endstop trigger and bangbang questions
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@deltajegga Can you include your current config.g?
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its still the same as up top except the last lines are
;M950 J1 C"!^duex.e2stop"
;M581 P1 T0 C0 -
Can you send M115 and verify that you're actually running 3.1.1?
Also, can you send M98 Pconfig.g and report any errors?
Also the content of M122 report please. -
If you are running 3.1.1 your M581 does require an S parameter.
https://duet3d.dozuki.com/Wiki/Gcode#Section_M581_RepRapFirmware_3_01RC2_and_later
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M115
FIRMWARE_NAME: RepRapFirmware for Duet 2 WiFi/Ethernet FIRMWARE_VERSION: 3.1.1 ELECTRONICS: Duet WiFi 1.02 or later + DueX5 FIRMWARE_DATE: 2020-05-19b2no errors on M98 other than my hotend sensor its not installed yet nor is the extruder motor.
M122
=== Diagnostics ===
RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet WiFi 1.02 or later + DueX5
Board ID: 08DLM-996RU-N8PS4-7J1F6-3SD6K-TUAZN
Used output buffers: 3 of 24 (11 max)
=== RTOS ===
Static ram: 27980
Dynamic ram: 94324 of which 96 recycled
Exception stack ram used: 264
Never used ram: 8408
Tasks: NETWORK(ready,368) HEAT(blocked,848) DUEX(suspended,160) MAIN(running,1656) IDLE(ready,80)
Owned mutexes: WiFi(NETWORK)
=== Platform ===
Last reset 00:03:01 ago, cause: power up
Last software reset at 2020-06-20 13:22, reason: User, spinning module GCodes, available RAM 8252 bytes (slot 2)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN
Error status: 0
MCU temperature: min 28.2, current 35.2, max 35.3
Supply voltage: min 23.9, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: standstill, SG min/max not available
Driver 1: standstill, SG min/max not available
Driver 2: standstill, SG min/max not available
Driver 3: standstill, SG min/max not available
Driver 4: standstill, SG min/max not available
Driver 5: standstill, SG min/max not available
Driver 6: standstill, SG min/max not available
Driver 7: standstill, SG min/max not available
Driver 8: standstill, SG min/max not available
Driver 9: standstill, SG min/max not available
Date/time: 2020-06-23 22:07:08
Cache data hit count 316873259
Slowest loop: 11.95ms; fastest: 0.12ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 20.0MBytes/sec
SD card longest read time 3.8ms, write time 6.0ms, max retries 0
=== Move ===
Hiccups: 0(0), FreeDm: 169, MinFreeDm: 169, MaxWait: 0ms
Bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== AuxDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== Heat ===
Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
Daemon is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 22.99ms; fastest: 0.00ms
Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
HTTP sessions: 1 of 8- WiFi -
Network state is active
WiFi module is connected to access point
Failed messages: pending 0, notready 0, noresp 0
WiFi firmware version 1.23
WiFi MAC address bc:dd:c2:2d:67:63
WiFi Vcc 3.42, reset reason Unknown
WiFi flash size 4194304, free heap 19864
WiFi IP address 192.168.1.161
WiFi signal strength -53dBm, reconnections 0, sleep mode modem
Socket states: 0 4 0 0 0 0 0 0
=== DueX ===
Read count 3, 0.99 reads/min
- WiFi -
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i tried
M950 J1 C"!^duex.e2stop"
M581 P1 T0 C0 S1still a no go. heres a picture, the red switch on top goes from white/green to two white wires down to the duex endstop. it has 3 wires for NC or NO, but i assume that doesn't really matter with the inversion capability. if feel like im missing something obvious.
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It's hard to tell from the photo of the wiring bundle but have you followed the Duex wiring guide on connecting the grounds with a short piece of wire as shown here? https://duet3d.dozuki.com/Wiki/Duex2_and_Duex5_Features#Section_Wiring
Can you send
echo sensors.gpIn[1].value
and report the results? -
yes its wired the same.
i get this backError: meta command: array index out of bounds
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@deltajegga said in endstop trigger and bangbang questions:
;M950 J1 C"!^duex.e2stop"
;M581 P1 T0 C0You've uncommented these lines right?
@deltajegga said in endstop trigger and bangbang questions:
i get this back
Error: meta command: array index out of boundsmeans gpIn[1] doesn't exist, so either the M950 J1 command wasn't run or it didn't work
What do you get if you send just M950 J1 in the console?
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hahaha, silly me. i guess it would help if i uncommented them.
ok i get a value of 0 back.and if i send the m950 j1 i get back
Pin !duex.e2stop, active: false -
@deltajegga said in endstop trigger and bangbang questions:
M950 J1 C"!^duex.e2stop"
M581 P1 T0 C0 S1And with this? Does it work as expected?
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no, it still resetes if i home
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I wonder if having the wiring bundled like that is causing the e stop switch pick up the signal from the endstop.
Usually when I'm making my looms I always twist the wires to try and prevent cross talk. Can you physically separate the wiring for the e stop from the bundle and test again?
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ok, interesting. so that solved the triggering when it shouldent problem. (i allways thought that only pwm and data lines cared about twisting.)
but it still wont trigger when i press the button. just a reminder im using a normally open switch.
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@deltajegga said in endstop trigger and bangbang questions:
just a reminder im using a normally open switch.
Try changing it to normally closed. This should be configurable with the S0 S1 switch, but it's worth a shot.
@deltajegga said in endstop trigger and bangbang questions:
(i allways thought that only pwm and data lines cared about twisting.)
I twist or braid everything when using cramped conduits. Just as a matter of habit.
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yeah still nothing.
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And you're sure the switch really works?
Do you have a regular endstop microswitch you can connect in its place to test? -
yeah i tested it with a multimeter at the plug on the duex.
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@deltajegga In RRF 3.1.1, the 'C' parameter has changed to 'R'. See https://duet3d.dozuki.com/Wiki/Gcode#Section_M581_RepRapFirmware_3_01RC2_and_later
Try changing command to
M581 P1 T0 R0 S1
Ian
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damn, got my hopes up. i tried that with !, ^, and !^ on the pin name but still nothing. here is a refresh of the config.
; Configuration file for Duet WiFi (firmware version 3) ; executed by the firmware on start-up ; ; generated by RepRapFirmware Configuration Tool v3.1.1 on Sun May 31 2020 21:54:40 GMT-0700 (Pacific Daylight Time) ; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"1M" ; set printer name ; Network M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet M587 S"MTS" P"Judy1985" ; Drives M569 P0 S0 ; physical drive 0 goes backwards X M569 P1 S0 ; physical drive 1 goes forwards RY M569 P2 S0 ; physical drive 2 goes backwards RZ M569 P3 S0 ; physical drive 3 goes forwards E M569 P5 S1 ; physical drive 5 goes forwards LY M569 P6 S0 ; physical drive 6 goes backwards LZ M584 X0 Y1:5 Z6:2 E3 ; set drive mapping M350 X16 Y16:16 Z16:16 E16 I1 ; configure microstepping with interpolation M92 X114.29 Y114.29:114.29 Z400.00:400.00 E420.00 ; set steps per mm M566 X300.00 Y300:300 Z12:12 E120.00 ; set maximum instantaneous speed changes (mm/min) M203 X4000.00 Y4000:4000 Z500:500 E1200.00 ; set maximum speeds (mm/min) M201 X150.00 Y150:150 Z20:20 E250.00 ; set accelerations (mm/s^2) M906 X800 Y1100:1100 Z600:600 E800 I50 ; set motor currents (mA) and motor idle factor in per cent M84 S90 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis min M208 X1400 Y880 Z900 S0 ; set axis max ; Endstops M574 X1 S1 P"xstop" ; configure active-high endstop for low end on X via pin xstop M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop M574 Z1 S2 ; configure Z-probe endstop for low end on Z ; Z-Probe M950 S0 C"duex.e2heat" ; create servo pin 0 for BLTouch M558 P9 C"zprobe.in+zprobe.mod" H10 F400 T8000 ; set Z probe type to bltouch and the dive height + speeds G31 P25 X28.3 Y0 Z1.3 ; set Z probe trigger value, offset and trigger height INCREASE Z TO MOVE CLOSER TO BED M557 X50:1380 Y50:870 S100 ; define mesh grid ; Heaters M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0 M307 H0 B0 S1.00 A137 D6.4 C1400 ; enable PID mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Fans M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off ; Tools M563 P0 D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Miscellaneous M671 X50:1480 Y400:400 S10 ; x gantry leveling M911 S22 R23 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss T0 ; select first tool M950 J1 C"duex.e2stop" M581 P1 T0 R0 S1 ;emergency stop