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    Did I fry my new board....

    Scheduled Pinned Locked Moved
    Duet Hardware and wiring
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    • Harvdog1undefined
      Harvdog1 @Phaedrux
      last edited by

      @Phaedrux One Z motor and the jumper is installed.

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Can you post a photo of driver 2 in case there's some damage visible?

        If the driver is damaged and you have a free extruder driver you can remap it to the z axis to get up and running.

        M584 X0 Y1 Z2 E3 ; set drive mapping

        would become

        M584 X0 Y1 Z4 E3 ; set drive mapping

        What are the specs of your motors? What is the rated current?

        M906 X400 Y400 Z400 E800 I30 ; set motor currents (mA) and motor idle factor in per cent

        It's recommended to set the current to 60-85% of the motors rated current.

        Do the other drivers work?

        Z-Bot CoreXY Build | Thingiverse Profile

        Harvdog1undefined 1 Reply Last reply Reply Quote 0
        • Harvdog1undefined
          Harvdog1 @Phaedrux
          last edited by

          @Phaedrux I had been working on this exact thing, I finally got the X going, I could issue it a command to move left or right and it started working. Prior to that it and the other 2 would just make horrible noises. Once it was working on the X, i checked the connections on the wiring, meaning how the wires were plugged into the little plastic things. The others were not matching that one, so I started moving wires around trying to replicate the one what was working. That did not work, now that one good wire will not work on the x axis...

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          • Vetiundefined
            Veti
            last edited by

            do not just randomly try wire position

            please follow this guide

            https://duet3d.dozuki.com/Wiki/Choosing_and_connecting_stepper_motors#Section_Connecting_stepper_motors

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            • Harvdog1undefined
              Harvdog1 @Phaedrux
              last edited by

              @Phaedrux
              48e88f80-d95b-4e23-bae7-a4d753d8cbf2-image.png

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              • Vetiundefined
                Veti
                last edited by

                @Harvdog1 said in Did I fry my new board....:

                M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1

                you configured e0heat but connected the heater to e1

                you really should be recrimping those connectors.

                Harvdog1undefined 1 Reply Last reply Reply Quote 0
                • Harvdog1undefined
                  Harvdog1 @Veti
                  last edited by

                  @Veti The crimper is in route. The hot end was connected like it is because I did it like one of the you tubers, he had his there. I see it now in position 1 and should be moved over to the left to zero.
                  Thank you

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                  • Vetiundefined
                    Veti
                    last edited by

                    @Harvdog1 said in Did I fry my new board....:

                    The hot end was connected like it is because I did it like one of the you tubers,

                    if you follow a guide please have a look at
                    https://duet3d.dozuki.com/Guide/Ender+3+Pro+and+Duet+Maestro+Guide+Part+1:+Wiring/37

                    it should be mostly be the same

                    Harvdog1undefined 1 Reply Last reply Reply Quote 0
                    • Harvdog1undefined
                      Harvdog1 @Veti
                      last edited by

                      @Veti The micro swiss hotend is working now, thank you. Is there a way to find out if the drivers are all ok?

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                      • Vetiundefined
                        Veti
                        last edited by

                        you said you had one that is working already.

                        you can move that one to the different ports to test each driver.
                        only move the connector when the duet is powered off.

                        Harvdog1undefined 1 Reply Last reply Reply Quote 0
                        • Harvdog1undefined
                          Harvdog1 @Veti
                          last edited by

                          @Veti I did try that with the known good wire, and the others did not work. When I plugged it back into the X, it no longer worked. So they are all down at the moment.

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                          • Vetiundefined
                            Veti
                            last edited by

                            what command are you using to test the movement?

                            Harvdog1undefined 1 Reply Last reply Reply Quote 0
                            • Harvdog1undefined
                              Harvdog1 @Veti
                              last edited by

                              @Veti I did a G1 X10, that kind of thing, did a couple of G1 X-10

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                              • Vetiundefined
                                Veti
                                last edited by

                                did you issue M564 S0 H0 before like it says in the guide?

                                Harvdog1undefined 1 Reply Last reply Reply Quote 0
                                • Harvdog1undefined
                                  Harvdog1 @Veti
                                  last edited by

                                  @Veti said in Did I fry my new board....:

                                  M564 S0 H0

                                  I dont remember, I have tried so many things. I just did, and got the error of insufficient axes homed

                                  Vetiundefined 1 Reply Last reply Reply Quote 0
                                  • Vetiundefined
                                    Veti @Harvdog1
                                    last edited by

                                    @Harvdog1 said in Did I fry my new board....:

                                    I just did, and got the error of insufficient axes homed

                                    you got that error after you put in M564 S0 H0 ?
                                    that makes no sense

                                    Harvdog1undefined 1 Reply Last reply Reply Quote 0
                                    • Harvdog1undefined
                                      Harvdog1 @Veti
                                      last edited by

                                      @Veti Sorry, that was the error for the G1 X10. The M564 S0 H0 got a green light, but nothing happened that I can tell.

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                                      • Vetiundefined
                                        Veti
                                        last edited by

                                        the command on its own does not do any movements

                                        have you read the linked wiki page?
                                        its described there
                                        https://duet3d.dozuki.com/Wiki/Choosing_and_connecting_stepper_motors#Section_Checking_connected_stepper_motors

                                        Harvdog1undefined 1 Reply Last reply Reply Quote 0
                                        • Harvdog1undefined
                                          Harvdog1 @Veti
                                          last edited by

                                          @Veti I will read that. X is working now, but goes the wrong way. Y and Z sound like they want to work, but do not go anywhere. Hot end works now. Bed heater is still down. Cant tell which is which as its a white wire. Tried it both way and get the error of rising too slow.
                                          Thank you so much

                                          Harvdog1undefined 1 Reply Last reply Reply Quote 0
                                          • Vetiundefined
                                            Veti
                                            last edited by

                                            @Harvdog1 said in Did I fry my new board....:

                                            Cant tell which is which as its a white wire. Tried it both way and get the error of rising too slow.

                                            as phaedrux wrote, it wont work without pid tuning.

                                            for the motors please use the known good stepper and move them to y and test again.

                                            Harvdog1undefined 2 Replies Last reply Reply Quote 0
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