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2 SD Cards - SBC - stop after pause.g 3.5beta2

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Beta Firmware
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  • undefined
    Phaedrux Moderator
    last edited by 14 Apr 2023, 20:57

    Are you able to make it halt consistently with a pause/resume? Next time that happens can you send M122 from the gcode console? Or is DWC completely unresponsive as well?

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 2 Replies Last reply 14 Apr 2023, 20:59 Reply Quote 0
    • undefined
      IndeX4D @Phaedrux
      last edited by 14 Apr 2023, 20:59

      @Phaedrux
      DWC is completely unresponsive.
      Mostly it´s freezing directly, sometimes it´s just slower after resume till next layer/wall.

      I can try it 3 more times.

      this time it stopped with first pause.
      see short video

      1 Reply Last reply Reply Quote 0
      • undefined
        IndeX4D @Phaedrux
        last edited by IndeX4D 14 Apr 2023, 21:00

        @Phaedrux WhatsApp Video 2023-04-14 at 22.59.46 (1).mp4

        May the speed before decides the behaviour. I´ll test it.

        1 Reply Last reply Reply Quote 0
        • undefined
          Phaedrux Moderator
          last edited by 14 Apr 2023, 21:08

          Can you send M122 B# where # is the canbus address of each of your expansion boards and copy and paste the results from each here?

          Z-Bot CoreXY Build | Thingiverse Profile

          undefined 2 Replies Last reply 14 Apr 2023, 21:08 Reply Quote 0
          • undefined
            IndeX4D @Phaedrux
            last edited by IndeX4D 14 Apr 2023, 21:08

            @Phaedrux
            just after restart?
            or do I have to make moves or homing before?

            1 Reply Last reply Reply Quote 0
            • undefined
              Phaedrux Moderator
              last edited by 14 Apr 2023, 21:09

              Any point is fine. I want to see that all the firmware versions are matching.

              Z-Bot CoreXY Build | Thingiverse Profile

              1 Reply Last reply Reply Quote 0
              • undefined
                Phaedrux Moderator
                last edited by 14 Apr 2023, 21:10

                When DWC is unresponsive, is the pi still running?

                Can you follow these steps to gather some logs on the pi?

                https://github.com/Duet3D/DuetSoftwareFramework/wiki/SBC-Setup-Guide#increasing-log-level

                Z-Bot CoreXY Build | Thingiverse Profile

                undefined 1 Reply Last reply 14 Apr 2023, 21:13 Reply Quote 0
                • undefined
                  IndeX4D @Phaedrux
                  last edited by 14 Apr 2023, 21:11

                  M122 B100
                  Diagnostics for board 100:
                  Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-beta.3 (2023-04-13 18:44:05)
                  Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1)
                  All averaging filters OK
                  Never used RAM 5360, free system stack 92 words
                  Tasks: Move(nWait,0.0%,149) HEAT(nWait,0.2%,85) CanAsync(nWait,0.0%,57) CanRecv(nWait,0.0%,76) CanClock(nWait,0.0%,67) ACCEL(nWait,0.0%,53) TMC(delaying,3.0%,57) MAIN(running,91.7%,346) IDLE(ready,0.0%,27) AIN(delaying,4.9%,142), total 100.0%
                  Last reset 00:13:22 ago, cause: software
                  Last software reset data not available
                  Driver 0: pos 0, 400.0 steps/mm,standstill, SG min 0, read errors 1, write errors 1, ifcnt 79, reads 8000, writes 12, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter 6/17, peak Rx sync delay 216, resyncs 0/0, no timer interrupt scheduled
                  VIN voltage: min 24.0, current 24.1, max 24.1
                  MCU temperature: min 40.8C, current 41.2C, max 41.3C
                  Last sensors broadcast 0x00000002 found 1 248 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 16062, send timeouts 0, received 10443, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: LIS3DH, status: 00
                  I2C bus errors 0, naks 3, other errors 0
                  14.4.2023, 23:10:11 M122 B110
                  Diagnostics for board 110:
                  Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-beta.3 (2023-04-13 18:44:05)
                  Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1)
                  All averaging filters OK
                  Never used RAM 5568, free system stack 92 words
                  Tasks: Move(nWait,0.0%,149) HEAT(nWait,0.2%,101) CanAsync(nWait,0.0%,57) CanRecv(nWait,0.0%,76) CanClock(nWait,0.0%,67) ACCEL(nWait,0.0%,53) TMC(nWait,3.0%,57) MAIN(running,91.8%,336) IDLE(ready,0.0%,27) AIN(delaying,4.9%,142), total 100.0%
                  Last reset 00:13:16 ago, cause: software
                  Last software reset at 2022-02-23 14:40, reason: StackOverflow, available RAM 2656, slot 0
                  Software reset code 0x0100 ICSR 0x0000000e SP 0x20007f34 Task HEAT Freestk 4042 ok
                  Stack: 20003fb0 20003fe4 00019d07 00000000 00000000 0000000a 0001a407 00000000 00019511 20003298 fffffffd a5a5a5a5 00000000 00000002 00000000 00000002 0001a1f7 00000000 20002130 200020d4 2000207c 00023368 200020d4 20002130 00000032 200021f8 00013ca5
                  Driver 0: pos 0, 690.0 steps/mm,standstill, SG min 14, read errors 0, write errors 1, ifcnt 80, reads 4925, writes 12, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter 5/16, peak Rx sync delay 213, resyncs 0/0, no timer interrupt scheduled
                  VIN voltage: min 24.2, current 24.2, max 24.3
                  MCU temperature: min 30.3C, current 36.6C, max 37.1C
                  Last sensors broadcast 0x00000004 found 1 97 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 12759, send timeouts 0, received 10354, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: LIS3DH, status: 00
                  I2C bus errors 0, naks 3, other errors 0
                  14.4.2023, 23:10:04 M122 B2
                  Diagnostics for board 2:
                  Duet EXP3HC rev 1.01 or earlier firmware version 3.5.0-beta.3 (2023-04-13 18:42:24)
                  Bootloader ID: not available
                  All averaging filters OK
                  Never used RAM 157816, free system stack 202 words
                  Tasks: Move(nWait,0.0%,162) HEAT(nWait,0.0%,90) CanAsync(nWait,0.0%,63) CanRecv(nWait,0.0%,79) CanClock(nWait,0.0%,70) TMC(nWait,5.8%,105) MAIN(running,92.8%,443) IDLE(ready,0.0%,40) AIN(delaying,1.3%,265), total 100.0%
                  Last reset 00:13:09 ago, cause: software
                  Last software reset data not available
                  Driver 0: pos 0, 80.0 steps/mm,standstill, SG min n/a, mspos 8, reads 63510, writes 11 timeouts 0, steps req 0 done 0
                  Driver 1: pos 0, 80.0 steps/mm,standstill, SG min n/a, mspos 8, reads 63510, writes 11 timeouts 0, steps req 0 done 0
                  Driver 2: pos 0, 80.0 steps/mm,standstill, SG min n/a, mspos 8, reads 63511, writes 11 timeouts 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter 3/22, peak Rx sync delay 183, resyncs 0/0, no timer interrupt scheduled
                  VIN voltage: min 24.0, current 24.0, max 24.0
                  V12 voltage: min 12.2, current 12.2, max 12.2
                  MCU temperature: min 37.2C, current 37.2C, max 37.8C
                  Last sensors broadcast 0x00000000 found 0 106 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 9492, send timeouts 0, received 13406, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  14.4.2023, 23:10:02 M122 B30
                  Diagnostics for board 30:
                  Duet EXP1HCL firmware version 3.5.0-beta.3 (2023-04-14 13:08:48)
                  Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10)
                  All averaging filters OK
                  Never used RAM 53516, free system stack 184 words
                  Tasks: Move(nWait,0.0%,156) HEAT(nWait,0.0%,82) CanAsync(nWait,0.0%,62) CanRecv(nWait,0.0%,77) CanClock(nWait,0.0%,68) TMC(nWait,39.7%,344) CLSend(nWait,0.0%,152) MAIN(running,58.4%,415) IDLE(ready,0.1%,29) AIN(nWait,1.8%,267), total 100.0%
                  Last reset 00:13:07 ago, cause: software
                  Last software reset data not available
                  Closed loop enabled: yes, pre-error threshold: 8.00, error threshold: 4.00, encoder type rotaryQuadrature, position 0
                  Encoder reverse polarity: no, raw count 0
                  Tuning mode: 0, tuning error: 0x1, collecting data: no
                  Control loop runtime (us): min=5, max=32, frequency (Hz): min=10870, max=17045
                  Driver 0: pos 0, 80.0 steps/mm,not tuned/calibrated, SG min n/a, mspos 680, reads 20926, writes 20 timeouts 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter 2/18, peak Rx sync delay 202, resyncs 0/0, next timer interrupt due in 4 ticks, enabled, next step interrupt due in 3704500696 ticks, disabled
                  VIN voltage: min 24.6, current 24.6, max 24.6
                  V12 voltage: min 12.2, current 12.2, max 12.2
                  MCU temperature: min 31.1C, current 31.1C, max 34.1C
                  Last sensors broadcast 0x00000000 found 0 59 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 6327, send timeouts 0, received 13369, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: none
                  I2C bus errors 12, naks 0, other errors 0
                  14.4.2023, 23:10:00 M122 B21
                  Diagnostics for board 21:
                  Duet EXP1HCL firmware version 3.5.0-beta.3 (2023-04-14 13:08:48)
                  Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10)
                  All averaging filters OK
                  Never used RAM 53344, free system stack 184 words
                  Tasks: Move(nWait,0.0%,156) HEAT(nWait,0.0%,82) CanAsync(nWait,0.0%,63) CanRecv(nWait,0.0%,77) CanClock(nWait,0.0%,68) TMC(nWait,39.3%,344) CLSend(nWait,0.0%,152) MAIN(running,58.6%,411) IDLE(ready,0.2%,29) AIN(nWait,1.9%,267), total 100.0%
                  Last reset 00:13:05 ago, cause: software
                  Last software reset data not available
                  Closed loop enabled: yes, pre-error threshold: 8.00, error threshold: 4.00, encoder type rotaryQuadrature, position -1
                  Encoder reverse polarity: no, raw count 65535
                  Tuning mode: 0, tuning error: 0x1, collecting data: no
                  Control loop runtime (us): min=5, max=32, frequency (Hz): min=10870, max=17045
                  Driver 0: pos 0, 80.0 steps/mm,not tuned/calibrated, SG min n/a, mspos 248, reads 55305, writes 20 timeouts 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter -1/16, peak Rx sync delay 201, resyncs 0/0, next timer interrupt due in 23 ticks, enabled, next step interrupt due in 3706150520 ticks, disabled
                  VIN voltage: min 27.3, current 27.3, max 27.3
                  V12 voltage: min 12.1, current 12.1, max 12.1
                  MCU temperature: min 29.4C, current 29.4C, max 31.8C
                  Last sensors broadcast 0x00000000 found 0 145 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 9435, send timeouts 0, received 13331, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: none
                  I2C bus errors 0, naks 0, other errors 0
                  14.4.2023, 23:09:58 M122 B20
                  Diagnostics for board 20:
                  Duet EXP1HCL firmware version 3.5.0-beta.3 (2023-04-14 13:08:48)
                  Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10)
                  All averaging filters OK
                  Never used RAM 53340, free system stack 186 words
                  Tasks: Move(nWait,0.0%,156) HEAT(nWait,0.0%,82) CanAsync(nWait,0.0%,63) CanRecv(nWait,0.0%,77) CanClock(nWait,0.0%,68) TMC(nWait,39.3%,344) CLSend(nWait,0.0%,152) MAIN(running,58.6%,417) IDLE(ready,0.2%,29) AIN(nWait,1.9%,267), total 100.0%
                  Last reset 00:13:02 ago, cause: software
                  Last software reset data not available
                  Closed loop enabled: yes, pre-error threshold: 8.00, error threshold: 4.00, encoder type rotaryQuadrature, position 0
                  Encoder reverse polarity: no, raw count 0
                  Tuning mode: 0, tuning error: 0x1, collecting data: no
                  Control loop runtime (us): min=5, max=32, frequency (Hz): min=10563, max=17045
                  Driver 0: pos 0, 80.0 steps/mm,not tuned/calibrated, SG min n/a, mspos 936, reads 27495, writes 20 timeouts 0, steps req 0 done 0
                  Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
                  Peak sync jitter 0/11, peak Rx sync delay 203, resyncs 0/0, next timer interrupt due in 15 ticks, enabled, next step interrupt due in 3707792031 ticks, disabled
                  VIN voltage: min 24.4, current 24.4, max 24.4
                  V12 voltage: min 12.1, current 12.1, max 12.1
                  MCU temperature: min 31.3C, current 31.3C, max 34.2C
                  Last sensors broadcast 0x00000000 found 0 206 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 9408, send timeouts 0, received 13293, lost 0, free buffers 37, min 37, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: none
                  I2C bus errors 0, naks 0, other errors 0
                  1 Reply Last reply Reply Quote 0
                  • undefined
                    IndeX4D @Phaedrux
                    last edited by IndeX4D 14 Apr 2023, 21:13

                    @Phaedrux ah I did not check the pi then.. I´ll do it
                    Should I do increase log level before?

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      Phaedrux Moderator
                      last edited by 14 Apr 2023, 21:34

                      It would be good to increase the log level and then provoke the error.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      undefined 3 Replies Last reply 14 Apr 2023, 21:35 Reply Quote 0
                      • undefined
                        IndeX4D @Phaedrux
                        last edited by IndeX4D 14 Apr 2023, 21:35

                        This post is deleted!
                        1 Reply Last reply Reply Quote 0
                        • undefined
                          IndeX4D @Phaedrux
                          last edited by 14 Apr 2023, 21:57

                          @Phaedrux

                          Can you please a small advice how I can open DCS to increase the log level?
                          Thanks

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            IndeX4D
                            last edited by 14 Apr 2023, 22:12

                            a94a51d0-ad94-4000-bd5c-ff4a7bbfa818-image.png

                            1 Reply Last reply Reply Quote 0
                            • undefined
                              IndeX4D @Phaedrux
                              last edited by 15 Apr 2023, 00:07

                              This post is deleted!
                              1 Reply Last reply Reply Quote 0
                              • undefined
                                IndeX4D
                                last edited by 15 Apr 2023, 00:26

                                Printer is stucked every pause.
                                and gives the last info see picture
                                b4e4e2bf-3d4e-4b65-b4b4-11b5d22aabcf-image.png

                                Pi still lives.
                                It´s doing this when get stucked.

                                cd53c6d4-beb0-4a5c-b3a6-6c8bf7a4d90e-image.png

                                undefined 1 Reply Last reply 16 Apr 2023, 13:47 Reply Quote 0
                                • undefined
                                  IndeX4D
                                  last edited by 15 Apr 2023, 22:40

                                  is that a normal output?

                                  1 Reply Last reply Reply Quote 0
                                  • undefined
                                    Phaedrux Moderator
                                    last edited by 16 Apr 2023, 04:10

                                    I'm not sure. With using closed loop and beta firmware, we will need to wait and see what @dc42 and @chrishamm have to say.

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    1 Reply Last reply Reply Quote 0
                                    • undefined
                                      chrishamm administrators @IndeX4D
                                      last edited by 16 Apr 2023, 13:47

                                      @IndeX4D Please upgrade to 3.5.0-beta.3, send M122 using the G-code console after it gets stuck, and post the output here. That little excerpt from the debug log isn't really useful, I'll need the full log in case the problem persists with 3.5.0-beta.3 and M122 doesn't show anything significant.

                                      Duet software engineer

                                      undefined 1 Reply Last reply 16 Apr 2023, 14:20 Reply Quote 0
                                      • undefined
                                        IndeX4D @chrishamm
                                        last edited by IndeX4D 16 Apr 2023, 14:20

                                        @chrishamm already is 3.5 beta3 and same behaviour.
                                        How can I give you the full log?

                                        Edit:
                                        When I print with an older dwc version then 3.5 beta1, I don´t have this problem.

                                        undefined 1 Reply Last reply 18 Apr 2023, 00:50 Reply Quote 0
                                        • undefined
                                          IndeX4D
                                          last edited by IndeX4D 17 Apr 2023, 23:55

                                          tell me when you find your bugs.
                                          I won´t investigate anymore.
                                          Sadly...... when I have more time, I would like to help you more, but can't let my printers standing still for such a long time.
                                          thanks

                                          1 Reply Last reply Reply Quote 0
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