big box madness
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@dc42 ; have taken it from the bigbox forum page as the reprap online configuration was also not working.
and yes used the same wires and all.Configuration file for BigBox 3D printer
; Communication and general
M111 S0 ; Debug off
M550 PBigBox ; Machine name and Netbios name (can be anything you like)
M551 Preprap ; Machine password (used for FTP)
;*** If you have more than one Duet on your network, they must all have different MAC addresses, so change the last digits
M540 P0xBE:0xEF:0xDE:0xAD:0xFE:0xED ; MAC Address
;*** Wifi Networking
M552 S1 ; Enable WiFiM555 P2 ; Set output to look like Marlin
M575 P1 B57600 S1 ; Comms parameters for PanelDue
; Movement section
M569 P0 S1 ; Drive 0 goes forwards (change to S0 to reverse it)
M569 P1 S0 ; Drive 1 goes forwards
M569 P2 S0 ; Drive 2 goes forwards
M569 P3 S1 ; Drive 3 goes forwards
M569 P4 S1 ; Drive 4 goes forwards
M574 X1 Y1 Z1.2 S1 ; set endstop configuration (X and Y endstops only, at low end, active high)
M906 X800 Y600 Z800 E600:600 ; Set motor currents (mA)
M201 X800 Y800 Z15 E1000 ; Accelerations (mm/s^2)
M203 X15000 Y15000 Z100 E3600 ; Maximum speeds (mm/min)
M566 X600 Y600 Z30 E20 ; Minimum speeds mm/minute
M208 X300 Y200 Z200 ; set axis maxima (adjust to suit your machine)
M208 X0 Y0 Z-0.2 S1 ; set axis minimum (adjust to make X=0 and Y=0 the edge of the bed)
M92 X160 Y360 Z1600 ; Set axis steps/mm
M92 E417.5:417.5 ; Set extruder steps per mm
G21 ; Work in millimetres
G90 ; Send absolute coordinates...
M83 ; ...but relative extruder moves
M350 X16 Y16 E16 I1 ; Set 16x microstepping with interpolation; Z probe section
M558 P1 X0 Y0 Z1 H3 F200 T5000 ; Smart IR Z probe, used for homing Z axis, dive height 3mm, probe speed 200mm/min, travel speed 5000mm/min
G31 Z1.4 P500 ; Set the probe height and threshold (put your own values here); Heater and thermistor section
;*** If you have a Duet board with 1K thermistor series resistors, change R4700 to R1000 to the following M305 commands
M305 P0 T100000 B4388 R4700 H30 L0 ; Put your own H and/or L values here to set the bed thermistor ADC correction
M305 P1 X200; B4388 R4700 H30 L0 ; Put your own H and/or L values here to set the first nozzle thermistor ADC correction
M305 P2 X201; H0 L0 ; Put your own H and/or L values here to set the second nozzle thermistor ADC correction
M301 H1 P10 I0.10 D100 T0.50 S1.0 ; PID settings for extruder 0
M301 H2 P10 I0.10 D100 T0.50 S1.0 ; PID settings for extruder 1
M570 S120 ; Increase to allow extra heating time if needed; Fans
M106 P0 F10 ; Fix for Bigbox Blower
M106 P1 T40 H1
M106 P2 T40 H2; Tool definition section
M563 P0 D0 H1 ; Define tool 0 to use extruder drive 0 and heater 1
G10 P0 S0 R0 ; Set tool 0 operating and standby temperatures
;*** If you have a dual-nozzle build, un-comment the following 2 lines
M563 P1 D1 H2 ; Define tool 1
G10 P1 S0 R0 ; Set tool 1 operating and standby temperatures; Bed probe section (not needed if you use a bed.g file)
;*** Adjust the XY coordinates in the following M557 commands to suit your build and the position of your Z probe
M557 P0 X60 Y0 ; Four...
M557 P1 X60 Y165 ; ...probe points...
M557 P2 X200 Y165 ; ...for bed...
M557 P3 X200 Y0 ; ...levelling
;M557 P4 X141 Y82.5 ; 5th probe point for levelling (un-comment this to get a 5th point at the centre of the bed); Epilogue
;*** If you are using axis compensation, put the figures in the following command
M556 S78 X0 Y0 Z0 ; Axis compensation here
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@magdi said in big box madness:
M92 X160 Y360
also are your steps correct for y?
This if from the github marlin config
define DEFAULT_AXIS_STEPS_PER_UNIT {160,180,1600,417.5} // default steps per unit for Titan BigBox -
@veti cheers for the help, have tried to change it still the same error messages
Warning: motor phase A may be disconnected reported by driver(s) 1
Warning: motor phase B may be disconnected reported by driver(s) 1 -
@magdi said in big box madness:
M906 X800 Y600 Z800 E600:600 ; Set motor currents (mA)
I am not familiar with the BigBox, but 600mA for the Y motor current sounds rather low to me. What motors are you using?
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@dc42 have changed to the x axis 800 amount as this works for the X but still no fix
- just upped to 1A still no movment of the Y and Z, X still runs though at 1A
motors are 42BYGHM809 Wantai 1.7A
- just upped to 1A still no movment of the Y and Z, X still runs though at 1A
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@magdi said in big box madness:
Warning: motor phase A may be disconnected reported by driver(s) 1
Warning: motor phase B may be disconnected reported by driver(s) 1Check the cable. if both phases are not connected no wonder that it does not move.
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I suggest you test the motors using G1 S2 moves at low speeds (send G91 first to put axis motion in relative mode).
If you plug the X motor into the Y or Z output, can you get it to move? Power down before connecting or disconnecting motors.
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Right im with you guys. Am now in the process of testing all the wires and getting the stepper sorted will then re-wire and hopefully be sorted.
Cheers for the help will confirm once complete
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@magdi said in big box madness:
M574 X1 Y1 Z1.2 S1 ; set endstop configuration (X and Y endstops only, at low end, active high)
Z1.2? I don't think that's valid.
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Hi @magdi,
Thanks for posting your config.g file and the model of your motor. You want to see it to no more than 1.45A.
That error normally relates to a wire being disconnected or not properly connected. As DC42 suggested try the known working X-Axis wire with either the Y or Z-Axis motor.
If that fails try plugging the known working X-Axis wire AND motor into the Y-Axis or Z-Axis port.
Best Regards
Ryan Lock
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So I've unplugged every wire on the motherboard, tested everything on another motherboard including all the wires for steppers and the steppers that I've been using. They all work there. Now I plug one motor into the duet (currently working with z motors) and nothing happens. Have tried every combination of pin connection and everything ugh.
I'm just pulling my hair out at this point im so confused.What have I done wrong?!
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I already made a suggestion to try to pin down the problem, but you appear to have ignored it.
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@dc42 have tried that i get the same error for connection sorry I didn't reply to it so that's with putting the x axis motor on another axis.
I was just doing what you then later said but I tested all the hardware to see if it worked first
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@ryan-lock thanks for the advice. I have tried moving around the x axis motor to other ports, with and without the same wire. And using that working X wire on other motors. Still the same errors unfortunately. Even got some new wires and the same issue
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Let's start with getting the X motor working when it is connected to the Y motor output. Please add the following command to the start of config.g:
M584 X1 Y0
That will swap the X and Y motor outputs over. Also connect the X motor to the Y motor output, and vice versa. Then try moving X and Y again. If the X motor (connected to the Y motor output) moves correctly when you command X movement, but the Y motor (connected to the X motor output) doesn't, then it is a configuration problem. If the X motor stops working but the Y motor starts working, then it is a problem with the Y driver.
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@dc42 said in big box madness:
M584 X1 Y0
right i have tried what you have advised. problem still persists with the Y driver, driving the x axis.
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Thanks. Please ask your supplier to replace your Duet.
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@dc42 so new board, new problems.
I cant seem to get the end stops to now work.
motors are moving fine but the end stops aren't doing their bit.have a 2 wire endstop so ive wired them on both ends of the endstop. (light starts off as red and then when the stops are engaged turns off) . have tried both X1 Y1 and X0 Y0 and the current code also on my endstop in config.g
M574 X2 Y2 S1 ; Set active high endstops
also i have an E3d hot end and am a bit confused about using the pt1000 amps? ive connected them currently straight to the duet but temps are like 2000c.
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@magdi right i have made stuff do things.
problem now is when i press to 'home y' it homes y a little and also homes x.
so both axis move not just one. But then they also dont move all of the way to homing. hopefully that makes sense.