Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Giant Delta printer Slow Homing issue.

    Scheduled Pinned Locked Moved
    My Duet controlled machine
    8
    84
    3.4k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • sozkanundefined
      sozkan @Phaedrux
      last edited by

      @Phaedrux said in Giant Delta printer Slow Homing issue.:

      M569 P1 P2 P3 are fine if those cause the motors to move those are the correct ones. It's just targeting those driver numbers.

      https://duet3d.dozuki.com/Wiki/Gcode?revisionid=HEAD#Section_M569_1_Stepper_driver_closed_loop_control

      It`s some how stable on motor step control, but with those settings, I cannot control Enable or disable the motor features as well as the direction due to the illegal numbering. Because event Mr. admin "dc42" suggests for the external motor drives the stepper breakout board legal codes P5,6,7,8. Somehow these legal settings only working enable and direction settings and unstable step signals for the motor.

      1 Reply Last reply Reply Quote 0
      • sozkanundefined
        sozkan @Phaedrux
        last edited by

        @Phaedrux said in Giant Delta printer Slow Homing issue.:

        And yes, reduce acceleration and jerk. That should help a bit.

        The motors are going to be loud. They are large and mounted to metal, but hopefully the adjusted timing and acceleration will make it a bit more bearable.

        @sozkan said in Giant Delta printer Slow Homing issue.:

        Because motors are accurately working on illegal code, but creating horrible sound and incorrectly working on legal code.

        It's not illegal code if it works.

        Since it is not functioning other variables except stepping, also according to the Firmware developer it is illegal 🙂

        sozkanundefined 1 Reply Last reply Reply Quote 0
        • sozkanundefined
          sozkan @sozkan
          last edited by

          @sozkan said in Giant Delta printer Slow Homing issue.:

          @Phaedrux said in Giant Delta printer Slow Homing issue.:

          And yes, reduce acceleration and jerk. That should help a bit.

          The motors are going to be loud. They are large and mounted to metal, but hopefully the adjusted timing and acceleration will make it a bit more bearable.

          @sozkan said in Giant Delta printer Slow Homing issue.:

          Because motors are accurately working on illegal code, but creating horrible sound and incorrectly working on legal code.

          It's not illegal code if it works.

          Since it is not functioning other variables except stepping, also according to the Firmware developer it is illegal 🙂

          Until I found a stable solution, I will continue with this achieved a motor enable issue by hardware and mechanical brake gearbox and right direction setup on external motor driver. I believe it might run G-codes sufficiently if there is no hidden failure.

          1 Reply Last reply Reply Quote 0
          • sozkanundefined
            sozkan @Phaedrux
            last edited by

            @Phaedrux said in Giant Delta printer Slow Homing issue.:

            M98 P"config.g"

            Hi,
            I have just done your advise:
            result :
            10/23/2020, 4:31:32 PM M122
            === Diagnostics ===
            RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2-beta1 running on Duet WiFi 1.02 or later
            Board ID: 08DGM-917DA-G4MS8-6JTD4-3S86J-19SHA
            Used output buffers: 3 of 24 (21 max)
            === RTOS ===
            Static ram: 23916
            Dynamic ram: 98532 of which 120 recycled
            Exception stack ram used: 544
            Never used ram: 7960
            Tasks: NETWORK(ready,125) HEAT(blocked,138) MAIN(running,328) IDLE(ready,20)
            Owned mutexes: WiFi(NETWORK)
            === Platform ===
            Last reset 00:03:52 ago, cause: power up
            Last software reset at 2020-10-22 20:24, reason: User, GCodes spinning, available RAM 8036, slot 0
            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN
            Error status: 0x028
            MCU temperature: min 30.7, current 32.4, max 32.6
            Supply voltage: min 24.2, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
            Driver 0: position 276494, standstill, SG min/max not available
            Driver 1: position 276494, standstill, SG min/max not available
            Driver 2: position 276494, standstill, SG min/max not available
            Driver 3: position 0, standstill, SG min/max not available
            Driver 4: position 0, standstill, SG min/max not available
            Driver 5: position 0
            Driver 6: position 0
            Driver 7: position 0
            Driver 8: position 0
            Driver 9: position 0
            Driver 10: position 0
            Driver 11: position 0
            Date/time: 2020-10-23 16:31:31
            Cache data hit count 407671411
            Slowest loop: 65.60ms; fastest: 0.15ms
            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
            === Storage ===
            Free file entries: 10
            SD card 0 detected, interface speed: 20.0MBytes/sec
            SD card longest read time 1.0ms, write time 28.7ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 169, MinFreeDm: 169, MaxWait: 0ms
            Bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 19, completed moves: 19, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP is idle in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            Daemon is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 217.22ms; fastest: 0.09ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
            HTTP sessions: 1 of 8

            • WiFi -
              Network state is active
              WiFi module is connected to access point
              Failed messages: pending 0, notready 0, noresp 2
              WiFi firmware version 1.23
              WiFi MAC address 80:7d:3a:3f:f6:73
              WiFi Vcc 3.38, reset reason Turned on by main processor
              WiFi flash size 4194304, free heap 22848
              WiFi IP address 192.168.43.196
              WiFi signal strength -67dBm, reconnections 0, sleep mode modem
              Clock register ffffffff
              Socket states: 0 0 0 0 0 0 0 0
              10/23/2020, 4:30:44 PM Error: Temperature reading fault on heater 1: sensor open circuit
              Error: Temperature reading fault on heater 2: sensor open circuit
              10/23/2020, 4:30:42 PM M98 P"config.g"
              HTTP is enabled on port 80
              FTP is disabled
              TELNET is disabled
              Error: Driver 6 does not support x0 microstepping with interpolation
              Driver 7 does not support x0 microstepping with interpolation
              Driver 8 does not support x0 microstepping with interpolation
              Driver 5 does not support x0 microstepping with interpolation
              Warning: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
              Warning: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 258C
            Phaedruxundefined 1 Reply Last reply Reply Quote 0
            • Phaedruxundefined
              Phaedrux Moderator @sozkan
              last edited by

              @sozkan said in Giant Delta printer Slow Homing issue.:

              RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2-beta1 running on Duet WiFi 1.02 or later

              I would say in your current situation of commissioning and tuning you should stick with firmware 3.1.1

              Upload this zip file as is, don't extract it, to the system tab in the web interface.

              https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet2and3Firmware-3.1.1.zip

              @sozkan said in Giant Delta printer Slow Homing issue.:

              Error: Driver 6 does not support x0 microstepping with interpolation
              Driver 7 does not support x0 microstepping with interpolation
              Driver 8 does not support x0 microstepping with interpolation
              Driver 5 does not support x0 microstepping with interpolation

              M350 X0 Y0 Z0 E0 I1

              I think you're going to need to specify a microstepping value. 0 won't work. Try 1.

              Z-Bot CoreXY Build | Thingiverse Profile

              sozkanundefined 1 Reply Last reply Reply Quote 0
              • sozkanundefined
                sozkan @Phaedrux
                last edited by

                @Phaedrux said in Giant Delta printer Slow Homing issue.:

                @sozkan said in Giant Delta printer Slow Homing issue.:

                RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2-beta1 running on Duet WiFi 1.02 or later

                I would say in your current situation of commissioning and tuning you should stick with firmware 3.1.1

                Upload this zip file as is, don't extract it, to the system tab in the web interface.

                https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet2and3Firmware-3.1.1.zip

                @sozkan said in Giant Delta printer Slow Homing issue.:

                Error: Driver 6 does not support x0 microstepping with interpolation
                Driver 7 does not support x0 microstepping with interpolation
                Driver 8 does not support x0 microstepping with interpolation
                Driver 5 does not support x0 microstepping with interpolation

                M350 X0 Y0 Z0 E0 I1

                I think you're going to need to specify a microstepping value. 0 won't work. Try 1.

                I will definitely try your advice soon. I was formating file structure, I can't connect web interface anymore now. I have backed up fully the SD card. Reverted back but still not connecting.

                sozkanundefined 1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  Your SD card needs a file structure like this: https://duet3d.dozuki.com/Wiki/SD_Card#Section_Creating_the_file_structure

                  The web interface files need be placed in the /www folder and come from here: https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/DuetWebControl-SD-3.1.1.zip

                  Z-Bot CoreXY Build | Thingiverse Profile

                  1 Reply Last reply Reply Quote 0
                  • sozkanundefined
                    sozkan @sozkan
                    last edited by

                    @sozkan said in Giant Delta printer Slow Homing issue.:

                    @Phaedrux said in Giant Delta printer Slow Homing issue.:

                    @sozkan said in Giant Delta printer Slow Homing issue.:

                    RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2-beta1 running on Duet WiFi 1.02 or later

                    I would say in your current situation of commissioning and tuning you should stick with firmware 3.1.1

                    Upload this zip file as is, don't extract it, to the system tab in the web interface.

                    https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet2and3Firmware-3.1.1.zip

                    @sozkan said in Giant Delta printer Slow Homing issue.:

                    Error: Driver 6 does not support x0 microstepping with interpolation
                    Driver 7 does not support x0 microstepping with interpolation
                    Driver 8 does not support x0 microstepping with interpolation
                    Driver 5 does not support x0 microstepping with interpolation

                    M350 X0 Y0 Z0 E0 I1

                    I think you're going to need to specify a microstepping value. 0 won't work. Try 1.

                    I will definitely try your advice soon. I was formating file structure, I can't connect web interface anymore now. I have backed up fully the SD card. Reverted back but still not connecting.

                    I normally install the beta update using the web interface. The CSS and www folders appeared in the sys folder after that.

                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @sozkan
                      last edited by

                      @sozkan said in Giant Delta printer Slow Homing issue.:

                      I normally install the beta update using the web interface. The CSS and www folders appeared in the sys folder after that.

                      Did you upload the full zip file without extracting it first?

                      You must not extract the zip file.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      sozkanundefined 1 Reply Last reply Reply Quote 0
                      • sozkanundefined
                        sozkan @Phaedrux
                        last edited by

                        @Phaedrux said in Giant Delta printer Slow Homing issue.:

                        @sozkan said in Giant Delta printer Slow Homing issue.:

                        I normally install the beta update using the web interface. The CSS and www folders appeared in the sys folder after that.

                        Did you upload the full zip file without extracting it first?

                        You must not extract the zip file.

                        yes I did in the past with zip in beta version upgrade. But this case I cannot connect web interface. Panedue console says it connected to the IP : 192.168.1.200 but on my hotspot network it shows unknow IP connection. I have uploaded the firmware files in the SD card that you sent me now and reinstall firmware using the PaneDue interface with "M997 S0 to install the firmware" and "M997 S1 to install the WiFi module firmware" so successfully updated. After I send M115 to confirm the new firmware version it is still beta version remain and not connected.

                        1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          It sounds like your /www folder may be missing still?

                          Z-Bot CoreXY Build | Thingiverse Profile

                          sozkanundefined 1 Reply Last reply Reply Quote 0
                          • sozkanundefined
                            sozkan @Phaedrux
                            last edited by

                            @Phaedrux said in Giant Delta printer Slow Homing issue.:

                            It sounds like your /www folder may be missing still?

                            I actually revert the backup which is previously connecting with no issue.
                            This problem just appeared. I have tried to connect different SSID name, I could not save into controller gives error on the saving list. It seems like the controller relying on "config.json" keep connecting old parameters. By the way, I have reinstalled back beta firmware just to see if it will connect.

                            1 Reply Last reply Reply Quote 0
                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              config.json is just used by the online config tool

                              Can you post a photo of what your SD card file structure looks like now?

                              Since you have a PanelDue it may be a good idea to add some macros to your SD card macros folder to aid in diagnostics.

                              https://github.com/Duet3D/RRF-machine-config-files/tree/master/DBotCoreXY/x0r-wifi-RRF3/macros/Diagnostics

                              At the bottom of that list are 3 wifi macros which you can customize with your SSID name to make clearing and adding the wifi network easy from the paneldue.

                              Sending M997 S1 should reflash the wifi server firmware in case something went wrong on the last update.

                              If you send M122 from a USB connection you can see the wifi server status at the end. The response is too large for the PanelDue to display.

                              Z-Bot CoreXY Build | Thingiverse Profile

                              sozkanundefined 2 Replies Last reply Reply Quote 0
                              • sozkanundefined
                                sozkan @Phaedrux
                                last edited by

                                @Phaedrux said in Giant Delta printer Slow Homing issue.:

                                config.json is just used by the online config tool

                                Can you post a photo of what your SD card file structure looks like now?

                                Since you have a PanelDue it may be a good idea to add some macros to your SD card macros folder to aid in diagnostics.

                                https://github.com/Duet3D/RRF-machine-config-files/tree/master/DBotCoreXY/x0r-wifi-RRF3/macros/Diagnostics

                                At the bottom of that list are 3 wifi macros which you can customize with your SSID name to make clearing and adding the wifi network easy from the paneldue.

                                Sending M997 S1 should reflash the wifi server firmware in case something went wrong on the last update.

                                If you send M122 from a USB connection you can see the wifi server status at the end. The response is too large for the PanelDue to display.

                                Thanks. Macros help to reset the wifi module. I am in DWC now finally.

                                1 Reply Last reply Reply Quote 0
                                • sozkanundefined
                                  sozkan @Phaedrux
                                  last edited by sozkan

                                  @Phaedrux !DuetSysStr.png
                                  I have added files on the sys folder before downgrade to the stable 3.11 version. I will update using the web interface.

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    I'm a little confused.

                                    Are you on 3.2 beta still, or 3.1.1?

                                    I think maybe some other files may be missing.

                                    You could try updating with 3.0 first, and then 3.1.1

                                    https://github.com/Duet3D/RepRapFirmware/releases/download/3.0/Duet2and3Firmware-3.0.zip

                                    https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet2and3Firmware-3.1.1.zip

                                    Remember to upload the entire intact zip file to the system tab. Don't extract.

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    sozkanundefined 1 Reply Last reply Reply Quote 0
                                    • sozkanundefined
                                      sozkan @Phaedrux
                                      last edited by

                                      @Phaedrux I have actually Upgraded to 3.0 at first. later 3.11 and latest beta. Presently I have downgraded to 3.1.1 using DWC .

                                      I have checked your previous recommendation Micro Stepping "1" it is still remain horrible sound ;

                                      ; Drives
                                      M569 P5 S0 R0 T3:3:5:0         ; Extruder drive 0 goes Forward
                                      M569 P6 S1 R0 T2.5:2.5:6:6  ; X:A drive 1 goes Forward
                                      M569 P7 S1 R0 T2.5:2.5:6:6  ; Y:B drive 2 goes Forward
                                      M569 P8 S1 R0 T2.5:2.5:6:6  ; Z:C physical drive 3 goes Forward
                                      
                                      M584 X6 Y7 Z8 E5                                  			 ; set drive mapping
                                      M350 X1 Y1 Z1 E1 I1                                ; configure microstepping without interpolation
                                      
                                      1 Reply Last reply Reply Quote 0
                                      • sozkanundefined
                                        sozkan
                                        last edited by sozkan

                                        Hi again.

                                        It was seemed resolved. But cracking sound revealed again on different homing variations.

                                        if one of the motors for each other and if two of the three-axis reaches the limit switches, the last motor starts on a noisy signal and can't complete the move distance. During the home Cracking noisy sound. The failing reason seems running less than the specified home distance. But the distance is correct.
                                        Please see the video on this issue:
                                        https://www.youtube.com/watch?v=2GGh0wQdLYQ

                                        I believe the hardware is fine. Because once it is successfully homed, working calibrated and smooth.

                                        if once fails on homing, and If I move the motors manually away from limit switches, homing again smooth. the somehow nosy signal appears if two limits switch on.

                                        I also doubted if limit switches contact cause power loss? Should I put a resistor in series to try?

                                        it is currently on the config file.

                                        ; Drives
                                        M569 P5 S0 R0 T3:3:5:0      ; Extruder drive 0 goes Forward
                                        M569 P2 S1 R0 T2.5:2.5:6:6  ; X:A drive 1 goes Forward
                                        M569 P3 S1 R0 T2.5:2.5:6:6  ; Y:B drive 2 goes Forward
                                        M569 P4 S1 R0 T2.5:2.5:6:6  ; Z:C physical drive 3 goes Forward
                                        
                                        M584 X6 Y7 Z8 E5                                   ; set drive mapping
                                        M350 X0 Y0 Z0 E0 I0                                ; configure microstepping without interpolation
                                        

                                        It says Y-axis not homed which is connected on E4 for on the breakout board. But during the Delta move, Y-axis toward the Z-axis direction, and Z motor moves more.

                                        sozkanundefined 1 Reply Last reply Reply Quote 0
                                        • sozkanundefined
                                          sozkan @sozkan
                                          last edited by

                                          @sozkan By the way my Home Gcode

                                          homedelta.g :

                                          ; homedelta.g
                                          ; called to home all towers on a delta printer
                                          ;
                                          ; generated by RepRapFirmware Configuration Tool v3.1.4 on Sun Sep 27 2020 20:52:39 GMT+0200 (Central European Summer Time)
                                          G91                         ; relative positioning
                                          ;*** Slow homing has been configured. Change F90 to F900 below when your configuration is working
                                          G1 H1 X1805 Y1805 Z1805 F800 ; move all towers to the high end stopping at the endstops (first pass)
                                          G1 H2 X-10 Y-10 Z-10 F800      ; go down a few mm
                                          ;*** Slow homing has been configured. Change F90 to F360 below when your configuration is working
                                          G1 H1 X10 Y10 Z10 F800      ; move all towers up once more (second pass)
                                          G1 Z-15 F1200                ; move down a few mm so that the nozzle can be centred
                                          G90                         ; absolute positioning
                                          G1 X0 Y0 F1000              ; move X+Y to the centre
                                          
                                          
                                          
                                          1 Reply Last reply Reply Quote 0
                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Are you sure the endstop for each tower actually corresponds to that tower at the board connection and firmware definition?

                                            d58d6c78-2e35-41d9-80e8-1a16ceb4824c-image.png

                                            https://reprap.org/wiki/Delta_geometry#Delta_columns_and_axis_names

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            sozkanundefined 1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA