Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Short to ground on drivers 0123

    Scheduled Pinned Locked Moved Unsolved
    Duet Hardware and wiring
    8
    63
    2.7k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • Touchthebitumundefined
      Touchthebitum @A Former User
      last edited by

      @bearer
      No, I'm far from a router

      Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
      BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

      A Former User? 1 Reply Last reply Reply Quote 0
      • A Former User?
        A Former User @Touchthebitum
        last edited by

        @Touchthebitum said in Short to ground on drivers 0123:

        @bearer
        No, I'm far from a router

        you can do all the tests over usb serial interface, or a direct (ethernet) connection to your computer with static ip addresses on both duet and computer when duet is in stand alone mode.

        Touchthebitumundefined 1 Reply Last reply Reply Quote 0
        • Touchthebitumundefined
          Touchthebitum @A Former User
          last edited by

          @bearer
          Ok, what do you need as info or tests ?

          Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
          BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

          A Former User? 1 Reply Last reply Reply Quote 0
          • A Former User?
            A Former User @Touchthebitum
            last edited by

            @Touchthebitum said in Short to ground on drivers 0123:

            what do you need as info or tests ?

            i suspect should repeat all the steps you did diagnosing the old board to see if the error persist when using the Duet as a stand alone board.

            you could also configure your raspberry pi to be a wifi to ethernet bridge , but imho its easier to set a static up for a direct ethernet connection but all three options would work.

            Touchthebitumundefined 1 Reply Last reply Reply Quote 0
            • Touchthebitumundefined
              Touchthebitum @A Former User
              last edited by

              @bearer
              I have a connected laptop to my board but I don't know ho to connect

              Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
              BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

              1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators
                last edited by dc42

                This is perplexing.

                • Are there any other connectors in the leads that connect the motors to the Duet? If so, please post a photo of them.
                • Please post a photo of the stepper motor wires where they go into the motor.
                • Please use your multimeter to check that there is no continuity between any of the motor wires and the body of the motor.
                • Use your multimeter to check that with the connectors fitted, the resistance across each phase is as expected (a few ohms, not a short circuit) and there is no continuity between the two motor phases. Your multimeter probes should be able to fit in the slots in the connector shells in order to make contact with the crimp pins inside.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                • A Former User?
                  A Former User
                  last edited by

                  to set a static IP address on the Duet, you have two options, config.g or USB. Both cases involves M552 S1 P192.168.1.14 as shown in https://duet3d.dozuki.com/Wiki/Gcode#Section_M552_Set_IP_address_enable_disable_network_interface

                  then you need to configure the correct network interface for the computer to use an address in the same network range. probably best to ask google how to do this for your operating system and version/language.

                  if you use the example above for the duet, set the PC to be IP address 192.168.1.15 with netmask 255.255.255.0 and leave the other settings blank or at their defaults.

                  if you have trouble with the computer let us know what operating system/version/language it is and maybe someone can help

                  Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                  • Touchthebitumundefined
                    Touchthebitum @dc42
                    last edited by Touchthebitum

                    @dc42

                    • No, it is direct wire from motor to the board

                    • motor connector.jpg list item

                    • I checked 10x and there is no continuity, resistance is ok

                    • I tested the motors plugged with the multimeter and it is the same result like unplugged

                    • no short between motor case and plugs

                    Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
                    BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

                    dc42undefined 1 Reply Last reply Reply Quote 0
                    • Touchthebitumundefined
                      Touchthebitum @A Former User
                      last edited by

                      @bearer
                      Thanks, I used usb to make tests.

                      First test : psu on, no connected motors, no movements:

                      m122
                      === Diagnostics ===
                      RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (standalone mode)
                      Board ID: 08DJM-956L2-G43S8-6JKD6-3SJ6L-KA02G
                      Used output buffers: 1 of 40 (21 max)
                      === RTOS ===
                      Static ram: 154604
                      Dynamic ram: 162384 of which 44 recycled
                      Exception stack ram used: 308
                      Never used ram: 75876
                      Tasks: ETHERNET(blocked,472) NETWORK(ready,244) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4628) IDLE(ready,76)
                      Owned mutexes:
                      === Platform ===
                      Last reset 00:14:54 ago, cause: power up
                      Last software reset at 2020-08-02 08:21, reason: User, spinning module LinuxInterface, available RAM 75776 bytes (slot 1)
                      Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                      Error status: 0
                      MCU temperature: min 30.0, current 30.7, max 30.7
                      Supply voltage: min 0.2, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                      12V rail voltage: min 0.1, current 12.1, max 12.4, under voltage events: 0
                      Driver 0: standstill, reads 42573, writes 11 timeouts 0, SG min/max 0/0
                      Driver 1: standstill, reads 42573, writes 11 timeouts 0, SG min/max 0/0
                      Driver 2: standstill, reads 42574, writes 11 timeouts 0, SG min/max 0/0
                      Driver 3: standstill, reads 42574, writes 11 timeouts 0, SG min/max 0/0
                      Driver 4: standstill, reads 42575, writes 11 timeouts 0, SG min/max 0/0
                      Driver 5: standstill, reads 42576, writes 11 timeouts 0, SG min/max 0/0
                      Date/time: 2020-08-02 21:35:01
                      Slowest loop: 4.89ms; fastest: 0.16ms
                      === Storage ===
                      Free file entries: 10
                      SD card 0 detected, interface speed: 25.0MBytes/sec
                      SD card longest read time 2.6ms, write time 0.0ms, max retries 0
                      === Move ===
                      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                      Bed compensation in use: none, comp offset 0.000
                      === MainDDARing ===
                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                      === AuxDDARing ===
                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                      === GCodes ===
                      Segments left: 0
                      Movement lock held by null
                      HTTP is idle in state(s) 0
                      Telnet is idle in state(s) 0
                      File is idle in state(s) 0
                      USB is idle in state(s) 0
                      Aux is idle in state(s) 0
                      Trigger is idle in state(s) 0
                      Queue is idle in state(s) 0
                      LCD is idle in state(s) 0
                      SBC is idle in state(s) 0
                      Daemon is idle in state(s) 0
                      Aux2 is idle in state(s) 0
                      Autopause is idle in state(s) 0
                      Code queue is empty.
                      === Network ===
                      Slowest loop: 5.26ms; fastest: 0.03ms
                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                      HTTP sessions: 1 of 8

                      • Ethernet -
                        State: active
                        Error counts: 0 0 0 0 0
                        Socket states: 5 2 2 2 2 0 0 0
                        === CAN ===
                        Messages sent 344, longest wait 0ms for type 0
                        === Linux interface ===
                        State: 0, failed transfers: 0
                        Last transfer: 894436ms ago
                        RX/TX seq numbers: 0/1
                        SPI underruns 0, overruns 0
                        Number of disconnects: 0
                        Buffer RX/TX: 0/0-0

                      Second test : psu on, no connected motors, movement on x through the panel Due:

                      Error: short-to-ground reported by driver(s) 0 1
                      8/2/2020, 9:36:51 PM Error: short-to-ground reported by driver(s) 0 1
                      8/2/2020, 9:36:47 PM m122
                      === Diagnostics ===
                      RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (standalone mode)
                      Board ID: 08DJM-956L2-G43S8-6JKD6-3SJ6L-KA02G
                      Used output buffers: 1 of 40 (22 max)
                      === RTOS ===
                      Static ram: 154604
                      Dynamic ram: 162384 of which 44 recycled
                      Exception stack ram used: 308
                      Never used ram: 75876
                      Tasks: ETHERNET(blocked,436) NETWORK(ready,244) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1424) TMC(blocked,60) MAIN(running,4628) IDLE(ready,76)
                      Owned mutexes:
                      === Platform ===
                      Last reset 00:16:39 ago, cause: power up
                      Last software reset at 2020-08-02 08:21, reason: User, spinning module LinuxInterface, available RAM 75776 bytes (slot 1)
                      Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                      Error status: 0
                      MCU temperature: min 30.6, current 31.9, max 32.0
                      Supply voltage: min 24.1, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                      12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                      Driver 0: short-to-ground standstill, reads 56010, writes 3 timeouts 0, SG min/max 0/8
                      Driver 1: short-to-ground standstill, reads 56009, writes 3 timeouts 0, SG min/max 0/8
                      Driver 2: standstill, reads 56013, writes 0 timeouts 0, SG min/max not available
                      Driver 3: standstill, reads 56012, writes 0 timeouts 0, SG min/max not available
                      Driver 4: standstill, reads 56013, writes 0 timeouts 0, SG min/max not available
                      Driver 5: standstill, reads 56013, writes 0 timeouts 0, SG min/max not available
                      Date/time: 2020-08-02 21:36:46
                      Slowest loop: 17.09ms; fastest: 0.21ms
                      === Storage ===
                      Free file entries: 10
                      SD card 0 detected, interface speed: 25.0MBytes/sec
                      SD card longest read time 2.3ms, write time 12.3ms, max retries 0
                      === Move ===
                      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 373, MaxWait: 984672ms
                      Bed compensation in use: none, comp offset 0.000
                      === MainDDARing ===
                      Scheduled moves: 1, completed moves: 1, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                      === AuxDDARing ===
                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                      === GCodes ===
                      Segments left: 0
                      Movement lock held by null
                      HTTP is idle in state(s) 0
                      Telnet is idle in state(s) 0
                      File is idle in state(s) 0
                      USB is idle in state(s) 0
                      Aux is idle in state(s) 0
                      Trigger is idle in state(s) 0
                      Queue is idle in state(s) 0
                      LCD is idle in state(s) 0
                      SBC is idle in state(s) 0
                      Daemon is idle in state(s) 0
                      Aux2 is idle in state(s) 0
                      Autopause is idle in state(s) 0
                      Code queue is empty.
                      === Network ===
                      Slowest loop: 19.59ms; fastest: 0.03ms
                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                      HTTP sessions: 1 of 8

                      • Ethernet -
                        State: active
                        Error counts: 0 0 0 0 0
                        Socket states: 5 2 2 2 2 0 0 0
                        === CAN ===
                        Messages sent 422, longest wait 0ms for type 0
                        === Linux interface ===
                        State: 0, failed transfers: 0
                        Last transfer: 999813ms ago
                        RX/TX seq numbers: 0/1
                        SPI underruns 0, overruns 0

                      Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
                      BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

                      droftartsundefined 1 Reply Last reply Reply Quote 0
                      • droftartsundefined
                        droftarts administrators @Touchthebitum
                        last edited by droftarts

                        @Touchthebitum rather than using the PanelDue (try with it disconnected in case it’s causing the problem), send Gcode moves via USB. First set a position for the X and Y axis with G92 X0 Y0, then send G1 X10 F300. You will need motors connected to driver 0 and 1, or you’ll get an error.

                        Guide to setting up direct Ethernet connection here: https://duet3d.dozuki.com/Wiki/Setting_up_networking_on_Duet#Section_Wired_direct_connection

                        Edit: when the PanelDue is sending commands, they should be echoed on the USB (I think). If so, what command is being sent to move X?

                        Ian

                        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                        Touchthebitumundefined 2 Replies Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @Touchthebitum
                          last edited by

                          @Touchthebitum, thanks for answering my previous questions. Two more:

                          • what is the stepper motor model number?
                          • what resistance do you measure across each phase?

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                          • Touchthebitumundefined
                            Touchthebitum @dc42
                            last edited by Touchthebitum

                            @dc42

                            Motors are Blurolls 17HM19-2004S

                            I get 1.7 (stabilised) as resistance on every motor on both phase

                            I'll execute tests this morning

                            Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
                            BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

                            1 Reply Last reply Reply Quote 0
                            • Touchthebitumundefined
                              Touchthebitum @droftarts
                              last edited by

                              @droftarts said in Short to ground on drivers 0123:

                              G1 X10 F300

                              No Panel Due Ethernet connection
                              G92 X0 Y0
                              G1 X10 F300

                              Error: short-to-ground reported by driver(s) 0 1
                              03/08/2020 à 15:04:54 m122
                              === Diagnostics ===
                              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (standalone mode)
                              Board ID: 08DJM-956L2-G43S8-6JKD6-3SJ6L-KA02G
                              Used output buffers: 2 of 40 (11 max)
                              === RTOS ===
                              Static ram: 154604
                              Dynamic ram: 162384 of which 44 recycled
                              Exception stack ram used: 272
                              Never used ram: 75912
                              Tasks: ETHERNET(blocked,436) NETWORK(ready,388) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1424) TMC(blocked,204) MAIN(running,4656) IDLE(ready,76)
                              Owned mutexes:
                              === Platform ===
                              Last reset 00:02:33 ago, cause: power up
                              Last software reset at 2020-08-02 08:21, reason: User, spinning module LinuxInterface, available RAM 75776 bytes (slot 1)
                              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                              Error status: 0
                              MCU temperature: min 22.7, current 32.1, max 32.2
                              Supply voltage: min 0.2, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                              12V rail voltage: min 0.1, current 12.1, max 12.4, under voltage events: 0
                              Driver 0: short-to-ground standstill, reads 44551, writes 14 timeouts 0, SG min/max 0/8
                              Driver 1: short-to-ground standstill, reads 44552, writes 14 timeouts 0, SG min/max 0/8
                              Driver 2: standstill, reads 44556, writes 11 timeouts 0, SG min/max 0/0
                              Driver 3: standstill, reads 44557, writes 11 timeouts 0, SG min/max 0/0
                              Driver 4: standstill, reads 44558, writes 11 timeouts 0, SG min/max 0/0
                              Driver 5: standstill, reads 44558, writes 11 timeouts 0, SG min/max 0/0
                              Date/time: 2020-08-03 15:04:53
                              Slowest loop: 29.12ms; fastest: 0.14ms
                              === Storage ===
                              Free file entries: 10
                              SD card 0 detected, interface speed: 25.0MBytes/sec
                              SD card longest read time 2.3ms, write time 23.8ms, max retries 0
                              === Move ===
                              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 373, MaxWait: 134960ms
                              Bed compensation in use: none, comp offset 0.000
                              === MainDDARing ===
                              Scheduled moves: 1, completed moves: 1, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                              === AuxDDARing ===
                              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                              === Heat ===
                              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                              === GCodes ===
                              Segments left: 0
                              Movement lock held by null
                              HTTP is idle in state(s) 0
                              Telnet is idle in state(s) 0
                              File is idle in state(s) 0
                              USB is idle in state(s) 0
                              Aux is idle in state(s) 0
                              Trigger is idle in state(s) 0
                              Queue is idle in state(s) 0
                              LCD is idle in state(s) 0
                              SBC is idle in state(s) 0
                              Daemon is idle in state(s) 0
                              Aux2 is idle in state(s) 0
                              Autopause is idle in state(s) 0
                              Code queue is empty.
                              === Network ===
                              Slowest loop: 28.84ms; fastest: 0.01ms
                              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                              HTTP sessions: 1 of 8

                              • Ethernet -
                                State: active
                                Error counts: 0 0 0 0 0
                                Socket states: 5 2 2 2 2 0 0 0
                                === CAN ===
                                Messages sent 613, longest wait 0ms for type 0
                                === Linux interface ===
                                State: 0, failed transfers: 0
                                Last transfer: 153531ms ago
                                RX/TX seq numbers: 0/1
                                SPI underruns 0, overruns 0
                                Number of disconnects: 0
                                Buffer RX/TX: 0/0-0

                              @droftarts said in Short to ground on drivers 0123:

                              Edit: when the PanelDue is sending commands, they should be echoed on the USB (I think). If so, what command is being sent to move X?

                              I don't see anything regarding echo on the command

                              Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
                              BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

                              1 Reply Last reply Reply Quote 0
                              • Touchthebitumundefined
                                Touchthebitum @droftarts
                                last edited by

                                @droftarts
                                Hello
                                Same results with YAT and USB commands without connected Panel Due. Error short on driver 0 1 ...
                                I don't know what to say anymore....

                                Sparkcube XL V 1.1 300x300x190, Radds, Raspberry, Keenovo silicone bedheat 220v, Big Booster Extruder, DIY building
                                BLV Cube 665mm Direct Drive with Duet3/SBC (RPi 4) Mosquito Magnum/Bond Tech Extruder/Vanadium Nozzle, Keenovo silicone bedheat 220v

                                1 Reply Last reply Reply Quote 0
                                • T3P3Tonyundefined
                                  T3P3Tony administrators
                                  last edited by

                                  @Touchthebitum please email me info@duet3d.com and I will arrange a return directly

                                  www.duet3d.com

                                  1 Reply Last reply Reply Quote 0
                                  • First post
                                    Last post
                                  Unless otherwise noted, all forum content is licensed under CC-BY-SA