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    Core XY movement issues

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    Duet Hardware and wiring
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    • JoergS5undefined
      JoergS5 @FxxToo
      last edited by JoergS5

      @fxxtoo That's good news, congratulations! One advantage of all this effort is that you know your printer very well now. Now relax and enjoy printing.

      The finding is valuable information and will help others in the future.

      And respect, that you had the patience to fight through it!

      FxxTooundefined 1 Reply Last reply Reply Quote 0
      • OBELIKSundefined
        OBELIKS @FxxToo
        last edited by

        @fxxtoo Hm, you get M350 before M92 if you use configurator. So that is also a problem with it.

        P3Steel Toolson mk2 - Duet 2 WiFi --> RatRig V-Core with Duet WiFi 1.03
        Original Prusa i3 MK3S

        FxxTooundefined 1 Reply Last reply Reply Quote 0
        • deckingmanundefined
          deckingman @FxxToo
          last edited by

          @fxxtoo said in Core XY movement issues:

          PROBLEM SOLVED....
          To all that have tried to help me, I want to say thank you to all of you. Turns out that I made a silly mistake in my config.g. dc42 posted , you should put the M92 command before and the firmware will take care of the M350 when it sees it based on your M92 settings. If this can help someone else from making this mistake or helps some one figure out whats wrong, then the past month of frustration will be worth it. Thanks again for the support...and the patience for a noob.

          I made a choice between one of two boards for my printer. I most definitely choose the right one.
          thanks,
          RJ

          Err, well I glad you've solved your problem but something is very amiss. Whether M350 comes before or after M92 should result in the same thing providing the steps per mm match the micro-stepping setting - see here https://duet3d.dozuki.com/Wiki/GCode#Section_M350_Set_microstepping_mode

          Just for the hell of it, I tried both ways on my CoreXY and in both cases I get no Y movement when I ask for an X movement. I'm still on a earlier version of firmware (1.20.1 RC2) so maybe you've found a bug in later firmware???

          Ian
          https://somei3deas.wordpress.com/
          https://www.youtube.com/@deckingman

          JoergS5undefined 2 Replies Last reply Reply Quote 0
          • JoergS5undefined
            JoergS5 @deckingman
            last edited by JoergS5

            This post is deleted!
            1 Reply Last reply Reply Quote 0
            • JoergS5undefined
              JoergS5 @deckingman
              last edited by JoergS5

              @deckingman there is a comment in the cartesian type docu:

              The M92 commands to set steps/mm should either come after any M350 command to set microstepping, or else the M92 parameters should be correct for the default x16 microstepping. This is because when you change microstepping, the steps/mm are automatically adjusted to take account of the change in microstepping.

              https://duet3d.dozuki.com/Wiki/ConfiguringRepRapFirmwareCartesianPrinter

              Maybe the information helps. But the original config setting would be ok after this description.

              deckingmanundefined 1 Reply Last reply Reply Quote 0
              • deckingmanundefined
                deckingman @JoergS5
                last edited by

                @joergs5 Yes I know that. The link you gave has the same information as the link I supplied.

                Ian
                https://somei3deas.wordpress.com/
                https://www.youtube.com/@deckingman

                JoergS5undefined 1 Reply Last reply Reply Quote 0
                • JoergS5undefined
                  JoergS5 @deckingman
                  last edited by

                  @deckingman

                  Independent of this thread, isn't it a problem if the two sides of the X axis are not connected stiff? If the tensions of the belts are not equal, there will be torsion forces in my understanding, which could lead to the 3 mm movements.

                  mrehorstdmdundefined deckingmanundefined 2 Replies Last reply Reply Quote 0
                  • mrehorstdmdundefined
                    mrehorstdmd @JoergS5
                    last edited by

                    @joergs5 Nope. The belts and motors define the motion. As long as the tensions are set to keep the X axis perpendicular to the Y axis, it will operate smoothly and will not cause any extraneous motion.

                    If the x axis guide rail weren't there, the motion would still work as it is supposed to.

                    https://drmrehorst.blogspot.com/

                    JoergS5undefined 1 Reply Last reply Reply Quote 0
                    • JoergS5undefined
                      JoergS5 @mrehorstdmd
                      last edited by JoergS5

                      @mrehorstdmd Thanks a lot, this was new to me! This gives me new innovative ideas to build a new printer!

                      I am thinking about a Corexy with wires, so the hotend needs only the z direction fixed.

                      1 Reply Last reply Reply Quote 0
                      • deckingmanundefined
                        deckingman @JoergS5
                        last edited by

                        @joergs5 As @mrehorstdmd said. If the tensions aren't equal then the axes may not be at right angles and the printed parts might no be square. But commanding 100mm of X movement should not make the Y carriage move.

                        Ian
                        https://somei3deas.wordpress.com/
                        https://www.youtube.com/@deckingman

                        JoergS5undefined 1 Reply Last reply Reply Quote 0
                        • JoergS5undefined
                          JoergS5 @deckingman
                          last edited by JoergS5

                          @deckingman Thanks Ian. To balance tension, I will try a seesaw, e.g. between the motors.
                          (after balancing I will fix it)

                          1 Reply Last reply Reply Quote 0
                          • FxxTooundefined
                            FxxToo @OBELIKS
                            last edited by

                            @obeliks
                            In all honesty, I started out with the config.g file from the configurator. In the beginning I wasn't keeping notes, on changes, problems, etc. I didn't notice the issue right away. I discovered it while getting the homing worked out.
                            So I could have put the M350 before the M92 statement when I started playing with micro stepping. So I would have to go back and use the configurator to find out if that is true or not.
                            RJ

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                            • FxxTooundefined
                              FxxToo @JoergS5
                              last edited by

                              @joergs5 Thanks! If it can help someone else to Not do what I did ans save some frustration..Perfect! rj

                              1 Reply Last reply Reply Quote 0
                              • FxxTooundefined
                                FxxToo
                                last edited by

                                @ everyone
                                I just found a post that might clarify this subject!! Hope this helps clear it up
                                Quoted from dc42
                                Which way round do you have the M350 and M92 commands in config.g?

                                If you have the M92 command before the M350 command, you need to set the steps/mm as they would be for x16 microstepping. When the M350 command is processed, the steps/mm will automatically be adjusted for the new microstepping.

                                If you have the M92 command after the M350 command, then the values need to be correct for the microstepping you declare in M350.
                                link to it
                                https://forum.duet3d.com/topic/2396/calibration/7

                                JoergS5undefined 1 Reply Last reply Reply Quote 0
                                • JoergS5undefined
                                  JoergS5 @FxxToo
                                  last edited by

                                  @fxxtoo I don't understand why order is a problem, because 0 movement of the second stepper is 0, no matter how the microstepping setting is, whether correct or not.

                                  I looked into the source, there are many variables like if it's a smart driver, if there is an additional extruder (bugfix), or whether one motor is stalled (homing).

                                  deckingmanundefined FxxTooundefined 2 Replies Last reply Reply Quote 0
                                  • deckingmanundefined
                                    deckingman @JoergS5
                                    last edited by

                                    @joergs5 said in Core XY movement issues:

                                    @fxxtoo I don't understand why order is a problem, because 0 movement of the second stepper is 0, no matter how the microstepping setting is, whether correct or not.
                                    .................

                                    Exactly! That's why I said something is seriously amiss. The "fix" doesn't make sense (even though it appears to have cured the OP's problem).

                                    Ian
                                    https://somei3deas.wordpress.com/
                                    https://www.youtube.com/@deckingman

                                    FxxTooundefined 1 Reply Last reply Reply Quote 0
                                    • FxxTooundefined
                                      FxxToo @JoergS5
                                      last edited by

                                      @joergs5
                                      II haven't looked at the source code, so can't comment on that. I think that the M350 uses the info from the M92 statement as the start of the calcs for the micro stepping. If a M92 comes after the M350 it might not clear something or miss something that the m350 set. Might be a question for dc42 or Tony. -RJ

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                                      • FxxTooundefined
                                        FxxToo @deckingman
                                        last edited by

                                        @deckingman
                                        Maybe dc42 or Tony can explain this. I just know that my issue went away when I put the M92 for the proper setting for x16 microstepping and then set microstepping with M350, as per the post I read from dc42. Still have a lot to learn about this. -rj

                                        JoergS5undefined 1 Reply Last reply Reply Quote 0
                                        • JoergS5undefined
                                          JoergS5 @FxxToo
                                          last edited by

                                          @fxxtoo maybe your problem reappears when you change to 1/64 stepping, because this was your original setting.

                                          1 Reply Last reply Reply Quote 0
                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Yes I would be interested to see if you can now recreate the problem to verify the fix.

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            FxxTooundefined 1 Reply Last reply Reply Quote 0
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