@jay_s_uk Yep you are very right, have just uploaded the later firmware 3.4.0 and it worked, many thanks for your help.
Best posts made by shaunppl
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RE: When slecting Hotend heater 1 in dashboard error
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Yeah i am trialing the revo hotend with the upgraded smart efficator board (a lot more accurate and less prone to the vibration issues when bed levelling) and using a fixed mounted hemera extruder not the flying spring mounts, seems to be more stable and prints faster.
Latest posts made by shaunppl
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RE: Duet 6HC randomly crasing (again)
@agmeadows have you double checked the power supply feed and or the power supply output, where is the printer situated ?.
power spikes are another source of electrical interference that could be effecting the boards as a fluctuating input or ground can trip the boards to reset. -
RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Yeah i am trialing the revo hotend with the upgraded smart efficator board (a lot more accurate and less prone to the vibration issues when bed levelling) and using a fixed mounted hemera extruder not the flying spring mounts, seems to be more stable and prints faster.
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk How are you getting on with your predator, I revamped mine with a rail conversion along with a meastro board and smart efficator made a hell of a difference.
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Yeah i think so, but now worried as my other prototype are all on the maestro boards and 2 failures means i will have to probably move them all to duet 3 boards.
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Had to upgrade to the Mini 5+ as my maestro board keeps wiping the sd cards ? and making them unreadable.
So took all my settings with it, so scraching head to sort 3 axis homing and other issues etc, talk about having a bad day. lol
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Yep you are very right, have just uploaded the later firmware 3.4.0 and it worked, many thanks for your help.
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Duet web control 3.4.0, FIRMWARE_NAME: RepRapFirmware for Duet 3 Mini 5+ FIRMWARE_VERSION: 3.2.2 ELECTRONICS: Duet 3 Mini5plus Ethernet FIRMWARE_DATE: 2021-02-11
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RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Just found them.
; tpost0.g
; called after tool 0 has been selected
;
; generated by RepRapFirmware Configuration Tool v3.3.10 on Mon May 23 2022 12:52:37 GMT+0100 (British Summer Time)
; Wait for set temperatures to be reached
M116 P0; tpre0.g
; called before tool 0 is selected
;
; generated by RepRapFirmware Configuration Tool v3.3.10 on Mon May 23 2022 12:52:37 GMT+0100 (British Summer Time) -
RE: When slecting Hotend heater 1 in dashboard error
@jay_s_uk Where do i find that ??
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When slecting Hotend heater 1 in dashboard error
When i click on heater 1 in the Dashboard screen to make it active i keep getting the following error and it will not activate the heater??
M568 P0 A1, The M568 command is no longer needed
This appears to be a javascript script ??
2, 11:23:46 M122
=== Diagnostics ===
RepRapFirmware for Duet 3 Mini 5+ version 3.2.2 running on Duet 3 Mini5plus Ethernet (standalone mode)
Board ID: 577A8-6096U-D65J0-40KMD-MH03Z-R8DWU
Used output buffers: 3 of 40 (23 max)
=== RTOS ===
Static ram: 98732
Dynamic ram: 102484 of which 72 recycled
Never used RAM 43928, free system stack 138 words
Tasks: NETWORK(ready,172) ETHERNET(blocked,560) HEAT(blocked,295) CanReceiv(blocked,947) CanSender(blocked,358) CanClock(blocked,362) TMC(blocked,97) MAIN(running,440) IDLE(ready,20) AIN(blocked,260)
Owned mutexes:
=== Platform ===
Last reset 00:34:38 ago, cause: software
Last software reset at 2022-05-24 10:47, reason: User, GCodes spinning, available RAM 44172, slot 0
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
Aux0 errors 0,0,0
Aux1 errors 0,0,0
Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: position 10000, standstill, SG min/max 0/4, read errors 0, write errors 0, ifcnt 32, reads 42406, writes 3, timeouts 0, DMA errors 0
Driver 1: position -6000, standstill, SG min/max 0/4, read errors 0, write errors 0, ifcnt 32, reads 42406, writes 3, timeouts 0, DMA errors 0
Driver 2: position 6000, standstill, SG min/max 0/6, read errors 0, write errors 0, ifcnt 32, reads 42406, writes 3, timeouts 0, DMA errors 0
Driver 3: position 0, standstill, SG min/max 0/0, read errors 0, write errors 0, ifcnt 29, reads 42409, writes 0, timeouts 0, DMA errors 0
Driver 4: position 0, standstill, SG min/max 0/0, read errors 0, write errors 0, ifcnt 29, reads 42409, writes 0, timeouts 0, DMA errors 0
Driver 5: position 0, standstill, SG min/max 0/6, read errors 0, write errors 0, ifcnt 32, reads 42406, writes 3, timeouts 0, DMA errors 0
Driver 6: position 0, standstill, SG min/max 0/6, read errors 0, write errors 0, ifcnt 32, reads 42405, writes 3, timeouts 0, DMA errors 0
Date/time: 2022-05-24 11:22:08
Cache data hit count 3719245232
Slowest loop: 8.65ms; fastest: 0.11ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 22.5MBytes/sec
SD card longest read time 3.7ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 83, maxWait 341151ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 10, completed moves 10, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters = 0 -1, chamberHeaters = -1 -1
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 9.11ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
HTTP sessions: 2 of 8- Ethernet -
State: active
Error counts: 0 0 0 0 0
Socket states: 5 2 2 2 2 0 0 0
=== CAN ===
Messages queued 16659, send timeouts 16658, received 0, lost 0, longest wait 0ms for reply type 0, free buffers 16
24/05/2022, 11:20:32 M568 P0 A1
The M568 command is no longer needed
Congif.g File:
; Configuration file for Duet 3 Mini 5+ (firmware version 3.3)
; executed by the firmware on start-up
;
; generated by RepRapFirmware Configuration Tool v3.3.10 on Mon May 23 2022 12:52:37 GMT+0100 (British Summer Time); General preferences
M575 P1 S1 B57600 ; enable support for PanelDue
G90 ; send absolute coordinates...
M83 ; ...but relative extruder moves
M550 P"Uni3D 001" ; set printer name
M669 K1 ; select CoreXY mode; Network
M552 P0.0.0.0 S1 ; enable network and set IP address
M586 P0 S1 ; enable HTTP
M586 P1 S0 ; disable FTP
M586 P2 S0 ; disable Telnet; Drives
M569 P0.0 S1 ; physical drive 0.0 goes forwards
M569 P0.1 S1 ; physical drive 0.1 goes forwards
M569 P0.2 S0 ; physical drive 0.2 goes backwards
M569 P0.3 S1 ; physical drive 0.3 goes forwards
M569 P0.5 S0 ; physical drive 0.5 goes backwards
M569 P0.6 S0 ; physical drive 0.6 goes backwards
M584 X0.0 Y0.1 Z0.2:0.5:0.6 E0.3 ; set drive mapping
M350 X32 Y32 Z32 E16 I1 ; configure microstepping with interpolation
M92 X400.00 Y400.00 Z800.00 E424.41 ; set steps per mm
M566 X600.00 Y600.00 Z60.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
M203 X1000.00 Y1000.00 Z180.00 E1200.00 ; set maximum speeds (mm/min)
M201 X500.00 Y500.00 Z20.00 E250.00 ; set accelerations (mm/s^2)
M906 X800 Y800 Z800 E800 I30 ; set motor currents (mA) and motor idle factor in per cent
M84 S30 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; set axis minima
M208 X330 Y330 Z600 S0 ; set axis maxima; Endstops
M574 X1 S1 P"io5.in" ; configure switch-type (e.g. microswitch) endstop for low end on X via pin io0.in
M574 Y1 S1 P"io6.in" ; configure switch-type (e.g. microswitch) endstop for low end on Y via pin io2.in
M574 Z1 S2 ; configure Z-probe endstop for low end on Z; Z-Probe
M950 S0 C"io3.out" ; create servo pin 0 for BLTouch
M558 P9 C"io3.in" H5 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
G31 P500 X0 Y40 Z2.5 ; set Z probe trigger value, offset and trigger height
M556 S50 X0 Y0 Z0 ; set orthogonal axis compensation parameters
M557 X15:330 Y15:330 S20 ; define mesh grid; Heaters
M308 S0 P"temp2" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 0 as thermistor on pin temp2
M950 H0 C"out0" T0 ; create bed heater output on out2 and map it to sensor 0
M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
M140 H0 ; map heated bed to heater 0
M143 H0 S120 ; set temperature limit for heater 0 to 120C
M308 S1 P"temp1" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 1 as thermistor on pin temp1
M950 H1 C"out1" T1 ; create nozzle heater output on out1 and map it to sensor 1
M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
M143 H1 S280 ; set temperature limit for heater 1 to 280C; Fans
M950 F0 C"out5" Q500 ; create fan 0 on pin out3 and set its frequency
M106 P0 S0 H1 T45 ; set fan 0 value. Thermostatic control is turned off
M950 F1 C"out3" Q500 ; create fan 1 on pin out4 and set its frequency
M106 P1 S1 H-1 ; set fan 1 value. Thermostatic control is turned on; Tools
M563 P0 D0 H1 F0 ; define tool 0
G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C; Custom settings are not defined
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