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    bltouch

    Scheduled Pinned Locked Moved Unsolved
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    • Phaedruxundefined
      Phaedrux Moderator @nemecek
      last edited by

      @nemecek said in bltouch:

      (i also have a problem with the z axis in home i don't know why it stops before the endstop)

      Are you sure that your steps per mm is 80?

      Z-Bot CoreXY Build | Thingiverse Profile

      nemecekundefined 1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Have you seen these pages?
        https://duet3d.dozuki.com/Wiki/ConfiguringRepRapFirmwareDeltaPrinter
        https://duet3d.dozuki.com/Wiki/Calibrating_a_delta_printer

        Z-Bot CoreXY Build | Thingiverse Profile

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        • nemecekundefined
          nemecek @Phaedrux
          last edited by

          @Phaedrux yes mm is 80 😕

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          • Phaedruxundefined
            Phaedrux Moderator @nemecek
            last edited by

            @nemecek said in bltouch:

            G1 H1 X405 Y405 Z405 F1800 ; move all towers to the high end stopping at the endstops (first pass)

            Try increasing the distance moved for the initial homing to ensure that it goes far enough to hit the endstops.

            That may solve one problem if you're sure 80 steps per mm is correct and it's moving the correct amount.

            Z-Bot CoreXY Build | Thingiverse Profile

            nemecekundefined 1 Reply Last reply Reply Quote 0
            • nemecekundefined
              nemecek @Phaedrux
              last edited by

              @Phaedrux yes I read but I don't know where I went wrong you can help me I'm really desperate

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                I'll do my best, unfortunately I'm not a delta guru. All I can really do is suggest to go through those docs carefully and try and understand what's going on. I can try and answer any specific questions.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • nemecekundefined
                  nemecek
                  last edited by

                  ok
                  thank you🙂

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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    I'm hoping that if we resolve the initial homing the probing will fall into place. If M401 M402 and G30 work correctly to deploy the pin and cause the head to move towards the bed that means the probe itself is working correctly.

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • nemecekundefined
                      nemecek @Phaedrux
                      last edited by

                      @Phaedrux said in bltouch:

                      G1 H1 X405 Y405 Z405 F1800

                      do I write like this? G1 H1 X700 Y700 Z700 F1800

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        That should do it.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • nemecekundefined
                          nemecek
                          last edited by nemecek

                          Sans titre.png

                          gives me this error
                          can I send you a video tomorrow? so you understand me better

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                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            @nemecek said in bltouch:

                            G1 X0 Y0 F6000 ; move X+Y to the centre

                            https://duet3d.dozuki.com/Wiki/Calibrating_a_delta_printer#Section_Homing_the_machine

                            See this section

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • nemecekundefined
                              nemecek @Phaedrux
                              last edited by nemecek

                              @Phaedrux good morning i read in your opinion should i delete it? G1 X0 Y0 F6000 ; move X+Y to the centre

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                              • nemecekundefined
                                nemecek @Phaedrux
                                last edited by

                                @Phaedrux ok perfect I solved the problem of the z axis by deleting this G1 X0 Y0 F6000; move X + Y to the center now and only one bltouch problem you can do
                                😊 😊

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                                • nemecekundefined
                                  nemecek
                                  last edited by

                                  hi I managed to get it working by changing the P9 to the P5 should be P9
                                  peche? can you explain it to me?

                                  M558 P5 H5 F120 T3000

                                  blt.png

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                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    Yes the BLTouch should use P9.

                                    I'm curious now what firmware version you are running. Should be 2.05.1.
                                    Can you please send M122 and post the results?

                                    Z-Bot CoreXY Build | Thingiverse Profile

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                                    • nemecekundefined
                                      nemecek
                                      last edited by

                                      yes

                                      M122
                                      

                                      === Diagnostics ===
                                      RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05.1 running on Duet WiFi 1.02 or later
                                      Board ID: 08DGM-956GU-DJMSN-6J1FL-3SJ6S-T9NVD
                                      Used output buffers: 3 of 24 (9 max)
                                      === RTOS ===
                                      Static ram: 25712
                                      Dynamic ram: 92604 of which 396 recycled
                                      Exception stack ram used: 432
                                      Never used ram: 11928
                                      Tasks: NETWORK(ready,628) HEAT(blocked,1232) MAIN(running,348) IDLE(ready,160)
                                      Owned mutexes:
                                      === Platform ===
                                      Last reset 00:40:29 ago, cause: power up
                                      Last software reset at 2020-06-28 19:10, reason: User, spinning module GCodes, available RAM 11968 bytes (slot 1)
                                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
                                      Error status: 0
                                      Free file entries: 10
                                      SD card 0 detected, interface speed: 20.0MBytes/sec
                                      SD card longest block write time: 6.1ms, max retries 0
                                      MCU temperature: min 29.1, current 40.2, max 40.8
                                      Supply voltage: min 11.9, current 12.1, max 12.2, under voltage events: 0, over voltage events: 0, power good: yes
                                      Driver 0: standstill, SG min/max 0/381
                                      Driver 1: standstill, SG min/max 0/371
                                      Driver 2: standstill, SG min/max 0/377
                                      Driver 3: standstill, SG min/max not available
                                      Driver 4: standstill, SG min/max not available
                                      Date/time: 2020-06-28 20:37:50
                                      Cache data hit count 4294967295
                                      Slowest loop: 49.05ms; fastest: 0.07ms
                                      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                      === Move ===
                                      Hiccups: 0, FreeDm: 160, MinFreeDm: 154, MaxWait: 305348ms
                                      Bed compensation in use: mesh, comp offset 0.000
                                      === DDARing ===
                                      Scheduled moves: 422, completed moves: 422, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                                      === Heat ===
                                      Bed heaters = -1 -1 -1 -1, chamberHeaters = -1 -1
                                      === GCodes ===
                                      Segments left: 0
                                      Stack records: 2 allocated, 0 in use
                                      Movement lock held by null
                                      http is idle in state(s) 0
                                      telnet is idle in state(s) 0
                                      file is idle in state(s) 0
                                      serial is idle in state(s) 0
                                      aux is idle in state(s) 0
                                      daemon is idle in state(s) 0
                                      queue is idle in state(s) 0
                                      autopause is idle in state(s) 0
                                      Code queue is empty.
                                      === Network ===
                                      Slowest loop: 15.44ms; fastest: 0.00ms
                                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                                      HTTP sessions: 1 of 8

                                      • WiFi -
                                        Network state is running
                                        WiFi module is connected to access point
                                        Failed messages: pending 0, notready 0, noresp 0
                                        WiFi firmware version 1.23
                                        WiFi MAC address 5c:cf:7f:76:6a:14
                                        WiFi Vcc 3.34, reset reason Turned on by main processor
                                        WiFi flash size 4194304, free heap 25944
                                        WiFi IP address 192.168.1.35
                                        WiFi signal strength -63dBm, reconnections 0, sleep mode modem
                                        Socket states: 0 0 0 0 0 0 0 0
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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        So what exactly happens when you have it set to P9 and do this test?

                                        https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe#Section_Static_test_using_the_web_interface

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • nemecekundefined
                                          nemecek
                                          last edited by

                                          it goes down without extracting the pin😭

                                          1 Reply Last reply Reply Quote 0
                                          • nemecekundefined
                                            nemecek
                                            last edited by

                                            total panic😬

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