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    cr-10s upgrade to duet 2 wifi motors and ac 750w bed problems

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    • DocTruckerundefined
      DocTrucker
      last edited by

      Have a general read through the documentation here too:

      https://duet3d.dozuki.com/

      Running 3 P3Steel with Duet 2. Duet 3 on the shelf looking for a suitable machine. One first generation Duet in a Logo/Turtle style robot!

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      • jobesynoob1234undefined
        jobesynoob1234
        last edited by

        please bare with me i believe i have a mix of adhd and autisum 🙂 so i tend to jump ahead of my self and miss steps but also some documentations i have read leave parts out and its thoughs parts that can get me confused 🙂 so im sorry if i stress any of yous out 🙂 and thank you so far i will re do my reprap and will be back

        DocTruckerundefined 1 Reply Last reply Reply Quote 0
        • DocTruckerundefined
          DocTrucker @jobesynoob1234
          last edited by

          @jobesynoob1234 it's easy enough to miss the piece of documentation that has the right information for you when new. My posts were intended to help, but their brief nature probably came over as being snappy. Not intended.

          Running 3 P3Steel with Duet 2. Duet 3 on the shelf looking for a suitable machine. One first generation Duet in a Logo/Turtle style robot!

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          • jobesynoob1234undefined
            jobesynoob1234
            last edited by

            hi again well re-did my reprap and heres the new config.g
            ; Configuration file for Duet WiFi (firmware version 1.21)
            ; executed by the firmware on start-up
            ;
            ; generated by RepRapFirmware Configuration Tool v2 on Mon May 13 2019 10:59:27 GMT+0100 (British Summer Time)

            ; General preferences
            G90 ; Send absolute coordinates...
            M83 ; ...but relative extruder moves

            ; Network
            M550 P"CREALITY CR-10S" ; Set machine name
            M552 S1 ; Enable network
            M586 P0 S1 ; Enable HTTP
            M586 P1 S1 ; Enable FTP
            M586 P2 S0 ; Disable Telnet

            ; Drives
            M569 P0 S0 ; Physical drive 0 goes forwards
            M569 P1 S0 ; Physical drive 1 goes forwards
            M569 P2 S1 ; Physical drive 2 goes forwards
            M569 P3 S1 ; Physical drive 3 goes backwards
            M350 X16 Y16 Z16 E16 I1 ; Configure microstepping with interpolation
            M92 X80.00 Y80.00 Z400.00 E842.00 ; Set steps per mm
            M566 X900.00 Y900.00 Z12.00 E120.00 ; Set maximum instantaneous speed changes (mm/min)
            M203 X18000.00 Y18000.00 Z180.00 E1500.00 ; Set maximum speeds (mm/min)
            M201 X3000.00 Y3000.00 Z100.00 E10000.00 ; Set accelerations (mm/s^2)
            M906 X1000.00 Y1000.00 Z1000.00 E1000.00 I30 ; Set motor currents (mA) and motor idle factor in per cent
            M84 S30 ; Set idle timeout

            ; Axis Limits
            M208 X0 Y0 Z0 S1 ; Set axis minima
            M208 X285 Y285 Z385 S0 ; Set axis maxima

            ; Endstops
            M574 X1 Y1 Z1 S1 ; Set active low and disabled endstops

            ; Z-Probe
            M558 P5 H5 F120 T6000 ; Set Z probe type to switch and the dive height + speeds
            G31 P500 X0 Y0 Z0 ; Set Z probe trigger value, offset and trigger height
            M557 X15:195 Y15:195 S20 ; Define mesh grid

            ; Heaters
            M307 H0 B0 S1.00 ; Disable bang-bang mode for the bed heater and set PWM limit
            M305 P0 T100000 B4138 R4700 ; Set thermistor + ADC parameters for heater 0
            M143 H0 S120 ; Set temperature limit for heater 0 to 120C
            M305 P1 T100000 B4138 R4700 ; Set thermistor + ADC parameters for heater 1
            M143 H1 S285 ; Set temperature limit for heater 1 to 285C

            ; Fans
            M106 P0 S0 I0 F500 H-1 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
            M106 P1 S1 I0 F500 H1 T45 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on

            ; Tools
            M563 P0 D0 H1 ; Define tool 0
            G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
            G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C

            ; Automatic power saving
            M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; Set voltage thresholds and actions to run on power loss

            ; Custom settings are not configured

            all motors home but my z still sounds energized and doesnt back off the endstop switch 😕

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            • Vetiundefined
              Veti
              last edited by

              have a look at you homeall.g

              it explains it

              ; Uncomment the following lines to lift Z after probing
              ;G91 ; relative positioning
              ;G1 S2 Z5 F100 ; lift Z relative to current position
              ;G90 ; absolute positioning

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              • jobesynoob1234undefined
                jobesynoob1234
                last edited by

                like this
                ; Uncomment the following lines to lift Z after probing
                //;G91 ; relative positioning
                //;G1 S2 Z5 F100 ; lift Z relative to current position
                //;G90 ; absolute positioning

                Vetiundefined 1 Reply Last reply Reply Quote 0
                • Vetiundefined
                  Veti @jobesynoob1234
                  last edited by

                  @jobesynoob1234

                  no // is c/java (and other programming languages)

                  uncomment mean removing comments not adding them.

                  so remove the ;

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                  • jobesynoob1234undefined
                    jobesynoob1234
                    last edited by

                    yip thats one of them confusing parts 🙂 with me using marlin
                    i did that and it now lifts but i can still hear power going through it 😕 is that normal

                    dc42undefined 1 Reply Last reply Reply Quote 0
                    • Vetiundefined
                      Veti
                      last edited by

                      see
                      https://duet3d.dozuki.com/Wiki/Reducing_Stand-Still_Noise

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                      • jobesynoob1234undefined
                        jobesynoob1234
                        last edited by

                        Ok i would like to say a massive thank you veti and doctrucker for steering me in the right direction you have saved me a lot of stress 🙂 all motors home heatbed works now i just need to level the bed and try a print 🙂 i still need to look into that "reducing stand still noise" but the important parts are sorted now so im a very happy bunny thank you again for your time

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                        • dc42undefined
                          dc42 administrators @jobesynoob1234
                          last edited by dc42

                          @jobesynoob1234 said in cr-10s upgrade to duet 2 wifi motors and ac 750w bed problems:

                          i did that and it now lifts but i can still hear power going through it is that normal

                          That's not uncommon. The current will be reduced automatically by a specified amount (default is to 30% of normal) after a specified idle time (default is 30 seconds), so it should get quieter after that. You can adjust that 30% and 30 seconds, they are controlled by the M906 command in config.g. If you find the standstill noise loud enough to be annoying, see the link posted by @Veti.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

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                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            The Creality motors seem to have a rather unpleasant whine at low power for some reason. It's not so much loud as it is piercing. 😫

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • jobesynoob1234undefined
                              jobesynoob1234 @dc42
                              last edited by

                              @dc42 hello yip thats what i also did i knocked it down to 10seconds 🙂

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                              • jobesynoob1234undefined
                                jobesynoob1234 @Phaedrux
                                last edited by

                                @phaedrux so will it help if i shove the current up to 1000ma 😕 i did first put them to 750ma!

                                Vetiundefined 1 Reply Last reply Reply Quote 0
                                • Vetiundefined
                                  Veti @jobesynoob1234
                                  last edited by

                                  @jobesynoob1234
                                  changing the current will not change the noise.

                                  jobesynoob1234undefined 1 Reply Last reply Reply Quote 0
                                  • jobesynoob1234undefined
                                    jobesynoob1234 @Veti
                                    last edited by

                                    @veti ah right well they can stay where they are then 🙂

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