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    Need help diagnosing bad stepper output signal on Duet 3

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    • Rushmere3Dundefined
      Rushmere3D @Noah
      last edited by

      @Noah

      If you run M98 P"config.g" again and it gives the same result as before, I think it's because you have multiple factors when you don't need them. If you tell the firmware the Z is 0.2:0.3:0.4 it knows to use one setting for all 3 steppers.

      Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

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      • Phaedruxundefined
        Phaedrux Moderator @Noah
        last edited by

        @Noah said in Need help diagnosing bad stepper output signal on Duet 3:

        M350 X16 Y16 Z16 E16:16:16 I1 to M350 X16 Y16 Z16:16:16 E16 I1

        The Z axis only needs a single entry as well. It's only when you have multiple extruder axis that each axis needs to be defined. The other axis with multiple motors all use the same settings since they aren't independent.

        So remove the multiple Z values as well.

        Z-Bot CoreXY Build | Thingiverse Profile

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        • Phaedruxundefined
          Phaedrux Moderator @Rushmere3D
          last edited by

          @Rushmere3D JYNX again!

          Z-Bot CoreXY Build | Thingiverse Profile

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          • Rushmere3Dundefined
            Rushmere3D @Phaedrux
            last edited by

            @Phaedrux haha

            Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

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            • Noahundefined
              Noah
              last edited by

              ok, haha
              thank you so much for dealing with the noob over here. I corrected all of the lines after m671 to show only one value for X,Y,Z,E
              I was just copying what the RRF config tool gave me for the multiple E motors since it did not have any option to add extra Z motors.
              Z homing and G32 working perfect again, and I only have one data point for motor 5 now
              Fingers crossed.

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Noahundefined
                Noah
                last edited by

                as soon as the hotend heats up and it will let me send extrude and retract commands, I'll let you know if the ext motor is behaving any differently now

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                • Noahundefined
                  Noah
                  last edited by

                  Hahahaha Phaedrux & Rushmere You guy are amazing!!!
                  wish I had asked a little sooner for someone to review my code... I really caused myself a couple of days of grief over here... I have good motor function on all motors now.
                  Now, I am off to tune my extrusion steps and try a print!|

                  Thank You both soooooo much

                  Noah

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                  • Noahundefined
                    Noah
                    last edited by Noah

                    Proper config for others refernce

                    ; Drives
                    M569 P0.0 S1 ; physical drive 0.0 goes forwards
                    M569 P0.1 S1 ; physical drive 0.1 goes forwards
                    M569 P0.2 S1 ; physical drive 0.2 goes forwards
                    M569 P0.3 S1 ; physical drive 0.3 goes forwards
                    M569 P0.4 S1 ; physical drive 0.4 goes forwards
                    M569 P0.5 S1 ; physical drive 0.5 goes forwards
                    M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5
                    M671 X-30.109:146.1:322.309 Y-10.413:317.797:-10.413 S50
                    M350 X16 Y16 Z16 E16 I1
                    M92 X160.00 Y160.00 Z1600.00 E873.00
                    M566 X1200.00 Y1200.00 Z30.00 E1800.00
                    M203 X18000.00 Y18000.00 Z1800.00 E3000.00
                    M201 X1600.00 Y1600.00 Z100.00 E2000.00
                    M906 X1200 Y1200 Z800 E950 I30
                    M84 S30

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                    • Phaedruxundefined
                      Phaedrux Moderator @Noah
                      last edited by

                      Glad you got it sorted.

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • Noahundefined
                        Noah
                        last edited by

                        I still do have the
                        Error: in file macro line 21: M350: array too long, max length = 1

                        but only for the M350 line

                        That's strange... what doesn't it like about my M350 X16 Y16 Z16 E16 I1

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                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Please upload your actual config.g file

                          Z-Bot CoreXY Build | Thingiverse Profile

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