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    Artillery Genius Duet 2 Wifi Configuration

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    • d0minik96undefined
      d0minik96 @Veti
      last edited by

      @Veti I just do the M564 S0 H0 Command so i can move axis without homing
      and than i just go to dashboard and click on the bottons to move the axis manual. I did not active do a mesh bed compensation, is there a way to check in config if there is any setting done ?

      1 Reply Last reply Reply Quote 0
      • Vetiundefined
        Veti
        last edited by

        in what way is the z axis moving when you move the x

        1 Reply Last reply Reply Quote 0
        • Vetiundefined
          Veti
          last edited by

          post your current config.g m122 and a picture of your wiring

          d0minik96undefined 1 Reply Last reply Reply Quote 0
          • d0minik96undefined
            d0minik96 @Veti
            last edited by

            @Veti The movement of second axis is not random, if i move pos the second axis does as well. when i move neg. it moves neg. aswell.

            M112:
            m122
            === Diagnostics ===
            RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2 running on Duet WiFi 1.02 or later
            Board ID: 0JD0M-9P6M2-NW4SN-6J9D2-3SD6S-9VT7M
            Used output buffers: 3 of 24 (18 max)
            === RTOS ===
            Static ram: 23460
            Dynamic ram: 73284 of which 24 recycled
            Never used RAM 15312, free system stack 189 words
            Tasks: NETWORK(ready,160) HEAT(blocked,309) MAIN(running,450) IDLE(ready,19)
            Owned mutexes: WiFi(NETWORK)
            === Platform ===
            Last reset 00:06:15 ago, cause: power up
            Last software reset at 2021-01-29 19:39, reason: User, GCodes spinning, available RAM 15276, slot 2
            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
            Error status: 0x00
            Aux0 errors 0,0,0
            MCU temperature: min 21.1, current 28.5, max 29.1
            Supply voltage: min 24.1, current 24.2, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
            Driver 0: position 0, standstill, SG min/max not available
            Driver 1: position 0, standstill, SG min/max not available
            Driver 2: position 0, standstill, SG min/max not available
            Driver 3: position 0, standstill, SG min/max not available
            Driver 4: position 0, standstill, SG min/max not available
            Driver 5: position 0
            Driver 6: position 0
            Driver 7: position 0
            Driver 8: position 0
            Driver 9: position 0
            Driver 10: position 0
            Driver 11: position 0
            Date/time: 2021-01-29 20:09:26
            Cache data hit count 464421949
            Slowest loop: 6.16ms; fastest: 0.20ms
            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
            === Storage ===
            Free file entries: 10
            SD card 0 detected, interface speed: 20.0MBytes/sec
            SD card longest read time 2.9ms, write time 0.0ms, max retries 0
            === Move ===
            DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
            === AuxDDARing ===
            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP is idle in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            Daemon is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 15.17ms; fastest: 0.00ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
            HTTP sessions: 1 of 8

            • WiFi -
              Network state is active
              WiFi module is connected to access point
              Failed messages: pending 0, notready 0, noresp 0
              WiFi firmware version 1.21RC2
              WiFi MAC address 40:f5:20:1d:c0:8e
              WiFi Vcc 3.45, reset reason Turned on by main processor
              WiFi flash size 4194304, free heap 16912
              WiFi IP address 192.168.178.160
              WiFi signal strength -51dBm, mode none, reconnections 0, sleep mode modem
              Clock register ffffffff
              Socket states: 0 0 0 0 0 0 0 0
            1 Reply Last reply Reply Quote 0
            • Vetiundefined
              Veti
              last edited by

              did you plug in x motor into the second z header by accident?

              WiFi firmware version 1.21RC2

              you did not update your wifi firmware

              1 Reply Last reply Reply Quote 0
              • d0minik96undefined
                d0minik96
                last edited by

                Could this be the problem ? When i click on Compensation and Callibration it says: Compensation in use: none.

                Im 100% Sure i use the right motor in the right plugs. Tested the connection like an hour ago and tested every motor while i plugged off all others

                1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  Upload this zip file to the system tab in DWC.

                  https://github.com/Duet3D/RepRapFirmware/releases/download/3.2/Duet2and3Firmware-3.2.zip

                  Z-Bot CoreXY Build | Thingiverse Profile

                  d0minik96undefined 2 Replies Last reply Reply Quote 0
                  • d0minik96undefined
                    d0minik96 @Phaedrux
                    last edited by

                    @Phaedrux I will test it after installation!

                    1 Reply Last reply Reply Quote 0
                    • Vetiundefined
                      Veti
                      last edited by

                      post your current config

                      d0minik96undefined 1 Reply Last reply Reply Quote 0
                      • d0minik96undefined
                        d0minik96 @Phaedrux
                        last edited by

                        @Phaedrux Reply how long does the installation normally take ? Now i cant connect. Does it save my Networksettings normally ?

                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                        • d0minik96undefined
                          d0minik96 @Veti
                          last edited by

                          @Veti The current config is the one i posted a bit upper in this thread. did not change anything since than and i cant connect to my board due to the update right now

                          1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator @d0minik96
                            last edited by

                            @d0minik96 said in Artillery Genius Duet 2 Wifi Configuration:

                            @Phaedrux Reply how long does the installation normally take ? Now i cant connect. Does it save my Networksettings normally ?

                            WiFi firmware version 1.21RC2

                            I wonder if your wifi firmware was so old that behaviour has changed.

                            You may need to connect with USB terminal to see what is happening. Use M122 to check if the wifi firmware was updated to 1.25.

                            Then use M552 S1 to see if it will enable and connect.
                            Use M587 to see a list of currently saved SSIDs
                            use M588 S"*" to clear all curently saved SSIDs
                            and then use M587 S"networkname" P"password" to readd your SSID

                            Z-Bot CoreXY Build | Thingiverse Profile

                            d0minik96undefined 1 Reply Last reply Reply Quote 0
                            • d0minik96undefined
                              d0minik96 @Phaedrux
                              last edited by

                              @Phaedrux M552 say Wifi is being started. But nothing happens and i cant connect. i have to wait until tomrrow to get my laptop in order to look on the sd card. Can i rescue the system somehow ?

                              Phaedruxundefined 1 Reply Last reply Reply Quote 0
                              • Phaedruxundefined
                                Phaedrux Moderator @d0minik96
                                last edited by

                                @d0minik96 said in Artillery Genius Duet 2 Wifi Configuration:

                                Can i rescue the system somehow ?

                                @Phaedrux said in Artillery Genius Duet 2 Wifi Configuration:

                                You may need to connect with USB terminal to see what is happening.
                                Use M122 to check if the wifi firmware was updated to 1.25.
                                Then use M552 S1 to see if it will enable and connect.
                                Use M587 to see a list of currently saved SSIDs
                                use M588 S"*" to clear all curently saved SSIDs
                                and then use M587 S"networkname" P"password" to readd your SSID

                                Z-Bot CoreXY Build | Thingiverse Profile

                                d0minik96undefined 1 Reply Last reply Reply Quote 0
                                • d0minik96undefined
                                  d0minik96 @Phaedrux
                                  last edited by

                                  @Phaedrux didnt work, guess i have to do a reset tomorrow

                                  1 Reply Last reply Reply Quote 0
                                  • d0minik96undefined
                                    d0minik96
                                    last edited by

                                    So i finally updated the software. It still does not work.

                                    I unplugged my Z and y Motor, so just my x Motor is plugged in.
                                    When i manual move the x axis in the dashboard: x- Axis moves like it should.
                                    When i manual move the z axis in the dashboard (attention!: z Motors are unplugged!!!) : x axis moves aswell. Whats strange is, that in this state the Motor moves kinda slower and there appeared popup that says: response takes 2 long. See console. Console: Warning: motor phase A may be disconnected reported by driver(s) 2
                                    Warning: motor phase B may be disconnected reported by driver(s) 2
                                    ( I think this comes because z Motors are unplugged and it tries to move z Axis aswell.)

                                    If i unplugg my X Motor and only plugg in one z axis: Z axis moves when i move manual z or x axis.

                                    i definitely did not mess up the wiring of the motors. So im sure this is a software issue.
                                    But i must admit my Board is not a original one, so it might be a hardware issue aswell.
                                    I will try to repeat the reprap config tool. maybe i messed up some settings there.... if somebody got a tipp for me what i can check i would be very pleased. My 3d Printer is laying arround on my workbench for a long time now and i finally want to print again :*(

                                    engikeneerundefined 1 Reply Last reply Reply Quote 0
                                    • engikeneerundefined
                                      engikeneer @d0minik96
                                      last edited by

                                      @d0minik96 Looking at your config.g posted above, line 10:

                                      M669 K2                                        ; select CoreXY mode
                                      

                                      That command sets your printer in 'Core XZ' configuration (like core xy, but with x&z). That's why you're getting the weird movement.

                                      I believe the artillery genius is a cartesian (like a prusa?) so you want:

                                      M669 K0 ; set cartesian mode
                                      

                                      For ref: https://duet3d.dozuki.com/Wiki/Gcode#Section_M669_Set_kinematics_type_and_kinematics_parameters

                                      E3D TC with D3Mini and Toolboards.
                                      Home-built CoreXY, Duet Wifi, Chimera direct drive, 2x BMG, 300x300x300 build volume
                                      i3 clone with a bunch of mods

                                      d0minik96undefined 2 Replies Last reply Reply Quote 2
                                      • d0minik96undefined
                                        d0minik96 @engikeneer
                                        last edited by

                                        @engikeneer said in Artillery Genius Duet 2 Wifi Configuration:

                                        M669 K0

                                        Oh man! That's it! It works finally!!!! Thank you so much. I really lost my hope with this conversation!

                                        1 Reply Last reply Reply Quote 1
                                        • d0minik96undefined
                                          d0minik96 @engikeneer
                                          last edited by

                                          @engikeneer still i wonder why core xz is wrong.

                                          i have a Baseplate that moves in y direction . and my extruder is moving in xz direction. ? Can you explain me why kartesian is the setting to take ?

                                          1 Reply Last reply Reply Quote 0
                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            This is coreXZ. It's very different. It's basically a coreXY rotated 90 degrees on it's end.

                                            https://reprap.org/forum/read.php?2,377858

                                            @engikeneer Good eye!

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            1 Reply Last reply Reply Quote 1
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