issue. I checked everything and it was built to be normally closed as recommended by the documentation. I'm going to start a new thread to make it easier for everyone to follow. I need to get this to work for a big project. I already ordered many boards for the other printers lol. I'll post a link to the new thread in a bit.

                    Hammadundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
                    • Hammadundefined
                      Hammad @Hammad
                      last edited by

                      @dc42 @deckingman @jay_s_uk @Phaedrux this is the link to the new thread.

                      new thread

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                      • Phaedruxundefined
                        Phaedrux Moderator @Hammad
                        last edited by

                        @hammad said in Duet3 Homing failed:

                        @deckingman The Homing status changed to the coordinates I entered with G92 X100 Y100 Z10. The Touchscreen showed X 100 Y 100 and Z 10. When I try to move the motors using the Touchscreen they don't move at all but the coordinates on the screen change. The wiring isn't the issue. I checked everything and it was built to be normally closed as recommended by the documentation. I'm going to start a new thread to make it easier for everyone to follow. I need to get this to work for a big project. I already ordered many boards for the other printers lol. I'll post a link to the new thread in a bit.

                        Thanks, that makes more sense. I'll check your new thread.

                        Z-Bot CoreXY Build | Thingiverse Profile

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