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Multiple Errors Duet3

Scheduled Pinned Locked Moved Solved
Firmware installation
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  • undefined
    Phaedrux Moderator @dk
    last edited by 22 Sept 2020, 18:17

    @dk Please post your config files so we can see what you have now.

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 1 Reply Last reply 22 Sept 2020, 21:35 Reply Quote 0
    • undefined
      dk @Phaedrux
      last edited by 22 Sept 2020, 21:35

      @Phaedrux

      Every time after reboot I get Error messages :
      Error: M950: Response timeout: CAN addr 1, req type 6027, RID=8
      Error: M106: Fan number 0 not found
      Error: M950: Response timeout: CAN addr 1, req type 6027, RID=10
      Error: M106: Fan number 1 not found

      And when I push Home all only one motor moves.

      Config.g
      ; Configuration file for Duet 3 (firmware version 3)
      ; executed by the firmware on start-up
      ;
      ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)

      ; General preferences
      G90 ; send absolute coordinates...
      M83 ; ...but relative extruder moves
      M550 P"Duet 3" ; set printer name
      M665 R240 L460 B190 H750 ; Set delta radius, diagonal rod length, printable radius and homed height
      M666 X0 Y0 Z0 ; put your endstop adjustments here, or let auto calibration find them

      ; Drives
      M569 P0.0 S1 ; physical drive 0.0 goes forwards
      M569 P0.1 S0 ; physical drive 0.1 goes forwards
      M569 P0.2 S0 ; physical drive 0.2 goes forwards
      M569 P1.0 S1 ; physical drive 1.0 goes forwards
      M584 X0.0 Y0.1 Z0.2 E1.0 ; set drive mapping
      M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
      M92 X160.00 Y160.00 Z160.00 E415.00 ; set steps per mm
      M566 X1200.00 Y1200.00 Z1200.00 E800.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X3000.00 Y3000.00 Z3000.00 E600.00 ; set maximum speeds (mm/min)
      M201 X3000.00 Y3000.00 Z3000.00 E1000.00 ; set accelerations (mm/s^2)
      M906 X1600 Y1600 Z1600 E900 I30 ; set motor currents (mA) and motor idle factor in per cent
      M84 S30 ; Set idle timeout

      ; Axis Limits
      M208 Z0 S1 ; set minimum Z

      ; Endstops
      M574 X2 S1 P"io0.in" ; configure active-high endstop for HIGH end on X via pin io0.in
      M574 Y2 S1 P"io1.in" ; configure active-high endstop for HIGH end on Y via pin io1.in
      M574 Z2 S1 P"io2.in" ; configure active-high endstop for HIGH end on Z via pin io2.in

      ; Z-Probe
      M950 S0 C"121.io0.out" ; create servo pin 0 for BLTouch
      M558 P9 C"121.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
      G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
      M557 R160 S40 ; define mesh grid

      ; Heaters
      M308 S0 P"temp3" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp3
      M950 H0 C"out1" T0 ; create bed heater output on out1 and map it to sensor 0
      M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
      M140 H0 ; map heated bed to heater 0
      M143 H0 S120 ; set temperature limit for heater 0 to 120C
      M308 S1 P"1.temp0" Y"thermistor" T500000 B4723 C1.19622e-7 ; configure sensor 1 as thermistor on pin 1.temp0
      M950 H1 C"1.out0" T1 ; create nozzle heater output on 1.out0 and map it to sensor 1
      M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit

      ; Fans
      M950 F0 C"1.out2" Q500 ; create fan 0 on pin 1.out2 and set its frequency
      M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
      M950 F1 C"1.out1" Q500 ; create fan 1 on pin 1.out1 and set its frequency
      M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on

      ; Tools
      M563 P0 D0 H1 F0 ; define tool 0
      G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

      ; Custom settings are not defined

      ; homedelta.g
      ; called to home all towers on a delta printer
      ;
      ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)
      G91 ; relative positioning
      G1 H1 X760 Y760 Z760 F1800 ; move all towers to the high end stopping at the endstops (first pass)
      G1 H2 X-5 Y-5 Z-5 F1800 ; go down a few mm
      G1 H1 X10 Y10 Z10 F360 ; move all towers up once more (second pass)
      G1 Z-5 F3600 ; move down a few mm so that the nozzle can be centred
      G90 ; absolute positioning
      G1 X0 Y0 F3600 ; move X+Y to the centre

      ; deployprobe.g
      ; called to deploy a physical Z probe
      ;
      ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)

      M950 S0 C"121.io0.out"
      M280 P0 S10 ; deploy BLTouch

      ; retractprobe.g
      ; called to retract a physical Z probe
      ;
      ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)
      M950 S0 C"121.io0.out"
      M280 P0 S90 ; retract BLTouch

      undefined 1 Reply Last reply 22 Sept 2020, 21:53 Reply Quote 0
      • undefined
        Phaedrux Moderator
        last edited by 22 Sept 2020, 21:37

        Can you send M122 and M98 P"config.g" and post the results?

        Z-Bot CoreXY Build | Thingiverse Profile

        undefined 1 Reply Last reply 22 Sept 2020, 23:23 Reply Quote 0
        • undefined
          droftarts administrators @dk
          last edited by 22 Sept 2020, 21:53

          @dk you have a Duet 3, and a Toolboard, correct? Did you follow the steps in this guide: https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board
          Have you changed the CAN address of your Toolboard? And if so, what to? See https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board#Section_Set_the_CAN_address

          Whatever it’s set to, at the moment you have some commands referring to CAN address 1 (extruder motor, hit end heater, fan etc), and some as CAN address 121, which is the default (BLTouch). Also, it may need a firmware update (further up in the document linked above).

          Ian

          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

          undefined 1 Reply Last reply 22 Sept 2020, 23:30 Reply Quote 0
          • undefined
            dk @Phaedrux
            last edited by 22 Sept 2020, 23:23

            @Phaedrux
            M122
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
            Board ID: 08DJM-956L2-G43S4-6JTDJ-3SJ6S-986GH
            Used output buffers: 1 of 40 (21 max)
            === RTOS ===
            Static ram: 154604
            Dynamic ram: 161404 of which 276 recycled
            Exception stack ram used: 224
            Never used ram: 76708
            Tasks: NETWORK(ready,1972) HEAT(blocked,1248) CanReceiv(suspended,3424) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4528) IDLE(ready,76)
            Owned mutexes:
            === Platform ===
            Last reset 00:00:44 ago, cause: power up
            Last software reset at 2020-09-22 22:34, reason: User, spinning module LinuxInterface, available RAM 76708 bytes (slot 0)
            Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
            Error status: 0
            MCU temperature: min 39.2, current 39.6, max 39.7
            Supply voltage: min 23.9, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
            12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0
            Driver 0: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
            Driver 1: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
            Driver 2: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
            Driver 3: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
            Driver 4: standstill, reads 24457, writes 0 timeouts 0, SG min/max not available
            Driver 5: standstill, reads 24456, writes 0 timeouts 0, SG min/max not available
            Date/time: 2020-09-22 22:34:11
            Slowest loop: 4.22ms; fastest: 0.20ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
            Bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is ready with "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon* is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 0.47ms; fastest: 0.01ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
            HTTP sessions: 0 of 8

            • Ethernet -
              State: disabled
              Error counts: 0 0 0 0 0
              Socket states: 0 0 0 0 0 0 0 0
              === CAN ===
              Messages sent 20, longest wait 0ms for type 0
              === Linux interface ===
              State: 0, failed transfers: 3
              Last transfer: 18ms ago
              RX/TX seq numbers: 539/540
              SPI underruns 3, overruns 3
              Number of disconnects: 0
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.1.1
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 0.02

            M98 P"config.g"
            Error: M569: Response timeout: CAN addr 1, req type 6018, RID=12
            Error: M350: Response timeout: CAN addr 1, req type 6021, RID=13
            Error: M906: Response timeout: CAN addr 1, req type 6017, RID=14
            Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
            Error: M308: Response timeout: CAN addr 1, req type 6011, RID=19
            Error: M950: Response timeout: CAN addr 1, req type 6026, RID=20
            Error: M307: Heater 1 not found
            Error: M950: Response timeout: CAN addr 1, req type 6027, RID=22
            Error: M106: Fan number 0 not found
            Error: M950: Response timeout: CAN addr 1, req type 6027, RID=24
            Error: M106: Fan number 1 not found

            1 Reply Last reply Reply Quote 0
            • undefined
              dk @droftarts
              last edited by 22 Sept 2020, 23:30

              @droftarts

              I have Duet3 and Toolboard with BMG and Mosquito Magnum + BL-touch
              I have follow all speps frome this guide.
              I did not changed the CAN address of Toolboard

              Sending M115 B121 give me :
              Board TOOL1LC firmware 3.1.0 (2020-05-15b1)

              undefined 1 Reply Last reply 22 Sept 2020, 23:35 Reply Quote 0
              • undefined
                droftarts administrators @dk
                last edited by 22 Sept 2020, 23:35

                @dk then you need to go through your config.g and change all references to CAN address 1 to 121, eg

                M569 P1.0 S1 ; physical drive 1.0 goes forwards

                Changes to:

                M569 P121.0 S1 ; physical drive 121.0 goes forwards
                

                Ian

                Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                undefined 1 Reply Last reply 23 Sept 2020, 01:36 Reply Quote 0
                • undefined
                  dk @droftarts
                  last edited by 23 Sept 2020, 01:36

                  @droftarts

                  Changed. I still cant extrude

                  undefined 1 Reply Last reply 23 Sept 2020, 11:44 Reply Quote 0
                  • undefined
                    droftarts administrators @dk
                    last edited by 23 Sept 2020, 11:44

                    @dk said in Multiple Errors Duet3:

                    @droftarts

                    Changed. I still cant extrude

                    Are there any errors now if you run M98 P"config.g"? You need to reset Duet for changes to config.g to take effect, or run M98 P"config.g". If there are still errors, please post your current config.g, along with the list of errors reported.

                    Assuming everything is set correctly with no errors, to extrude you either need to heat up the hot end to a temperature above 160C, or allow cold extrusion with M302 P1 (see https://duet3d.dozuki.com/Wiki/Gcode?revisionid=HEAD#Section_M302_Allow_cold_extrudes).

                    For the probe, you have already defined the servo pin with M950 S0 C"121.io0.out" ; create servo pin 0 for BLTouch in config.g, so it's unnecessary (and may cause confusion if you change the configuration later) in deployprobe.g and retractprobe.g. Delete the M950 line in these files.

                    Does the BLTouch do a self-test at startup? It should extend and retract the pin itself twice if it has power (which you say it does as the red LED comes on). If deployprobe.g and retractprobe.g still don't work, try inverting the input in config.g with '!', ie M950 S0 C"!121.io0.out". You can either send this command in the gcode console (and add it to config.g if it works), edit config.g and reset Duet, or edit config.g and run M98 P"config.g" for the command to take effect. If it still isn't functioning, check the wiring, and post a picture of how it's wired.

                    @dk said in Multiple Errors Duet3:

                    Can I find somewhere configuration files for any real working Delta printer on Duet3 with Tool board?

                    We don't have a machine with this configuration to share a working config with you. Many home-built printers are bespoke, and it's possible that you are the first with this combination! If there are any other users who see this and have a similar setup, please share your config files.

                    Ian

                    Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                    undefined 1 Reply Last reply 23 Sept 2020, 20:27 Reply Quote 0
                    • undefined
                      dk @droftarts
                      last edited by 23 Sept 2020, 20:27

                      @droftarts

                      I have change Toolboard address to 20 following this procedure See https://duet3d.dozuki.com/Wiki/Duet_3_Tool_Board#Section_Set_the_CAN_address , and change M569 P20.0 S1
                      Now I can extrude.
                      I also change address for heater and Thermistor and gget them work to!
                      M308 S1 P"20.temp0" Y"thermistor" T500000 B4723 C1.19622e-7
                      M950 H1 C"20.out0" T1

                      And I also change address for BL-touch (with and without ! ) and delete M950 line from deployprobe.g and retractprobe.g files. But it's still don't work.
                      ; Z-Probe
                      M950 S0 C"20.io0.out" ; create servo pin 0 for BLTouch
                      M558 P9 C"20.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
                      G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                      M557 R160 S40 ; define mesh grid

                      And BLTouch does not self-test at startup. Just steady red light. I connect it to Duet2 I have on another printer and it perform startup test as usual.

                      M98 P"config.g" give me just one warning (no Errors any more)
                      Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C

                      So I assume the problem is in Z-probe settings

                      IMG_7378.jpg

                      1 Reply Last reply Reply Quote 0
                      • undefined
                        Phaedrux Moderator
                        last edited by 23 Sept 2020, 20:41

                        Does the BLTouch power up if you connect it directly to the main board and change your pin names accordingly?

                        Z-Bot CoreXY Build | Thingiverse Profile

                        undefined 1 Reply Last reply 24 Sept 2020, 01:52 Reply Quote 0
                        • undefined
                          dk @Phaedrux
                          last edited by 24 Sept 2020, 01:52

                          @Phaedrux
                          Yes, it does

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            Phaedrux Moderator
                            last edited by 24 Sept 2020, 02:02

                            Do you have a different BLTouch that isn't V3.1 to test with on the tool board?

                            Z-Bot CoreXY Build | Thingiverse Profile

                            undefined 2 Replies Last reply 24 Sept 2020, 02:59 Reply Quote 0
                            • undefined
                              dk @Phaedrux
                              last edited by 24 Sept 2020, 02:59

                              @Phaedrux

                              I have 3 BL-touch 3.1 And I test all 3 of them. They all work with IO_7 and doesn't work with Toolboard

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                dk @Phaedrux
                                last edited by 24 Sept 2020, 17:58

                                @Phaedrux
                                When I change the white and yellow wire in places, BL-touch does self-test at startup. And Status window DWC shows Z-Probe 1000
                                But it still does not work. I can't extract pin. M280 P0 S10 has no effect.
                                And G32 give Error: Z probe already triggered at start of probing move

                                Z-Probe settings from Config.g:
                                M950 S0 C"20.io0.out" ; create servo pin 0 for BLTouch
                                M558 P9 C"20.io0.in" H5 F120 T1000 ; set Z probe type to bltouch and the dive height + speeds
                                G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                                M557 R160 S40 ; define mesh grid

                                ; deployprobe.g
                                M280 P0 S10 ; deploy BLTouch

                                ; retractprobe.g
                                M280 P0 S90 ; retract BLTouch

                                undefined 1 Reply Last reply 24 Sept 2020, 18:05 Reply Quote 0
                                • undefined
                                  Phaedrux Moderator @dk
                                  last edited by 24 Sept 2020, 18:05

                                  @dk said in Multiple Errors Duet3:

                                  When I change the white and yellow wire in places

                                  What do you mean by this?

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  undefined 1 Reply Last reply 24 Sept 2020, 20:33 Reply Quote 0
                                  • undefined
                                    dk @Phaedrux
                                    last edited by 24 Sept 2020, 20:33

                                    @Phaedrux
                                    Swap these two wires

                                    IMG_7378.jpg

                                    1 Reply Last reply Reply Quote 0
                                    • undefined
                                      Phaedrux Moderator
                                      last edited by 24 Sept 2020, 20:39

                                      Ah ok, so you had the io in and io out swapped.

                                      Since it says it's already triggered you could invert the signal pin, but I don't think that should be necessary.

                                      Try adding an ! to the pin name. M558 P9 C"!20.io0.in"

                                      That should get rid of the already triggered error, but do carefully test that touching the deployed pin halts movement.

                                      https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe#Section_Dynamic_test

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      undefined 2 Replies Last reply 24 Sept 2020, 23:21 Reply Quote 0
                                      • undefined
                                        dk @Phaedrux
                                        last edited by 24 Sept 2020, 23:21

                                        @Phaedrux

                                        No, with ! Status window DWC shows Z-Probe 0
                                        But it did self-test at startup.
                                        Should I chenge any other settings ?

                                        ; Z-Probe
                                        M950 S0 C"20.io0.out" ; create servo pin 0 for BLTouch
                                        M558 P9 C"20.io0.in" H5 F600 T1000 ; set Z probe type to bltouch and the dive height + speeds
                                        G31 P500 X20 Y25 Z3 ; set Z probe trigger value, offset and trigger height
                                        M557 R160 S40 ; define mesh grid

                                        1 Reply Last reply Reply Quote 0
                                        • undefined
                                          dk @Phaedrux
                                          last edited by 28 Sept 2020, 02:04

                                          @Phaedrux
                                          When I connect BL-touch to IO_7 it works. So I think the problem is in Toolboard

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