Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Multiple Errors Duet3

    Scheduled Pinned Locked Moved Solved
    Firmware installation
    6
    63
    3.6k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • A Former User?
      A Former User @dk
      last edited by A Former User

      @dk said in Multiple Errors Duet3:

      BL-touch on 1LC Tool board

      https://duet3d.dozuki.com/Wiki/Duet_3_firmware_configuration_limitations

      afaik thats not going to work until 3.3 is released, unless the toolboard is also controlling the z motor

      droftartsundefined 1 Reply Last reply Reply Quote 0
      • droftartsundefined
        droftarts administrators @A Former User
        last edited by

        @bearer BLTouch on toolboard works fine for Z homing and bed levelling. Some people are having issues with intermittent comms or power supply, but we’re having difficulty replicating that to troubleshoot.

        Ian

        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

        1 Reply Last reply Reply Quote 0
        • droftartsundefined
          droftarts administrators
          last edited by

          @dk said in Multiple Errors Duet3:

          Now I trying to figure out how to get BL-touch on 1LC Tool board get to work. It can't be done through https://configurator.reprapfirmware.org isn't it?

          For physical connections, see https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board#Section_Connecting_a_BL_Touch

          The configuration tool can produce the code, but doesn't set the CAN address, and I've noticed an error in the input pin drop down. So you'll need to edit config.g afterwards. Setting the following:
          600e1828-8bff-41e9-8722-bbf3cc8bf061-image.png

          and

          684b65cc-4d2f-4270-9492-0ae87ae4c891-image.png

          Produces:

          ; Z-Probe
          M950 S0 C"1.io0.out"                           ; create servo pin 0 for BLTouch
          M558 P9 C"^1.temp1" H5 F120 T6000              ; set Z probe type to bltouch and the dive height + speeds
          G31 P500 X0 Y0 Z2.5                            ; set Z probe trigger value, offset and trigger height
          

          Assuming CAN address is 121, change this to:

          ; Z-Probe
          M950 S0 C"121.io0.out"                           ; create servo pin 0 for BLTouch
          M558 P9 C"^121.io0.in" H5 F120 T6000              ; set Z probe type to bltouch and the dive height + speeds
          G31 P500 X0 Y0 Z2.5                            ; set Z probe trigger value, offset and trigger height
          

          Not sure if you actually need the pull-up resistor ^, but shouldn't hurt. Test and report back!

          Ian

          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

          dc42undefined dkundefined 2 Replies Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators @droftarts
            last edited by

            @droftarts said in Multiple Errors Duet3:

            Not sure if you actually need the pull-up resistor ^, but shouldn't hurt. Test and report back!

            All Duet 3 ioX.in ports have permanent pullup resistors, on the main board and on expansion boards. So you never need to use ^ in the name. We recommend that you do not, because enabling it reduces the noise margin..

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            1 Reply Last reply Reply Quote 0
            • dkundefined
              dk @droftarts
              last edited by

              @droftarts Unfortunately, this didn't help. I tried with and without ^. BL-touch lights up in red but does not extend.
              Can I find somewhere configuration files for any real working Delta printer on Duet3 with Tool board? This would help me a lot in setting up my printer.

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @dk
                last edited by

                @dk Please post your config files so we can see what you have now.

                Z-Bot CoreXY Build | Thingiverse Profile

                dkundefined 1 Reply Last reply Reply Quote 0
                • dkundefined
                  dk @Phaedrux
                  last edited by

                  @Phaedrux

                  Every time after reboot I get Error messages :
                  Error: M950: Response timeout: CAN addr 1, req type 6027, RID=8
                  Error: M106: Fan number 0 not found
                  Error: M950: Response timeout: CAN addr 1, req type 6027, RID=10
                  Error: M106: Fan number 1 not found

                  And when I push Home all only one motor moves.

                  Config.g
                  ; Configuration file for Duet 3 (firmware version 3)
                  ; executed by the firmware on start-up
                  ;
                  ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)

                  ; General preferences
                  G90 ; send absolute coordinates...
                  M83 ; ...but relative extruder moves
                  M550 P"Duet 3" ; set printer name
                  M665 R240 L460 B190 H750 ; Set delta radius, diagonal rod length, printable radius and homed height
                  M666 X0 Y0 Z0 ; put your endstop adjustments here, or let auto calibration find them

                  ; Drives
                  M569 P0.0 S1 ; physical drive 0.0 goes forwards
                  M569 P0.1 S0 ; physical drive 0.1 goes forwards
                  M569 P0.2 S0 ; physical drive 0.2 goes forwards
                  M569 P1.0 S1 ; physical drive 1.0 goes forwards
                  M584 X0.0 Y0.1 Z0.2 E1.0 ; set drive mapping
                  M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                  M92 X160.00 Y160.00 Z160.00 E415.00 ; set steps per mm
                  M566 X1200.00 Y1200.00 Z1200.00 E800.00 ; set maximum instantaneous speed changes (mm/min)
                  M203 X3000.00 Y3000.00 Z3000.00 E600.00 ; set maximum speeds (mm/min)
                  M201 X3000.00 Y3000.00 Z3000.00 E1000.00 ; set accelerations (mm/s^2)
                  M906 X1600 Y1600 Z1600 E900 I30 ; set motor currents (mA) and motor idle factor in per cent
                  M84 S30 ; Set idle timeout

                  ; Axis Limits
                  M208 Z0 S1 ; set minimum Z

                  ; Endstops
                  M574 X2 S1 P"io0.in" ; configure active-high endstop for HIGH end on X via pin io0.in
                  M574 Y2 S1 P"io1.in" ; configure active-high endstop for HIGH end on Y via pin io1.in
                  M574 Z2 S1 P"io2.in" ; configure active-high endstop for HIGH end on Z via pin io2.in

                  ; Z-Probe
                  M950 S0 C"121.io0.out" ; create servo pin 0 for BLTouch
                  M558 P9 C"121.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
                  G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                  M557 R160 S40 ; define mesh grid

                  ; Heaters
                  M308 S0 P"temp3" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp3
                  M950 H0 C"out1" T0 ; create bed heater output on out1 and map it to sensor 0
                  M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
                  M140 H0 ; map heated bed to heater 0
                  M143 H0 S120 ; set temperature limit for heater 0 to 120C
                  M308 S1 P"1.temp0" Y"thermistor" T500000 B4723 C1.19622e-7 ; configure sensor 1 as thermistor on pin 1.temp0
                  M950 H1 C"1.out0" T1 ; create nozzle heater output on 1.out0 and map it to sensor 1
                  M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit

                  ; Fans
                  M950 F0 C"1.out2" Q500 ; create fan 0 on pin 1.out2 and set its frequency
                  M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
                  M950 F1 C"1.out1" Q500 ; create fan 1 on pin 1.out1 and set its frequency
                  M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on

                  ; Tools
                  M563 P0 D0 H1 F0 ; define tool 0
                  G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                  G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

                  ; Custom settings are not defined

                  ; homedelta.g
                  ; called to home all towers on a delta printer
                  ;
                  ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)
                  G91 ; relative positioning
                  G1 H1 X760 Y760 Z760 F1800 ; move all towers to the high end stopping at the endstops (first pass)
                  G1 H2 X-5 Y-5 Z-5 F1800 ; go down a few mm
                  G1 H1 X10 Y10 Z10 F360 ; move all towers up once more (second pass)
                  G1 Z-5 F3600 ; move down a few mm so that the nozzle can be centred
                  G90 ; absolute positioning
                  G1 X0 Y0 F3600 ; move X+Y to the centre

                  ; deployprobe.g
                  ; called to deploy a physical Z probe
                  ;
                  ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)

                  M950 S0 C"121.io0.out"
                  M280 P0 S10 ; deploy BLTouch

                  ; retractprobe.g
                  ; called to retract a physical Z probe
                  ;
                  ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)
                  M950 S0 C"121.io0.out"
                  M280 P0 S90 ; retract BLTouch

                  droftartsundefined 1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Can you send M122 and M98 P"config.g" and post the results?

                    Z-Bot CoreXY Build | Thingiverse Profile

                    dkundefined 1 Reply Last reply Reply Quote 0
                    • droftartsundefined
                      droftarts administrators @dk
                      last edited by

                      @dk you have a Duet 3, and a Toolboard, correct? Did you follow the steps in this guide: https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board
                      Have you changed the CAN address of your Toolboard? And if so, what to? See https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board#Section_Set_the_CAN_address

                      Whatever it’s set to, at the moment you have some commands referring to CAN address 1 (extruder motor, hit end heater, fan etc), and some as CAN address 121, which is the default (BLTouch). Also, it may need a firmware update (further up in the document linked above).

                      Ian

                      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                      dkundefined 1 Reply Last reply Reply Quote 0
                      • dkundefined
                        dk @Phaedrux
                        last edited by

                        @Phaedrux
                        M122
                        === Diagnostics ===
                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                        Board ID: 08DJM-956L2-G43S4-6JTDJ-3SJ6S-986GH
                        Used output buffers: 1 of 40 (21 max)
                        === RTOS ===
                        Static ram: 154604
                        Dynamic ram: 161404 of which 276 recycled
                        Exception stack ram used: 224
                        Never used ram: 76708
                        Tasks: NETWORK(ready,1972) HEAT(blocked,1248) CanReceiv(suspended,3424) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4528) IDLE(ready,76)
                        Owned mutexes:
                        === Platform ===
                        Last reset 00:00:44 ago, cause: power up
                        Last software reset at 2020-09-22 22:34, reason: User, spinning module LinuxInterface, available RAM 76708 bytes (slot 0)
                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                        Error status: 0
                        MCU temperature: min 39.2, current 39.6, max 39.7
                        Supply voltage: min 23.9, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
                        12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0
                        Driver 0: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
                        Driver 1: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
                        Driver 2: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
                        Driver 3: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
                        Driver 4: standstill, reads 24457, writes 0 timeouts 0, SG min/max not available
                        Driver 5: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
                        Date/time: 2020-09-22 22:34:11
                        Slowest loop: 4.22ms; fastest: 0.20ms
                        === Storage ===
                        Free file entries: 10
                        SD card 0 not detected, interface speed: 37.5MBytes/sec
                        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                        === Move ===
                        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                        Bed compensation in use: none, comp offset 0.000
                        === MainDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === AuxDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === Heat ===
                        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                        === GCodes ===
                        Segments left: 0
                        Movement lock held by null
                        HTTP* is ready with "M122" in state(s) 0
                        Telnet is idle in state(s) 0
                        File is idle in state(s) 0
                        USB is idle in state(s) 0
                        Aux is idle in state(s) 0
                        Trigger* is idle in state(s) 0
                        Queue is idle in state(s) 0
                        LCD is idle in state(s) 0
                        SBC is idle in state(s) 0
                        Daemon* is idle in state(s) 0
                        Aux2 is idle in state(s) 0
                        Autopause is idle in state(s) 0
                        Code queue is empty.
                        === Network ===
                        Slowest loop: 0.47ms; fastest: 0.01ms
                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                        HTTP sessions: 0 of 8

                        • Ethernet -
                          State: disabled
                          Error counts: 0 0 0 0 0
                          Socket states: 0 0 0 0 0 0 0 0
                          === CAN ===
                          Messages sent 20, longest wait 0ms for type 0
                          === Linux interface ===
                          State: 0, failed transfers: 3
                          Last transfer: 18ms ago
                          RX/TX seq numbers: 539/540
                          SPI underruns 3, overruns 3
                          Number of disconnects: 0
                          Buffer RX/TX: 0/0-0
                          === Duet Control Server ===
                          Duet Control Server v3.1.1
                          Code buffer space: 4096
                          Configured SPI speed: 8000000 Hz
                          Full transfers per second: 0.02

                        M98 P"config.g"
                        Error: M569: Response timeout: CAN addr 1, req type 6018, RID=12
                        Error: M350: Response timeout: CAN addr 1, req type 6021, RID=13
                        Error: M906: Response timeout: CAN addr 1, req type 6017, RID=14
                        Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
                        Error: M308: Response timeout: CAN addr 1, req type 6011, RID=19
                        Error: M950: Response timeout: CAN addr 1, req type 6026, RID=20
                        Error: M307: Heater 1 not found
                        Error: M950: Response timeout: CAN addr 1, req type 6027, RID=22
                        Error: M106: Fan number 0 not found
                        Error: M950: Response timeout: CAN addr 1, req type 6027, RID=24
                        Error: M106: Fan number 1 not found

                        1 Reply Last reply Reply Quote 0
                        • dkundefined
                          dk @droftarts
                          last edited by

                          @droftarts

                          I have Duet3 and Toolboard with BMG and Mosquito Magnum + BL-touch
                          I have follow all speps frome this guide.
                          I did not changed the CAN address of Toolboard

                          Sending M115 B121 give me :
                          Board TOOL1LC firmware 3.1.0 (2020-05-15b1)

                          droftartsundefined 1 Reply Last reply Reply Quote 0
                          • droftartsundefined
                            droftarts administrators @dk
                            last edited by

                            @dk then you need to go through your config.g and change all references to CAN address 1 to 121, eg

                            M569 P1.0 S1 ; physical drive 1.0 goes forwards

                            Changes to:

                            M569 P121.0 S1 ; physical drive 121.0 goes forwards
                            

                            Ian

                            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                            dkundefined 1 Reply Last reply Reply Quote 0
                            • dkundefined
                              dk @droftarts
                              last edited by

                              @droftarts

                              Changed. I still cant extrude

                              droftartsundefined 1 Reply Last reply Reply Quote 0
                              • droftartsundefined
                                droftarts administrators @dk
                                last edited by

                                @dk said in Multiple Errors Duet3:

                                @droftarts

                                Changed. I still cant extrude

                                Are there any errors now if you run M98 P"config.g"? You need to reset Duet for changes to config.g to take effect, or run M98 P"config.g". If there are still errors, please post your current config.g, along with the list of errors reported.

                                Assuming everything is set correctly with no errors, to extrude you either need to heat up the hot end to a temperature above 160C, or allow cold extrusion with M302 P1 (see https://duet3d.dozuki.com/Wiki/Gcode?revisionid=HEAD#Section_M302_Allow_cold_extrudes).

                                For the probe, you have already defined the servo pin with M950 S0 C"121.io0.out" ; create servo pin 0 for BLTouch in config.g, so it's unnecessary (and may cause confusion if you change the configuration later) in deployprobe.g and retractprobe.g. Delete the M950 line in these files.

                                Does the BLTouch do a self-test at startup? It should extend and retract the pin itself twice if it has power (which you say it does as the red LED comes on). If deployprobe.g and retractprobe.g still don't work, try inverting the input in config.g with '!', ie M950 S0 C"!121.io0.out". You can either send this command in the gcode console (and add it to config.g if it works), edit config.g and reset Duet, or edit config.g and run M98 P"config.g" for the command to take effect. If it still isn't functioning, check the wiring, and post a picture of how it's wired.

                                @dk said in Multiple Errors Duet3:

                                Can I find somewhere configuration files for any real working Delta printer on Duet3 with Tool board?

                                We don't have a machine with this configuration to share a working config with you. Many home-built printers are bespoke, and it's possible that you are the first with this combination! If there are any other users who see this and have a similar setup, please share your config files.

                                Ian

                                Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                dkundefined 1 Reply Last reply Reply Quote 0
                                • dkundefined
                                  dk @droftarts
                                  last edited by

                                  @droftarts

                                  I have change Toolboard address to 20 following this procedure See https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board#Section_Set_the_CAN_address , and change M569 P20.0 S1
                                  Now I can extrude.
                                  I also change address for heater and Thermistor and gget them work to!
                                  M308 S1 P"20.temp0" Y"thermistor" T500000 B4723 C1.19622e-7
                                  M950 H1 C"20.out0" T1

                                  And I also change address for BL-touch (with and without ! ) and delete M950 line from deployprobe.g and retractprobe.g files. But it's still don't work.
                                  ; Z-Probe
                                  M950 S0 C"20.io0.out" ; create servo pin 0 for BLTouch
                                  M558 P9 C"20.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
                                  G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                                  M557 R160 S40 ; define mesh grid

                                  And BLTouch does not self-test at startup. Just steady red light. I connect it to Duet2 I have on another printer and it perform startup test as usual.

                                  M98 P"config.g" give me just one warning (no Errors any more)
                                  Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C

                                  So I assume the problem is in Z-probe settings

                                  IMG_7378.jpg

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    Does the BLTouch power up if you connect it directly to the main board and change your pin names accordingly?

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    dkundefined 1 Reply Last reply Reply Quote 0
                                    • dkundefined
                                      dk @Phaedrux
                                      last edited by

                                      @Phaedrux
                                      Yes, it does

                                      1 Reply Last reply Reply Quote 0
                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        Do you have a different BLTouch that isn't V3.1 to test with on the tool board?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        dkundefined 2 Replies Last reply Reply Quote 0
                                        • dkundefined
                                          dk @Phaedrux
                                          last edited by

                                          @Phaedrux

                                          I have 3 BL-touch 3.1 And I test all 3 of them. They all work with IO_7 and doesn't work with Toolboard

                                          1 Reply Last reply Reply Quote 0
                                          • dkundefined
                                            dk @Phaedrux
                                            last edited by

                                            @Phaedrux
                                            When I change the white and yellow wire in places, BL-touch does self-test at startup. And Status window DWC shows Z-Probe 1000
                                            But it still does not work. I can't extract pin. M280 P0 S10 has no effect.
                                            And G32 give Error: Z probe already triggered at start of probing move

                                            Z-Probe settings from Config.g:
                                            M950 S0 C"20.io0.out" ; create servo pin 0 for BLTouch
                                            M558 P9 C"20.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
                                            G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                                            M557 R160 S40 ; define mesh grid

                                            ; deployprobe.g
                                            M280 P0 S10 ; deploy BLTouch

                                            ; retractprobe.g
                                            M280 P0 S90 ; retract BLTouch

                                            Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA