scratch last i changed the sensitivity to S2 and it worked but it also jogged the Y axis back slightly is this a belt tension issue? ps thanks for your help and the speedy responses
Posts made by robbrown92
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RE: Sensorless homing corexy not working since upgrade to RR3
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RE: Sensorless homing corexy not working since upgrade to RR3
I changed the code to
M574 X1 S3 ; configure sensorless endstop for low end on X M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop M915 X:Y S5 F1 R0 ; sensorless homing parameters
it still runs into the x end and they pushes the y axis back
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Sensorless homing corexy not working since upgrade to RR3
So i last used my printer with RR 1.2 just updated and renewed the config and everything works apart from the sensorless homing no matter what i set the motor current to or the sensitivity it just plants into the x home and makes loads of noise i have included my complete config and also the testing macro that i am using.
; Configuration file for Duet WiFi (firmware version 3) ; executed by the firmware on start-up ; ; generated by RepRapFirmware Configuration Tool v2.1.8 on Wed Apr 22 2020 22:44:08 GMT+0100 (British Summer Time) ; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"HEVO" ; set printer name M669 K1 ; select CoreXY mode ; Network M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet M552 P192.168.1.103 ; set fixed IP ; Drives M569 P0 S1 ; physical drive 0 goes forwards M569 P1 S1 ; physical drive 1 goes forwards M569 P2 S1 ; physical drive 2 goes forwards M569 P3 S0 ; physical drive 3 goes backwards M584 X0 Y1 Z2 E3 ; set drive mapping M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z4000.00 E420.00 ; set steps per mm M566 X900.00 Y900.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min) M203 X6000.00 Y6000.00 Z180.00 E1200.00 ; set maximum speeds (mm/min) M201 X500.00 Y500.00 Z20.00 E250.00 ; set accelerations (mm/s^2) M906 X800 Y800 Z800 E800 I30 ; set motor currents (mA) and motor idle factor in per cent M84 S30 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X300 Y00 Z200 S0 ; set axis maxima ; Endstops M574 X1 S3 ; configure sensorless endstop for low end on X M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop M915 X S5 F1 R0 ; sensorless homing parameters ; Z-Probe M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch M558 P9 C"^zprobe.in" H5 F100 T2000 ; set Z probe type to bltouch and the dive height + speeds G31 P25 X36 Y10 Z2.5 ; set Z probe trigger value, offset and trigger height M557 X15:215 Y15:195 S20 ; define mesh grid ; Heaters M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H1 S280 ; set temperature limit for heater 1 to 280C M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Fans M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on ; Tools M563 P0 S"E3D V6" D0 H1 F0 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined
M400 ; make sure everything has stopped before we make changes M574 X1 S3 ; set endstops to use motor stall M913 X25 ; reduce motor current to 50% to prevent belts slipping G91 ; use relative positioning G1 H1 X-300 F4000 ; move all carriages up 700mm, stopping at the endstops G90 ; back to absolute positioning M400 ; make sure everything has stopped before we reset the motor currents M913 X100 Y100 Z100 ; motor currents back to normal G1 X0 Y0 F2000 ; centre the head and set a reasonable feed rate M574 X2 Y2 Z2 S1 ; set endstops back to normal so that homedelta.g works
for some reason when i run the macro it moves the Y axis toward the back?
yes i know it makes more sense to use a physical endstop but it worked when i built the printer and havent easily left space to wire in the additional stop
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RE: Heater faults on second layer
@dc42 it’s not that, I have the sock and I’m not printing using a cooling fan
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Heater faults on second layer
Bloody frustrating print starts and runs fine gets to second ish layer and faults
Error: Heating fault on heater 1, temperature excursion exceeded 15.0°C
Resume-after-power-fail state savedthen have to emergency stop the printer to get it to reset.
Watching the temps it prints at 225 then suddenly drops to 180 and fails. im thinking my cartridge thermistor is probably buggered?
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Mesh grid skipping first line
running my meshlevel macro
G90 ; Absolute coordinates
M557 X0:240 Y0:220 S20 ; Bed probe from and to
M401 ; Lower BLTouch probe
G29 S2 ; Clears bed height map in RepRapFirmware
G29 ; Kicks off the Z probing across the height map
M402 ; Retract BLTouch probeReturns this, and skips the first layer of probe points on the Y0
M98 P0:/macros/meshlevel.g
Warning: Skipping grid point (0.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (20.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (40.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (60.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (80.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (100.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (120.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (140.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (160.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (180.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (200.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (220.0, 0.0) because Z probe cannot reach it
Warning: Skipping grid point (240.0, 0.0) because Z probe cannot reach it -
RE: BLTouch was working and now isn't.
@dc42 said in BLTouch was working and now isn't.:
M307 H3 A-1 C-1 D-1
so i changed it to M307 H3 A-1 C-1 D-1 and it seems to work, cant remember why i would have it set differently?
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RE: Problem with Duet Web Control
I use Chrome and mine defaults to http://192.168.0.39/
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RE: BLTouch was working and now isn't.
M307 is there however i had it configured to this
M307 H3 A465.7, C176.6, D3.2 S1 ;
M558 P5 X0 Y0 Z1 H5 F120 T2000
G31 X32 Y10 Z2.9 P25 -
BLTouch was working and now isn't.
So i had a month or so not using my printer, went back on today and tried to reset the bltouch pin using a macro.
M280 P3 S160 I1
it returns;
M98 P0:/macros/Reset BLtouch
Error: Invalid servo index 3 in M280 commandNothing has changed in my config so i have no idea what has gone wrong.
M307 H3
returns
M307 H3
Heater 3 model: gain 340.0, time constant 140.0, dead time 5.5, max PWM 1.00, calibration voltage 0.0, mode PID, inverted no, frequency default
Computed PID parameters for setpoint change: P13.4, I0.482, D51.4
Computed PID parameters for load change: P13.It's a pain as i am keen to get printing again.