3.5.0rc1: Input shaping causes layer shifts!?
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@dc42 I will do teat print with IS disabled and then post results. I modified my config for x and y steppers and changed print external perimeter accel to 2000 because of ringing. Defaul accel is 5k. I’m off my printer right now.
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@dc42 Okay, after a flash with Bossa the printer is up and running again ( @droftarts it turned out to be an outdated IAP file after all, the last version is from November '22 and mine was from June '22), and here is the requested data:
The print file is in the first post of this thread.
The current config.g is this one, it includes the M593 command:
; Konfigurationsdatei für Duet WiFi Firmware 3.5.0rc2 ; Stand: 26.12.2023 G4 P2000 ; 2s warten, daß die Duet in Ruhe starten kann - hilft bei einem Reset?? ; Allgemeine Einstellungen ; M451 ; FDM-Drucker M669 K0 S50 ; Kartesischer Drucker, 20ms Mindest-Segmentzeit von Marlin-Sourcen des J1 übernommen M111 S0 ; Debugging aus G21 ; Basiseinheit Millimeter G90 ; Absolute Koordinaten... M83 ; ... außer beim Extruder M555 P1 ; Firmware-Kompatibilität wie RepRapFirmware M200 D1.75 ; Filamentdurchmesser 1,75mm für alle Extruder (nicht notwendig, aber es schadet nicht) ; globale Variablen ; if !exists(global.Druckplattendicke) global Druckplattendicke = 5.00 ; Dicke der Druckplatte if !exists(global.Z_Limit_min) global Z_Limit_min = 200 ; kleinster zulässiger Max-Wert für Z if !exists(global.Z_Limit_max) global Z_Limit_max = 216 ; größter zulässiger Max-Wert für Z ; PanelDue ; ;M575 P1 S1 B115200 ; IO-Port für PanelDue aktivieren M575 P1 S1 B57600 ; testweise auf 57600 Baud reduziert ; Definition der Sensoren - 2x PT100 mit Vorverstärker am Hotend, 1x 100K-NTC (laut Marlin ein Epcos 100k-Thermistor?) am Bett ; M308 S0 P"temp0" Y"thermistor" A"T_Heizbett" T100000 B4092 ; Sensor 0 = Heizbett-Temperatursensor ; Hotend-Temperatursensoren - Anmerkungen: ; 1. die Vorverstärker im Hotend arbeiten nur im Bereich von 120...310°C linear. Daher weichen die Anzeigewerte insbesondere bei Raumtemperatur ca. 10...15° nach unten ab. ; 2. Originalwerte laut der Sensorkurve von Snapmaker in Marlin: B-121.551 C549.644. Damit ist der Ausgabewert aber bei 190°C mindestens 2°C zu niedrig (außen am Heizblock gemessen) ; Daher Anzeigewert um 5°C nach oben korrigiert auf: M308 S1 P"temp1" Y"linear-analog" A"T_Hotend1" F1 B-116.551 C554.644 ; Sensor 1 = PT100 mit Vorverstärker am Hotend 1 (links). GND und 3,3V kommen vom Filamentsensor, Signal an Pin Temp1 legen! M308 S2 P"temp2" Y"linear-analog" A"T_Hotend2" F1 B-116.551 C554.644 ; Sensor 2 = PT100 mit Vorverstärker am Hotend 1 (links). GND und 3,3V kommen vom Filamentsensor, Signal an Pin Temp2 legen! ; M308 S3 P"temp3" Y"thermistor" A"Bauraum" T100000 B4092 ; reserviert für Sensor 3 = Sensor für Bauraumheizung M308 S10 Y"mcu-temp" A"Elektronik" ; Sensor 10 = Prozessortemperatur der Duet für Elektronikraumkühlung - die Stepper haben nur einen dreistufigen Temperatursensor M308 S11 Y"drivers" A"Steppertreiber" ; Sensor 11 = Steppertreibertemperatur der Duet. 0°C=normal, 100°C=Überhitzungswarnung, 130°C=überhitzt. ; Definition der Anschlüsse ; Führendes "!": Pin wird zum Prozessor hin invertiert, die Firmware macht das automatisch) ; 2-Pin-Lüfter am 4-Pin-Anschluß: einfach nur die beiden Pins V_OUTLCx und OUTx benutzen, den Rest frei lassen ; Lüfter mit VIN (24V) betreiben - Jumper entsprechend setzen ; M950 H0 C"out0" T0 ; Heizelement 0 (Heizbett mit Temperatursensor 0) M950 H1 C"out1" T1 ; Heizelement 1 (Extruder-Heizung mit Temperatursensor 1) M950 H2 C"out2" T2 ; Heizelement 2 (Extruder-Heizung mit Temperatursensor 2) ; H3 (out3) freihalten für Bauraumheizung M950 F0 C"out4" Q50 ; Lüfter 1 (Bauteilkühlung Hotend 1) PWM-Frequenz 50 Hz (sonst schwankt die Drehzhl) M950 F1 C"out5" Q50 ; Lüfter 2 (Bauteilkühlung Hotend 2) PWM-Frequenz 50 Hz (sonst schwankt die Drehzahl) M950 F2 C"out7" Q500 ; Lüfter 3 (Hotendkühlung Hotend 1) M950 F3 C"out8" Q500 ; Lüfter 4 (Hotendkühlung Hotend 2) M950 F4 C"out6" Q50 ; Lüfter 5 (Elektronikraumlüfter) PWM-Frequenz 50 Hz (sonst schwankt die Drehzahl) M950 P9 C"out9" Q100 ; LED-Streifen an Ausgang 9 ; Definition der Antriebe ; falls die Timings manuell justiert werden müssen: Parameter T1:1:0.5:6 F6 = 1us min.step pulse, 1us min.step interval, 0,5us DIR setup time, hold time 6us, Toff=6 ; Originale Daten: ; Normal: TMC StealthChop für alle Achsen an, max. Tempo X200 Y200 mm/s, max. Beschleunigung X8000 Y8000 mm/s² ; Silent: TMC StealthChop für alle Achsen an, max. Tempo X105 Y105 mm/s, max. Beschleunigung X3000 Y3000 mm/s² ; Performance (Laut): TMC StealthChop für X und Y aus, max. Tempo X350 Y350 mm/s, max. Beschleunigung M201 X10000 Y10000 mm/s² ; Steppereinstellungen von Snapmaker am TMC2210 - Achtung: Snapmaker ändert im Idle-Zustand einige der Parameter! ; Stealthchop: für alle Stepper eingeschaltet <-- macht bei den Extrudern null Sinn. ; TPWMTHRS: X und Y: 8, Z: 16, E: Defaultwert (welcher auch immer das sein mag...egal, s.o.) ; Timing: off-time 4 --> F4, hysteresis_end 2, hysteresis_start 1 --> Y1:2 ; ; Defaultwerte der Duet: ccr 0x08053, toff 3, tblank 1, thigh 200 (46.9 mm/sec), tpwmthrs 200 (46.9 mm/sec), pwmScaleSum 26, pwmScaleAuto 0, pwmOfsAuto 39, pwmGradAuto 0, pos 760 ; ; Werte aus der Duet-Hilfe: ; Cnnnn (firmware 2.0 and later, only applies to TMC2660, TMC22xx, TMC2160 and TMC516x stepper drivers) Lowest 17 bits of the chopper control register value. ; Bnn (firmware 2.02RC1 and later) Blanking time (tbl) in the chopper control register, 0 to 3. See the TMC driver datasheet. ; Hnn (firmware 2.02RC2 and later) thigh parameter for those stepper driver chips that support it, e.g. TMC5160 and TMC2160. ; Send M569 P# (where # is the driver number) with no additional parameters to see how this translates into mm/sec. See also the V parameter. ; Yaa:bb or Yaa:bb:cc (firmware 2.02RC2 and later) Hysteresis start, end and decrement values in the chopper control register. See the TMC driver datasheet for the meaning. ; Vnnn (firmware 2.02RC1 and later) tpwmthrs parameter for those stepper driver chips that support it. This is the interval in clock cycles between 1/256 microsteps below ; which the drivers will switch from stealthChop to to spreadCycle mode. Only applies when the driver is configured in stealthChop mode. ; Typical value are from 100 (high speed) to 4000 (low speed). Send M569 P# (where # is the driver number) with no additional parameters to see how this translates into mm/sec. ; Fnn (firmware 2.02 and later) Off-time in the chopper control register, 1 to 15 ; ; Verhältnisse laut TMC-Datenblatt: TCOOLTHRS ≥ TSTEP ≥ TPWMTHRS ≥ THIGH ; Werte für tpwmthrs: V94 = 100mm/s (XYU) bzw. V310 (Z) (sollte der Einstellung von Snapmaker entsprechen?), V25 = 375mm/s und damit für alle Bewegungen gültig ; ; M569 P0.0 S0 D3 H94 V94 ; Test - Defaultwerte. Ergebnis: Motor etwas lauter und mit weniger Drehmoment M569 P0.0 S0 F4 Y1:2 D3 H5 V25 ; Antrieb an DRIVER_0 (X) läuft rückwärts mit StealthChop2, thigh klein (sonst wird CoolStep abgedreht), tpwmhrs auf 375mm/s eingestellt, M915 P0.0 T1 ; ... und tcoolthrs extrem niedrig, so daß CoolStep immer aus ist M569 P0.1 S1 F4 Y1:2 D3 H5 V25 ; Antrieb an DRIVER_1 (U) läuft vorwärts mit StealthChop2, thigh klein (sonst wird CoolStep abgedreht), tpwmhrs auf 375mm/s eingestellt M915 P0.1 T1 ; ... und tcoolthrs extrem niedrig, so daß CoolStep immer aus ist M569 P0.2 S1 D2 ; Antrieb an DRIVER_2 (Z) läuft vorwärts mit Spreadcycle ; M569 P0.3 S0 D2 ; testweise auf Spreadcycle umgestellt. Nutzt nix. M569 P0.3 S0 F4 Y1:2 D3 H5 V25 ; Antrieb an DRIVER_3 (Y) läuft rückwärts mit StealthChop2, thigh klein (sonst wird CoolStep abgedreht), tpwmhrs auf 375mm/s eingestellt M915 P0.3 T1 ; ... und tcoolthrs extrem niedrig, so daß CoolStep immer aus ist M569 P0.4 S0 D2 ; Antrieb an DRIVER_2 (E1) läuft rückwärts mit Spreadcycle M569 P0.5 S1 D2 ; Antrieb an DRIVER_3 (E2) läuft vorwärts mit Spreadcycle ; Definition der Achsen und Extruder ; ACHTUNG beim Einstellen der Steprate und der Interpolation: mehr als 480kHz (max. 650kHz bei nur einem Motor in Betrieb) packt die Duet 3 6HC nicht. Das sollte aber dicke reichen... ; M584 X0.0 U0.1 Y0.3 Z0.2 E0.5:0.4 ; Antriebe zu Achsen zuweisen M350 E64:64 Z16 I0 ; Mikrostepping ohne Interpolation für Z (mit der 2mm-Steigung der Schraube entspricht ein Vollschritt exakt 0,01mm) und E M350 X16 U16 Y16 I1 ; Mikrostepping mit Interpolation für X, U, Y entspricht 0,0125mm pro Mikroschritt M92 X80 U80 Y80 Z1600 E138.58:138.58 S16 ; (Mikro-)Schritte pro mm ; M566 X600 U600 Y600 Z100 E300:300 ; testweise erhöht wg. Layer Shifts. Nutzt nix. M566 X342 U342 Y342 Z100 E300:300 ; Maximale sofortige Geschwindigkeitsänderungen (mm/min). E-Wert aus Marlin, XYUZ-Werte aus Junction Deviation 0,013 errechnet (vgl. https://blog.kyneticcnc.com/2018/10/computing-junction-deviation-for-marlin.html). Für XYU möglichst klein halten (Input Shaping) M203 X21000 U21000 Y21000 Z600 E4800:4800 ; Maximalgeschwindigkeiten (mm/min) M201 X1000 U1000 Y1000 Z500 E5000:5000 ; Maximalbeschleunigungen je Achse (mm/s²) (Z aus J1-Cura-Profil) - Snapmaker-Daten X,U,Y=10000 sind wegen des Werts in M204 völliger Humbug! (Gesamtbeschleunigung max 1000, daher können die XY-Komponenten nicht höher sein) M204 P900 T900 ; höchste erlaubte Gesamtbeschleunigung für Druck und Bewegung (Originalwert Snapmaker: 1000, da fängt aber der Tisch an zu wackeln...) M906 X1000 U1000 Y1400 Z1000 E800:800 I95 ; Motorströme (mA) und Faktor des Ruhestroms in Prozent TODO höhere Ruhestromabsenkung möglich? M84 S30 ; Timeout für Ruhestrom (s) ; M915 X U Y S20 F1 R2 ; Stallguard für X, U und Y TODO Wert festlegen: Snapmaker definiert den Wert als 8 bei einer Bandbreite von 0...255 beim TMC2209; der TMC2160 der Duet hat aber -64...63 ; Beispielwerte für F von X und Y in mm/s: ; F200 --> 100mm in 30s ; F1000 --> 100mm in 6,5s ; F2000 --> 100mm in 3,1s ; F3000 --> 100mm in 2,1s ; Koordinatendefinition ; Nullpunkt = Mittelpunkt des Druckbetts = Zentrum der XY-Korrekturöffnung ; M208 X-175.5 Y-101 Z0 U-151 S1 ; Achsen-Minima M208 X151 Y101 Z209 U175.5 S0 ; Achsen-Maxima - nur grobe Vorgabe für Z, korrekter Wert wird beim Bedleveling ermittelt und in der Datei z_max.g gespeichert ; Definition der I/O-Ports ; Achtung: IO_0 wird vom Flachbandkabel der PanelDue belegt, nicht nutzen! ; ; Endstops M574 X1 S1 P"io1.in" ; X-Endstop: aktiv für Signal auf "High-Level" (NC-Schalter, paßt für die Gabellichtschranke) M574 U2 S1 P"io2.in" ; U-Endstop: aktiv am oberen Ende für Signal auf "High-Level" (NC-Schalter, paßt für die Gabellichtschranke) M574 Y1 S1 P"io3.in" ; Y-Endstop: aktiv für Signal auf "High-Level" (NC-Schalter, paßt für die Gabellichtschranke) M574 Z2 S1 P"io4.in" ; Z-Endstop: aktiv am oberen Ende für Signal auf "High-Level" (NC-Schalter) ; ; Filamentsensoren ; Die Duet unterstützt keine analogen Filamensensoren! Daher müssen die Sensoren des J1 auf digitale Hallsensoren umgebaut oder z.B. ein Arduino als "Übersetzer" verwendet werden ; Werte für Umbau auf Hallsensor mit 2x12 Magneten je Sensor: M591 D0 P7 C"io5.in" L4.2 R50:150 E12.5 S0 ; Filamentsensor für Extruder 0, Impulssignal, an "io5.in", 4mm/Impuls, Toleranz 50...150%, erste 3 Pulse = 12,5mm verwerfen M591 D1 P7 C"io6.in" L4.2 R50:150 E12.5 S0 ; Filamentsensor für Extruder 1, Impulssignal, an "io6.in", 4mm/Impuls, Toleranz 50...150%, erste 3 Pulse = 12,5mm verwerfen ; gemessene Werte: TODO - nach einigen Drucken mit M591 D0 bzw. M591 D1 auslesen und anpassen! ; D0: 3.989mm/pulse, min 95%, max 131% over 143.6mm mit PETG ; 3.985mm/pulse, min 96%, max 130% over 143.6mm mit PETG ; 4.224mm/pulse, min 95%, max 128% over 143.6mm mit PETG ; ; Druckdüsen als Z-Sensoren ; Achtung, diese Werte werden von den drei Kalibriermakros temporär überschrieben! M558 P8 C"^!io7.in" H2 F150 R0.2 T720 K0 B0 ; Z-Sensor Hotend 1=binär ohne Entprellfilter, 2mm Antasthöhe, invertiert (active low)&Pulldownwiderstand aktiv, 300mm/min Meßgeschwindigkeit, 0,5s Recoveryzeit, XY-Bewegung zwischen Messungen 1800mm/min, Heizelemente an G31 K0 P500 X0 Y0 Z{-global.Druckplattendicke-2} ; Z-Sensor Hotend 1: Triggerwert, Offset und Auslösehöhe M558 P8 C"^!io8.in" H2 F150 R0.2 T720 K1 B0 ; Z-Sensor Hotend 2=binär ohne Entprellfilter, 2mm Antasthöhe, invertiert (active low)&Pulldownwiderstand aktiv, 300mm/min Meßgeschwindigkeit, 0,5s Recoveryzeit, XY-Bewegung zwischen Messungen 1800mm/min, Heizelemente an G31 K1 P500 U0 Y0 Z{-global.Druckplattendicke-2} ; Z-Sensor Hotend 2: Triggerwert, Offset und Auslösehöhe ; Hinweis: es darf nur an den Schrauben gemessen werden. Muß in bed.g definiert werden - M557 nicht verwenden! ; Bettleveling ; M671 X0:-114.5:114.5 Y86:-93:-93 S3.0 P0.5 ; Position der Einstellschrauben ; Einstellungen Heizbett (H0) ; auf PID umgestellt, Bang-Bang macht man auch beim Bett nicht mehr, produziert Z-Banding... M140 H0 ; Heizelement 0 initialisieren M307 H0 R0.155 K0.140:0.000 D5.68 E1.35 S1.00 B0 ; Heizelement 0 (Heizbett) Kalibrierungsdaten M143 H0 S110 ; Temperaturlimit für Heizelement 0 (Heizbett) = 110°C ; Einstellungen Heizelemente Hotends (H1 und H2) ; ; M307 H1 R2.186 K0.17:0.11 D5.67 S1.00 V24.0 ; Heizelement 1 (Hotend 1) alte Kalibrierungsdaten aus Marlin umgerechnet M307 H1 R2.461 K0.335:0.144 D6.09 E1.35 S1.00 B0 V23.9 ; Heizelement 1 (Hotend 1) Kalibrierungsdaten, kalibriert mit 250°C und F0.55 M143 H1 S320 ; Temperaturlimit für Heizelement 1 = 320°C M570 H1 P5 T16 ; erlaubte Temperaturabweichung erhöhen, um die bei Raumtemperatur krumme Verstärkerkennlinie abzufangen (sonst Heater Fault) ; M307 H2 R2.186 K0.17:0.11 D5.67 S1.00 V24.0 ; Heizelement 2 (Hotend 2) alte Kalibrierungsdaten aus Marlin umgerechnet M307 H2 R2.476 K0.347:0.131 D5.52 E1.35 S1.00 B0 V23.9 ; ; Heizelement 2 (Hotend 2) Kalibrierungsdaten, kalibriert mit 250°C und F0.55 M143 H2 S320 ; Temperaturlimit für Heizelement 2 = 320°C M570 H2 P5 T16 ; erlaubte Temperaturabweichung erhöhen, um die bei Raumtemperatur krumme Verstärkerkennlinie abzufangen (sonst Heater Fault) M302 P0 S160 R120 ; Limit für Extruderbewegungen: extrudieren nur ab 160°, zurückziehen nur ab 120° ; Einstellungen Lüfter ; M106 P0 S0 H-1 B0.2 L0.17 X1.0 C"Werkzeuglüfter 1" ; Lüfter 0: Startwert 0%, Steuerung via Thermosensor nicht aktiv, Blip-Dauer 0,2s, Geschwindigkeit von 17%-100% M106 P1 S0 H-1 B0.2 L0.17 X1.0 C"Werkzeuglüfter 2" ; Lüfter 1: Startwert 0%, Steuerung via Thermosensor nicht aktiv, Blip-Dauer 0,2s, Geschwindigkeit von 17%-100% M106 P2 S1.0 H1 T45 C"Hotendlüfter 1" ; Lüfter 2: Startwert 100%, Aktiviert, wenn Heizelement 1 > 45°C M106 P3 S1.0 H2 T45 C"Hotendlüfter 2" ; Lüfter 3: Startwert 100%, Aktiviert, wenn Heizelement 2 > 45°C M106 P4 H10:11 T40:60 B0.2 L0.17 X1.0 C"Elektroniklüfter" ; Lüfter 4: Aktiviert, wenn Prozessortemperatur > 40°C, läuft bei 70°C oder wenn Steppertreiber eine Überhitzungswarung ausgibt mit 100%. ; Werkzeuge (Tools) ; M563 S"Hotend 1" P0 D0 H1 F0 ; Werkzeug 0 = Extruder 0 + Heizelement 1 G10 P0 X0 Y0 Z0 ; Achsenoffsets für Werkzeug 0 M568 P0 R0 S0 ; Defaulttemperaturen Werkzeug 0 0°C (=aus) M563 S"Hotend 2" P1 D1 H2 F1 X3 ; Werkzeug 1 = Extruder 1 + Heizelement 2, X auf U gemappt G10 P1 X0 Y0 Z0 ; Achsenoffsets für Werkzeug 1 M568 P1 R0 S0 ; Defaulttemperaturen Werkzeug 1 0°C (=aus) ; M563 S"Duplizieren" P2 D0:1 H1:2 X0:3 ; Werkzeug 2 = beide Extruder, 150mm versetzt ; G10 P2 X75 U-75 Y0 Z0 ; Achsenoffsets für Werkzeug 2 ; M567 P2 E1:1 ; Extrusionsverhältnis für beide Hotends gleich ; M563 S"Spiegeln" P3 D0:1 H1:2 X0:3 ; Werkzeug 3 = Extruder 1 + Heizelement 2, X auf U gemappt und 300mm versetzt. U mit M579 U-1 invertieren, wenn das Tool aktiv ist! Homing anpassen! ; G10 P3 X75 U-75 Y0 Z0 ; Achsenoffsets für Werkzeug 3 ; M567 P3 E1:1 ; Extrusionsverhältnis für beide Hotends gleich ; LEDs ; M42 P9 S0.5 ; LED-Streifen auf 50% ; Geschwindigkeitsverbesserndes Voodoo (Input Shaping, Pressure Advance etc.) ; Empfehlung: erst Input shaping justieren, dann Pressure Advance, dann Retraction! ; ; testweise Input Shaping deaktiviert M593 P"zvddd" F58 D0.1 L0.25 ; Input Shaping bei 58Hz, Dämpfungsfaktor 0,1 - TODO testen, ob ei2 oder zvddd besser ist. Dem Sensor nach sind beide ziemlich gleichauf ; M593 P"ei2" F58 D0.1 L0.03 ; Input Shaping bei 58Hz, Dämpfungsfaktor 0,1 M572 D0:1 S0.05 ; Pressure Advance. Originalwert 0,02 war klar zu niedrig... M309 P0 S0.035 ; Hotend 1 Feedforward-Wert M309 P1 S0.035 ; Hotend 2 Feedforward-Wert ; Retractwerte (M207) siehe Filamente! ; Netzwerk - WLAN-Modul ans Ende setzen wegen Timing-Bug... ; M550 P"Duplimatix" ; Maschinenname M552 I0 S0 ; Ethernetanschluß deaktiviert M586 P0 S1 ; HTTP-Server aktiv M586 P1 S0 ; FTP deaktiviert M586 P2 S0 ; Telnet deaktiviert M552 I1 S1 ; WLAN-Modul aktiv ; Sonstiges ; T0 ; Erstes Werkzeug bei Start ausgewählt M42 P9 S0.25 ; LED-Streifen dimmen M98 P"Korrekturwert_z_max.g" ; korrigiertes Z_Max einlesen M98 P"Korrekturwert_xy_offset_tool1.g" ; XY-Offset Hotend 2 einlesen M207 P0 S1.5 R0 F2400 T2400 ; Default-Retractwerte Hotend 1: 1,5mm und 40mm/s M207 P1 S1.5 R0 F2400 T2400 ; Default-Retractwerte Hotend 2; 1,5mm und 40mm/s M911 S21.5 R23.5 P"M913 X0 U0 Y0 Z1 E0:0 G91 M83 G1 Z1 F1000" ; Bei Spannungsausfall Zustand sichern, dann X, U und Y aus und Z 1mm absenken
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@dc42 [2nd part of message]
And here is the M122 readout, taken about a mm (6..7 layers) after the layer shift occurred:
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5.0-rc.2+ (2024-01-15 11:56:21) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTDL-3SN6L-998UU Used output buffers: 7 of 40 (34 max) === RTOS === Static ram: 155184 Dynamic ram: 123028 of which 0 recycled Never used RAM 64156, free system stack 122 words Tasks: NETWORK(2,nWait 7,15.4%,228) HEAT(3,nWait 1,0.0%,321) Move(4,nWait 6,2.7%,214) CanReceiv(6,nWait 1,0.0%,940) CanSender(5,nWait 7,0.0%,334) CanClock(7,delaying,0.0%,334) TMC(4,nWait 6,9.9%,56) MAIN(1,running,71.5%,103) IDLE(0,ready,0.4%,30), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 01:16:09 ago, cause: software Last software reset at 2024-01-19 23:05, reason: User, Gcodes spinning, available RAM 64316, slot 2 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 MCU temperature: min 45.6, current 47.3, max 47.6 Supply voltage: min 23.6, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.3, max 12.7, under voltage events: 0 Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/1420/1368, gc cycles 13 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, mspos 216, reads 27266, writes 28 timeouts 0 Driver 1: ok, SG min 0, mspos 453, reads 27266, writes 28 timeouts 0 Driver 2: standstill, SG min 0, mspos 984, reads 27271, writes 23 timeouts 0 Driver 3: ok, SG min 0, mspos 794, reads 27268, writes 26 timeouts 0 Driver 4: ok, SG min 0, mspos 306, reads 27275, writes 19 timeouts 0 Driver 5: standstill, SG min 0, mspos 714, reads 27276, writes 19 timeouts 0 Date/time: 2024-01-20 00:21:28 Slowest loop: 212.54ms; fastest: 0.05ms === Storage === Free file entries: 17 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 4.6ms, write time 2.8ms, max retries 0 === Move === DMs created 125, segments created 32, maxWait 119504ms, bed compensation in use: none, height map offset 0.000, max steps late 1, ebfmin -1.00, ebfmax 1.00 next step interrupt due in 326 ticks, disabled Moves shaped first try 21, on retry 2279, too short 16527, wrong shape 66349, maybepossible 10398 === DDARing 0 === Scheduled moves 139469, completed 139424, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.3 Heater 2 is on, I-accum = 0.4 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 3 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 S10" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0, sync state 1 Queue2 is idle in state(s) 0 Q0 segments left 10, axes/extruders owned 0x4000000e Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 50750242 clear 353671 Extruder 0 sensor: ok Extruder 1 sensor: ok === CAN === Messages queued 41120, received 0, lost 0, errs 21703023, boc 0 Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 22850/0/0 Tx timeouts 0,0,22849,0,0,18269 last cancelled message type 30 dest 127 === Network === Slowest loop: 103.88ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(2) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = Interface state: disabled Error counts: 0 0 0 0 0 0 Socket states: 0 0 0 0 0 0 0 0 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1beta6 MAC address 70:04:1d:be:ad:b8 Module reset reason: Power up, Vcc 0.00, flash size 4194304, free heap 221836 WiFi IP address 192.168.178.31 Signal strength -62dBm, channel 2, mode 802.11n, reconnections 0 Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
The layer shift (in y axis direction) occurred at 5.5 or 5.65mm height. It might be worth to point out though that while I got a layer shift of several millimeters with rc1, now it is only some tenths of a millimeter.
Luckily, I sat directly at the printer and watched it while that happened. One thing is worth noting:
I got an audible low-frequency-"bang" from the printer twice around this height and the whole table (which is a solid 40kg wood plate mounted on electric frame) was shaking - something it only does if the y axis does some really hefty acceleration or deceleration. One of these "bangs" created the small layer shift. The printer was printing one of the inner perimeters of the outside surface of the print and did not cross any perimeters or holes in the structure at the time.
Please note no protruding material or such was there that might have blocked the nozzle, and the noise was also quite different from when that happens - such a print error usually creates more of a"rumbling" noise on my printer, with a higher-pitched "klack" or rattling noise if the motor looses one or more steps that it wants to make.
If I would have to conclude what might have created that noise, I would say the Y axis got... well... delayed and had to hurry to catch up, if that does make any sense... -
@NeoDue you need to switch to spreadcycle to avoid the bangs which happens when stealth chop switches modes, change M569 to use D2 rather than D3.
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@oliof Thanks, but a bang that happens only with Input shaping active has nothing to do with StealthChop unless I overlook something serious. Apart from that, I already had this problem and had solved it - take a look at the additional V parameter in my config.g, that switch you mention never happens
I rather fathom if dc42 can find why I have such an amount of CAN errors (without actually using CAN for anything, probably apart from internal Duet communication...?) the problem might vanish.
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@NeoDue if the switch never happens you reduce the attainable torque of your motors. You really want spreadcycle for faster motion.
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@NeoDue said in 3.5.0rc1: Input shaping causes layer shifts!?:
@oliof Thanks, but a bang that happens only with Input shaping active has nothing to do with StealthChop unless I overlook something serious. Apart from that, I already had this problem and had solved it - take a look at the additional V parameter in my config.g, that switch you mention never happens
I think it would be worth running a test to be sure. Do you still get the layer shift if you run the same print with the motors in Spreadcycle? If not that might help us determine what is causing the layer shift. It may be that something in the way the IS pulses are generated is triggering a mode switch.
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@oliof Well, I simply copied the behaviour of the original Snapmaker Marlin board there which probably means they chose the motors accordingly, and I do not have any issues obviously resulting from lacking motor torque. On the contrary - the printer is very well capable of getting the nozzle over significant buildups in the currnet configuration which makes me more fear for the linear bearings
Therefore I do not see any need for Spreadcycle. The only thing that does is making the printer noisy, at least for the speeds I am running at.
But you are right: the basic noise did sound like the "StealthChop -->SpreadCycle-Bang".@gloomyandy I will test that. One more thing: I did a second print over night, and is seems the layer shift does not occur as reliable as it did with rc1. Therefore I will rather focus on whether the "bang" will occur or not since that seems to be an indication of the primary fault which then may cause the shift, okay?
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@gloomyandy I just ran the test with every "M69...D3..." in the above config replaced with an "M569... D2...", and I got a layer shift of about 1,5mm in x direction at 2.8mm height. Here is the M122 message:
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5.0-rc.2+ (2024-01-15 11:56:21) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTDL-3SN6L-998UU Used output buffers: 13 of 40 (33 max) === RTOS === Static ram: 155184 Dynamic ram: 122892 of which 0 recycled Never used RAM 64436, free system stack 134 words Tasks: NETWORK(2,nWait 7,15.8%,172) HEAT(3,nWait 1,0.0%,321) Move(4,nWait 6,2.7%,218) CanReceiv(6,nWait 1,0.0%,940) CanSender(5,nWait 7,0.0%,334) CanClock(7,delaying,0.0%,334) TMC(4,nWait 6,9.8%,56) MAIN(1,running,71.0%,103) IDLE(0,ready,0.6%,30), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 00:35:43 ago, cause: software Last software reset at 2024-01-20 17:07, reason: User, Gcodes spinning, available RAM 65188, slot 0 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x00 Aux0 errors 0,0,0 MCU temperature: min 41.9, current 46.2, max 46.4 Supply voltage: min 23.6, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.3, max 12.6, under voltage events: 0 Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/848/796, gc cycles 6 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, mspos 968, reads 34287, writes 32 timeouts 0 Driver 1: standstill, SG min 0, mspos 232, reads 34287, writes 32 timeouts 0 Driver 2: ok, SG min 0, mspos 344, reads 34296, writes 23 timeouts 0 Driver 3: standstill, SG min 0, mspos 904, reads 34294, writes 26 timeouts 0 Driver 4: standstill, SG min 0, mspos 750, reads 34301, writes 19 timeouts 0 Driver 5: ok, SG min 0, mspos 630, reads 34301, writes 19 timeouts 0 Date/time: 2024-01-20 17:43:20 Slowest loop: 210.67ms; fastest: 0.05ms === Storage === Free file entries: 18 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 4.4ms, write time 2.8ms, max retries 0 === Move === DMs created 125, segments created 26, maxWait 147856ms, bed compensation in use: none, height map offset 0.000, max steps late 1, ebfmin -1.00, ebfmax 1.00 next step interrupt due in 19 ticks, disabled Moves shaped first try 8, on retry 806, too short 4137, wrong shape 32361, maybepossible 2891 === DDARing 0 === Scheduled moves 65368, completed 65308, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.2 Heater 1 is on, I-accum = 0.3 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 3 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0, sync state 1 Queue2 is idle in state(s) 0 Q0 segments left 1, axes/extruders owned 0x80000007 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 23485446 clear 403402 Extruder 0 sensor: ok Extruder 1 sensor: ok === CAN === Messages queued 19281, received 0, lost 0, errs 10170873, boc 0 Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 10717/0/0 Tx timeouts 0,0,10716,0,0,8563 last cancelled message type 30 dest 127 === Network === Slowest loop: 203.98ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = Interface state: disabled Error counts: 0 0 0 0 0 0 Socket states: 0 0 0 0 0 0 0 0 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1beta6 MAC address 70:04:1d:be:ad:b8 Module reset reason: Power up, Vcc 0.00, flash size 4194304, free heap 225180 WiFi IP address 192.168.178.31 Signal strength -63dBm, channel 2, mode 802.11n, reconnections 0 Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
I will let the print run on until it reaches the height where got issues before and add the result to this post.
Edit:
a second layer shift occurred as expected - same height and same direction (y) as in the test above, again with a "bang" (which did however sound more silent as when I use StealthChop.
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5.0-rc.2+ (2024-01-15 11:56:21) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTDL-3SN6L-998UU Used output buffers: 13 of 40 (40 max) === RTOS === Static ram: 155184 Dynamic ram: 122892 of which 0 recycled Never used RAM 64292, free system stack 134 words Tasks: NETWORK(2,nWait 7,15.4%,172) HEAT(3,nWait 1,0.0%,321) Move(4,nWait 6,2.6%,214) CanReceiv(6,nWait 1,0.0%,940) CanSender(5,nWait 7,0.0%,334) CanClock(7,delaying,0.0%,334) TMC(4,nWait 6,10.0%,56) MAIN(1,running,71.7%,103) IDLE(0,ready,0.2%,30), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 01:17:48 ago, cause: software Last software reset at 2024-01-20 17:07, reason: User, Gcodes spinning, available RAM 65188, slot 0 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x04 Aux0 errors 0,0,0 MCU temperature: min 46.1, current 47.2, max 47.5 Supply voltage: min 23.6, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.3, max 12.7, under voltage events: 0 Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/1900/1848, gc cycles 13 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, mspos 200, reads 7160, writes 0 timeouts 0 Driver 1: ok, SG min 0, mspos 248, reads 7160, writes 0 timeouts 0 Driver 2: standstill, SG min 0, mspos 856, reads 7159, writes 0 timeouts 0 Driver 3: ok, SG min 0, mspos 155, reads 7160, writes 0 timeouts 0 Driver 4: ok, SG min 0, mspos 558, reads 7160, writes 0 timeouts 0 Driver 5: standstill, SG min 0, mspos 150, reads 7160, writes 0 timeouts 0 Date/time: 2024-01-20 18:25:25 Slowest loop: 5.71ms; fastest: 0.07ms === Storage === Free file entries: 18 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 4.2ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 32, maxWait 8579ms, bed compensation in use: none, height map offset 0.000, max steps late 1, ebfmin -1.00, ebfmax 1.00 next step interrupt due in 65 ticks, disabled Moves shaped first try 11, on retry 1436, too short 12206, wrong shape 33206, maybepossible 7359 === DDARing 0 === Scheduled moves 137991, completed 137931, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.3 Heater 2 is on, I-accum = 0.4 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is doing "G1 X-14.075 Y-6.155 E.00556" in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0, sync state 1 Queue2 is idle in state(s) 0 Q0 segments left 1, axes/extruders owned 0x4000000e Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 51690012 clear 403402 Extruder 0 sensor: ok Extruder 1 sensor: ok === CAN === Messages queued 22723, received 0, lost 0, errs 11996865, boc 0 Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 12624/0/0 Tx timeouts 0,0,12624,0,0,10099 last cancelled message type 30 dest 127 === Network === Slowest loop: 20.30ms; fastest: 0.07ms Responder states: MQTT(0) HTTP(2) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = Interface state: disabled Error counts: 0 0 0 0 0 0 Socket states: 0 0 0 0 0 0 0 0 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1beta6 MAC address 70:04:1d:be:ad:b8 Module reset reason: Power up, Vcc 0.00, flash size 4194304, free heap 220964 WiFi IP address 192.168.178.31 Signal strength -60dBm, channel 2, mode 802.11n, reconnections 0 Clock register 00002002 Socket states: 5 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
(edit: corrected height of 1st layer shift)
(2nd edit: I just saw that I did two additional smaller layer shifts in Y between the two that are mentioned in this post, so there are four in total) -
@NeoDue Thanks for running that test, I notice that you have a number of custom driver settings using M569 and M915, how did you choose those values?
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@gloomyandy yes, you are right - my X and Y steppers are set with an M569 P0.0 S0 F4 Y1:2 D2 H5 V25.
This means:- F4 = off-time 4 - the Duet default value is F3, the value that was set by Snapmaker was F6. I settled with something in between that worked and "sounded good". According to the TMC data sheet, the value does not play a role in StealthChop anyway.
- Y1:2 Hysteresis start and end values in the chopper control register --> taken from the original Marlin code for the TMC2209 drivers since the datasheets claim those have the same range for both drivers. I admit the code I had to go through was more than chaotic, but I hoped for the best and it... well, worked, that is why I left those values. Again, according to the TMC data sheet, these do not play a role in StealthChop.
- V25 = tpwmthrs: first of all, the TMC steppers do create issues when dynamicly switching from StealthChop over to SpreadCycle, as Oliof correctly pointed out. Since I know that the TMC steppers on the original controller board of my printer use StealthChop all the time, I went to mimick that behaviour and followed the advice from @dc42 given here: https://forum.duet3d.com/topic/22436/missing-steps-cant-print-spreadcycle-stealthchop-tuning-help/131 --> in order to not switch over to Spreadcycle, I set V25 which translates to 375mm/s - which then is high enough never to leave StealthChop mode.
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@NeoDue @oliof I'm a little surprised that using spreadcycle made the problem worse. Usually as mentioned above spreadcycle is a more "powerful" mode and tends to have less issues with lost steps.
I wonder if any of the custom settings you have (that would then have been enabled) could have come into play?
It looks like you have enabled CoolStep with M915 T1. My understanding of how that works is that with the settings you have the motor current could be reduced to 50% of the selected value if the motor loading during the previous moves is low. I wonder if that might be causing problems with your print?
@NeoDue If you can face another test print it may be worth using the default RRF spreadcycle settings with no special timing and no coolstep options?
Just to explain why I'm asking about all of this... There have been very few reports of this problem from others, this may mean that there is something in your configuration that makes the problem more likely to show up.
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@gloomyandy Yes, I understand As noted above, I had tried that for the Y axis alone with RC1 (did not help back then), but I will retry right now.
From my understanding, M915 T1 effectively turns off Coolstep, that is the reason for these lines.
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@NeoDue From my reading of the code and of the TMC 5160 datasheet a value of 1 will be setting the lowest bit of the COOLCONF register which will set the SEMIN value to 1. The datasheet says:
If the StallGuard2 result falls below SEMIN*32, the motor current becomes increased to reduce motor load angle. %0000: smart current control CoolStep off %0001 … %1111: 1 … 15
So a value of 0 will disable CoolStep but 1 will have it enabled. The RRF default is to set the COOLCONF register to 0.
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@gloomyandy That went fast - tested with the following stepper settings:
M569 P0.0 S0 D2 ; testweise auf Spreadcycle umgestellt. M569 P0.1 S1 D2 ; testweise auf Spreadcycle umgestellt. M569 P0.2 S1 D2 ; Antrieb an DRIVER_2 (Z) läuft vorwärts mit Spreadcycle M569 P0.3 S0 D2 ; testweise auf Spreadcycle umgestellt. M569 P0.4 S0 D2 ; Antrieb an DRIVER_2 (E1) läuft rückwärts mit Spreadcycle M569 P0.5 S1 D2 ; Antrieb an DRIVER_3 (E2) läuft vorwärts mit Spreadcycle
Got the same layer shift in x direction again, this time a little earlier at 2.2mm and aborted the test...
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5.0-rc.2+ (2024-01-15 11:56:21) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTDL-3SN6L-998UU Used output buffers: 11 of 40 (40 max) === RTOS === Static ram: 155184 Dynamic ram: 122892 of which 0 recycled Never used RAM 64436, free system stack 130 words Tasks: NETWORK(2,nWait 7,15.7%,208) HEAT(3,nWait 1,0.0%,323) Move(4,nWait 6,2.6%,239) CanReceiv(6,nWait 1,0.0%,940) CanSender(5,nWait 7,0.0%,334) CanClock(7,delaying,0.0%,334) TMC(4,nWait 6,9.8%,56) MAIN(1,running,71.3%,103) IDLE(0,ready,0.6%,30), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 00:36:51 ago, cause: software Last software reset at 2024-01-20 20:43, reason: User, Gcodes spinning, available RAM 64292, slot 1 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x04 Aux0 errors 0,0,0 MCU temperature: min 42.4, current 46.6, max 46.7 Supply voltage: min 23.6, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.3, max 12.7, under voltage events: 0 Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/1448/1396, gc cycles 6 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, mspos 200, reads 16312, writes 29 timeouts 0 Driver 1: standstill, SG min 0, mspos 232, reads 16312, writes 29 timeouts 0 Driver 2: standstill, SG min 0, mspos 296, reads 16318, writes 23 timeouts 0 Driver 3: standstill, SG min 0, mspos 792, reads 16319, writes 23 timeouts 0 Driver 4: standstill, SG min 0, mspos 906, reads 16323, writes 19 timeouts 0 Driver 5: standstill, SG min 0, mspos 42, reads 16323, writes 19 timeouts 0 Date/time: 2024-01-20 21:20:11 Slowest loop: 212.34ms; fastest: 0.05ms === Storage === Free file entries: 17 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 4.3ms, write time 2.8ms, max retries 0 === Move === DMs created 125, segments created 26, maxWait 138976ms, bed compensation in use: none, height map offset 0.000, max steps late 1, ebfmin -1.00, ebfmax 1.00 no step interrupt scheduled Moves shaped first try 8, on retry 803, too short 4102, wrong shape 32067, maybepossible 2863 === DDARing 0 === Scheduled moves 64822, completed 64822, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.4 Heater 1 is on, I-accum = 0.4 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 S1" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x8000000f Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 23245648 clear 1679404 Extruder 0 sensor: ok Extruder 1 sensor: ok === CAN === Messages queued 19891, received 0, lost 0, errs 10499544, boc 0 Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 11056/0/0 Tx timeouts 0,0,11055,0,0,8834 last cancelled message type 30 dest 127 === Network === Slowest loop: 106.55ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = Interface state: disabled Error counts: 0 0 0 0 0 0 Socket states: 0 0 0 0 0 0 0 0 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 0, noresp 0 Firmware version 2.1beta6 MAC address 70:04:1d:be:ad:b8 Module reset reason: Power up, Vcc 0.00, flash size 4194304, free heap 225160 WiFi IP address 192.168.178.31 Signal strength -59dBm, channel 2, mode 802.11n, reconnections 0 Clock register 00002002 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
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@NeoDue Interesting, though it is a bit concerning though that this seems to be a different layer shift to what you were seeing with your original settings. Can you try disabling input shaping and see if this "new" layer shift goes away?
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@gloomyandy That test is already running
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@gloomyandy I got the "T1" from somewhere deep inside this forum when we had our last discussion about the topic ( https://forum.duet3d.com/topic/33756/rrf-3-5-0-rc1-shaking-rattling-in-stealthchop ). But thanks, as you put it, it sounds more logical.
Edit: judging from a finger test of the Y motor temperature, the two settings do not seem to make any difference though.
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@gloomyandy Confirmation completed: With Spreadcycle enabled, default M569 and M915 settings otherwise and Input shaping turned off as the only change relative to the previous attempts with Spreadcycle, the first 6mm of the part come out perfectly fine.
I need to slightly correct my first Spreadcycle report though - I did not get two but rather four layer shifts then. I added this to the corresponding post above.
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@NeoDue That's just my take on what the datasheet says, I've not experimented with any of those settings for COOLSTEP.