Artillery Genius Duet 2 Wifi Configuration
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@Veti i set it upo wrong with the configurator. it should be thermistor 1 in merlin like the heatbed. heatbed sensor shows 20°C so it works. Not sure what i did wrong with the extruder thermistor
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is it 200 or 2000 ?
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@Veti 2000
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So i just did some try and error. I have 2 Z motors. They worked against each other. Now it they work right.
y axis works fine. When i move X-axis z Axis moves aswell. I move the motors without homing atm.
I plugged all motors off and tried each motor alone with the y axis. they worked all great. not sure why they move together when i move z or y axis alone in the dashboard. U have any suggestions what i can check ? -
2000 means open circuit.
so check the wiring.
measure the resistance with a multimeter
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@Veti ok!
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@Veti Both Thermistors work now! Thank you very much
U have any idea why both x and z axis move when i try to move one of them ?
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i could be because of mesh compensation
how are you moving the axis?
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@Veti I just do the M564 S0 H0 Command so i can move axis without homing
and than i just go to dashboard and click on the bottons to move the axis manual. I did not active do a mesh bed compensation, is there a way to check in config if there is any setting done ? -
in what way is the z axis moving when you move the x
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post your current config.g m122 and a picture of your wiring
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@Veti The movement of second axis is not random, if i move pos the second axis does as well. when i move neg. it moves neg. aswell.
M112:
m122
=== Diagnostics ===
RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2 running on Duet WiFi 1.02 or later
Board ID: 0JD0M-9P6M2-NW4SN-6J9D2-3SD6S-9VT7M
Used output buffers: 3 of 24 (18 max)
=== RTOS ===
Static ram: 23460
Dynamic ram: 73284 of which 24 recycled
Never used RAM 15312, free system stack 189 words
Tasks: NETWORK(ready,160) HEAT(blocked,309) MAIN(running,450) IDLE(ready,19)
Owned mutexes: WiFi(NETWORK)
=== Platform ===
Last reset 00:06:15 ago, cause: power up
Last software reset at 2021-01-29 19:39, reason: User, GCodes spinning, available RAM 15276, slot 2
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
Aux0 errors 0,0,0
MCU temperature: min 21.1, current 28.5, max 29.1
Supply voltage: min 24.1, current 24.2, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: position 0, standstill, SG min/max not available
Driver 1: position 0, standstill, SG min/max not available
Driver 2: position 0, standstill, SG min/max not available
Driver 3: position 0, standstill, SG min/max not available
Driver 4: position 0, standstill, SG min/max not available
Driver 5: position 0
Driver 6: position 0
Driver 7: position 0
Driver 8: position 0
Driver 9: position 0
Driver 10: position 0
Driver 11: position 0
Date/time: 2021-01-29 20:09:26
Cache data hit count 464421949
Slowest loop: 6.16ms; fastest: 0.20ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 20.0MBytes/sec
SD card longest read time 2.9ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
Daemon is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 15.17ms; fastest: 0.00ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
HTTP sessions: 1 of 8- WiFi -
Network state is active
WiFi module is connected to access point
Failed messages: pending 0, notready 0, noresp 0
WiFi firmware version 1.21RC2
WiFi MAC address 40:f5:20:1d:c0:8e
WiFi Vcc 3.45, reset reason Turned on by main processor
WiFi flash size 4194304, free heap 16912
WiFi IP address 192.168.178.160
WiFi signal strength -51dBm, mode none, reconnections 0, sleep mode modem
Clock register ffffffff
Socket states: 0 0 0 0 0 0 0 0
- WiFi -
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did you plug in x motor into the second z header by accident?
WiFi firmware version 1.21RC2
you did not update your wifi firmware
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Could this be the problem ? When i click on Compensation and Callibration it says: Compensation in use: none.
Im 100% Sure i use the right motor in the right plugs. Tested the connection like an hour ago and tested every motor while i plugged off all others
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Upload this zip file to the system tab in DWC.
https://github.com/Duet3D/RepRapFirmware/releases/download/3.2/Duet2and3Firmware-3.2.zip
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@Phaedrux I will test it after installation!
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post your current config
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@Phaedrux Reply how long does the installation normally take ? Now i cant connect. Does it save my Networksettings normally ?
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@Veti The current config is the one i posted a bit upper in this thread. did not change anything since than and i cant connect to my board due to the update right now
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@d0minik96 said in Artillery Genius Duet 2 Wifi Configuration:
@Phaedrux Reply how long does the installation normally take ? Now i cant connect. Does it save my Networksettings normally ?
WiFi firmware version 1.21RC2
I wonder if your wifi firmware was so old that behaviour has changed.
You may need to connect with USB terminal to see what is happening. Use M122 to check if the wifi firmware was updated to 1.25.
Then use M552 S1 to see if it will enable and connect.
Use M587 to see a list of currently saved SSIDs
use M588 S"*" to clear all curently saved SSIDs
and then use M587 S"networkname" P"password" to readd your SSID