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    Error: bad Command XXX W/RRF 3.2 and leveling issue

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    • 3DPrintingWorldundefined
      3DPrintingWorld @martin7404
      last edited by

      @martin7404 I guess you would need more power with a little less reduction, I just tried to keep it low as possible incase of a crash. I would turn up the acceleration, that was a typo. Its saves a couple seconds homing.

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      • 3DPrintingWorldundefined
        3DPrintingWorld @martin7404
        last edited by

        @martin7404 so you are saying, if mesh bed is on or off it doesn't make a difference?

        martin7404undefined 1 Reply Last reply Reply Quote 0
        • martin7404undefined
          martin7404
          last edited by

          I just went to PRF 3.2 again and it is the same

          2/16/2021, 1:27:27 PM	G32 bed probe heights: 0.004 -0.006 -0.020, mean -0.007, deviation from mean 0.010
          2/16/2021, 1:27:02 PM	g32
          Leadscrew adjustments made: 0.067 0.023 -0.004, points used 3, (mean, deviation) before (0.032, 0.022) after (-0.000, 0.000)
          2/16/2021, 1:25:25 PM	G32 bed probe heights: 0.040 0.024 0.011, mean 0.025, deviation from mean 0.012
          2/16/2021, 1:25:01 PM	g32
          Leadscrew adjustments made: -0.160 -0.085 -0.057, points used 3, (mean, deviation) before (-0.106, 0.032) after (-0.000, 0.000)
          2/16/2021, 1:15:15 PM	G29
          30 points probed, min error -0.122, max error 0.006, mean -0.044, deviation 0.036
          Height map saved to file 0:/sys/heightmap.csv
          

          Muldex IDEX Duet2+Duex5
          Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
          Sapphire Pro with Duet2, with closed-loop motors
          custom high temp E3D tool changer with Duet2+Duex

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          • 3DPrintingWorldundefined
            3DPrintingWorld @martin7404
            last edited by

            @martin7404 The weight did not have any effect on leveling, It was still out of level. The Z height was .25mm lower but I think that's because the arm that holds the BL touch was flexing from the weight I put on it.

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            • martin7404undefined
              martin7404 @3DPrintingWorld
              last edited by martin7404

              @3DPrintingWorld Yes NO difference if G29 is on or off

              Muldex IDEX Duet2+Duex5
              Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
              Sapphire Pro with Duet2, with closed-loop motors
              custom high temp E3D tool changer with Duet2+Duex

              3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
              • 3DPrintingWorldundefined
                3DPrintingWorld @martin7404
                last edited by

                @martin7404 Is your bed actual level or is it just saying that it is?

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                • martin7404undefined
                  martin7404
                  last edited by

                  Using steel 10.5 gauge and panel due to steps I am within what G29 probing says les than 0.15

                  Muldex IDEX Duet2+Duex5
                  Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                  Sapphire Pro with Duet2, with closed-loop motors
                  custom high temp E3D tool changer with Duet2+Duex

                  3DPrintingWorldundefined 2 Replies Last reply Reply Quote 0
                  • 3DPrintingWorldundefined
                    3DPrintingWorld @martin7404
                    last edited by

                    @martin7404 Ok, not perfect but acceptable. Seems like your configuration is working properly. This about of error could be caused by the head tilting. A second bearing could help with that but would also increase the weight.

                    If you used the same base config as me, I don't understand my issues. I'm thinking about ordering a new board just to see because I don't see how it can be on my end.

                    martin7404undefined 1 Reply Last reply Reply Quote 0
                    • 3DPrintingWorldundefined
                      3DPrintingWorld @martin7404
                      last edited by

                      @martin7404 Instead of two bearings, what about a option to upgrade to the wide series, mgw9h. This should reduce the tilt, and would result in less binding then two bearings mounted on different planes would.
                      mgw9h.png

                      martin7404undefined 1 Reply Last reply Reply Quote 0
                      • martin7404undefined
                        martin7404
                        last edited by martin7404

                        @3DPrintingWorld said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                        mgw9h

                        Yes , but you have to switch to 4020 profile for the X and the mass would not be less
                        I took a look at hiwin pdf's . So LDO rails must light clearance type ZF (4 to 10 microns clearence between block adn rail) so 0.06-0.07 mm on 25 mm cantilever seems normal too. Maybe we can switch to light to slight preload blocks

                        Muldex IDEX Duet2+Duex5
                        Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                        Sapphire Pro with Duet2, with closed-loop motors
                        custom high temp E3D tool changer with Duet2+Duex

                        3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                        • 3DPrintingWorldundefined
                          3DPrintingWorld @martin7404
                          last edited by

                          @martin7404 Why would we have to switch to a 4020? I have not placed it in the model yet but I think it would fit on the 2020 just fine. As you say a preload would be an improvement too, especially considering there is only a single bearing. It would probably will have to get a genuine Hiwini though for a preload option.

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                          • martin7404undefined
                            martin7404
                            last edited by

                            Sorry I missed that 09MGW is a single row of bolts.
                            MGW is better I agree X momentum is about 3 times bigger

                            Muldex IDEX Duet2+Duex5
                            Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                            Sapphire Pro with Duet2, with closed-loop motors
                            custom high temp E3D tool changer with Duet2+Duex

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                            • 3DPrintingWorldundefined
                              3DPrintingWorld @Phaedrux
                              last edited by

                              @Phaedrux There really is not much I can omit from the config as most of it is needed for homing. I can remove heaters, fans, and filament sensors but I don't see how that is going to help.

                              Have you seen any documentation to recover from the firmware being deleted?

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                              • 3DPrintingWorldundefined
                                3DPrintingWorld @Phaedrux
                                last edited by

                                @Phaedrux neverminded, I found fallback procedure 3.

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                                • martin7404undefined
                                  martin7404 @3DPrintingWorld
                                  last edited by

                                  @3DPrintingWorld more likely due to the magnetic mat not flat within 0.15 mm. I tried pushing the X head lightly with my finger during G32, no diference

                                  Muldex IDEX Duet2+Duex5
                                  Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                  Sapphire Pro with Duet2, with closed-loop motors
                                  custom high temp E3D tool changer with Duet2+Duex

                                  1 Reply Last reply Reply Quote 0
                                  • martin7404undefined
                                    martin7404
                                    last edited by martin7404

                                    So found a major problem with Muldex and PRF 3.2
                                    Started a print with T1 ( right , not main extruder) and all of suden the machine is printing in thin air , a few mm up, looked at paneldue and it shows of Z layer + my T1 offset - Z+2.85. Canceled the print.
                                    In manual when I entrer T0 or T1 in the console , both heads come to exact position , measured with 10.5 mm steel gauge .
                                    I do not understan what is hapening . With PRF 3.0 it was printing like a charm
                                    Here is my config

                                    G90                                             ; send absolute coordinates...
                                    M83                                             ; ...but relative extruder moves
                                    M550 P"Muldex"                                  ; set printer name
                                    
                                    
                                    ; Network
                                    M552 S1                                        ; enable network
                                    M586 P0 S1                                      ; enable HTTP
                                    M586 P1 S0                                      ; disable FTP
                                    M586 P2 S0                                      ; disable Telnet
                                    
                                    ; Drives
                                    M569 P0 S0                                      ; X physical drive 0 goes backwards
                                    M569 P1 S0                                      ; Y right physical drive 1 goes backwards
                                    M569 P2 S1                                      ; Y left physical drive 2 goes forwards
                                    M569 P3 S1                                      ; U physical drive 3 goes forwards
                                    M569 P4 S1                                     ; E1 physical drive 4 goes backwards
                                    M569 P5 S1                                      ; Z left physical drive 5 goes backwards
                                    M569 P6 S1                                     ; Z center physical drive 6 goes backwards
                                    M569 P7 S0                                      ; Z right physical drive 7 goes forwards
                                    M569 P8 S1                                      ; E2 physical drive 8 goes forwards
                                    
                                    M584 X0 Y1:2 U3 Z5:6:7 E4:8                     ; set drive mapping
                                    
                                    M350 X16 U16 Y16 Z16 E16:16 I1                                                           ; configure microstepping with interpolation
                                    M92 X199.7 U200 Y199.8:199.8 Z799.2:799.2:799.2 E813.07:830.00                        ; set steps per mm (1760nimble)
                                    M566 X1000.00 U1000.00 Y1000.00:1000.00 Z80.00:80.00:80.00 E100.00:100.00                ; set maximum instantaneous speed changes (mm/min)(Nimble 40)
                                    M203 X12000.00 U12000.00 Y12000.00:12000.00 Z1000.00:1000.00:1000.00 E4200.00:4200.00    ; set maximum speeds (mm/min)
                                    M201 X1310.00 U1310.00 Y1310.00:1310.00 Z35.00:35.00:35.00 E800.00:800.00                    ; set accelerations (mm/s^2)(500)(Nimble 120)
                                    M906 X900 U900 Y900:900 Z900:900:900 E1000:1000 I30                                        ; set motor currents (mA) and motor idle factor in per cent(Nimble 500)
                                    M84 S120                                                                                  ; Set idle timeout
                                    
                                    ; Axis Limits
                                    M208 X-18 Y0 U40 Z0 S1                          ; set axis min - adjust X to align nozzle
                                    M208 X350 U422.7 Y333 Z300 S0                   ; set axis max 
                                    
                                    M669 K0 Y1:-1:0:1				                ; select Markforged Kinematics Y to react with X and U
                                    
                                    ; Endstops
                                    M574 X1 S1 P"xstop"                             ;X axis active high endstop switch
                                    M574 Y2 S1 P"ystop+e1stop"                      ;Y Double max active high endstop switch
                                    ;M574 Y1 S4 ; configure sensorless endstop for low end on Y
                                    M574 U2 S1 P"e0stop"                            ;U axis active high endstop switch
                                    ;M574 Z2 S4
                                    
                                    ;Stall Detection(no used)
                                    ;M574 Y1 S4                                     ; Y axis stall detection
                                    ;M915 P1:9 S3 F1 R0                             ; Y axis stall detection
                                    
                                    ; Z-Probe
                                    M671 X-20.6:200:420.6 Y14.3:333.3:14.3 S10       ; Locations left, center, right          
                                    M950 S0 C"duex.e6heat"                          ; create servo pin 0 for BLTouch
                                    M558 P9 C"zprobe.in+zprobe.mod" H8 F600 A1 T12000   ; set Z probe type to bltouch and the dive height + speeds 
                                    G31 P25 X-29 Y0 Z1.42                           ; set Z probe trigger value, offset and trigger height(lower number farther away)1.8build 1.7glass 
                                    M557 X10:320 Y20:290 S60                       ; probe from X=10 to 390, Y=10 to 290mm with a mesh spacing of 20mm
                                    
                                    ; Heaters
                                    M308 S0 P"bedtemp" Y"thermistor" T100000 B4534 C9.565227e-8      ; configure sensor 0 as thermistor on pin bedtemp
                                    M950 H0 C"bedheat" T0                                            ; create bed heater output on bedheat and map it to sensor 0
                                    M143 H0 S120                                                     ; set temperature limit for heater 0 to 120C
                                    M307 H0 B0 S1.00                                                 ; disable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0                                                          ; map heated bed to heater 0
                                    M308 S1 P"e0temp" Y"thermistor" T100000 B4725 C0 R4700  ; configure sensor 1 as thermistor on pin e0temp
                                    M950 H1 C"e0heat" T1                                             ; create nozzle heater output on e0heat and map it to sensor 1
                                    M143 H1 S280                                                     ; set temperature limit for heater 1 to 280C
                                    M307 H1 B0 S1.00                                                 ; disable bang-bang mode for heater  and set PWM limit
                                    M308 S2 P"e1temp" Y"thermistor" T100000 B4725 C0 R4700 ; configure sensor 2 as thermistor on pin e1temp
                                    M950 H2 C"e1heat" T2                                             ; create nozzle heater output on e1heat and map it to sensor 2
                                    M143 H2 S280                                                     ; set temperature limit for heater 2 to 280C
                                    M307 H2 B0 S1.00                                                 ; disable bang-bang mode for heater  and set PWM limit
                                    
                                    ; Fans
                                    M950 F0 C"fan0" Q500                             ; create fan 0 on pin fan0 and set its frequency
                                    M106 P0 S0 H-1                               ; set fan 0 value. Thermostatic control is turned off
                                    M950 F1 C"fan1" Q500                             ; create fan 1 on pin fan1 and set its frequency
                                    M106 P1 S1 H1 T45                                ; set fan 1 value. Thermostatic control is turned on
                                    M950 F2 C"fan2" Q500                             ; create fan 2 on pin fan2 and set its frequency
                                    M106 P2 S0 H-1                                   ; set fan 2 value. Thermostatic control is turned off
                                    M950 F3 C"duex.fan8" Q500                        ; create fan 3 on pin duex.fan8 and set its frequency
                                    M106 P3 S1 H2 T45                                ; set fan 3 value. Thermostatic control is turned on
                                    
                                    ; LEDs
                                    M950 F4 C"duex.fan6" ;Q500                       ; create LED 4 on pin duex.fan6 and set its frequency
                                    M106 P4 S128 H-1                                 ; set LED 4 value. Thermostatic control is turned OFF
                                    M950 F5 C"duex.fan7" ;Q500                       ; create LED 5 on pin duex.fan7 and set its frequency
                                    M106 P5 S128 H-1                                 ; set LED 5 value. Thermostatic control is turned OFF
                                    
                                    ; Tools
                                    M563 P0 D0 H1 F0 S"Left"                         ; define tool 0 Left 
                                    G10 P0 X0 Y0 Z0                                  ; set tool 0 axis offsets y was .45
                                    G10 P0 R0 S0                                     ; set initial tool 0 active and standby temperatures to 0C
                                    
                                    M563 P1 D1 H2 X3 F2 S"Right"                     ; define tool 1 Right
                                    G10 P1 X0 Y0 Z2.55                          ; set tool 1 axis offsets - adjust Y to alignn nozzle
                                    G10 P1 R0 S0                                     ; set initial tool 1 active and standby temperatures to 0C
                                    
                                    M563 P2 D0:1 H1:2 X0:3 F0:2 S"Copy"              ; define tool 2 Copy
                                    G10 P2 X90 Y0 U-90 S0 R0                         ; set tool 2 axis offsets (WAS 105)
                                    M567 P2 E1:1         
                                    M568 P2 S1 ; turn on mixing for tool 2           ; set mix ratio 100% on both extruders
                                    ;G10 L1 P1 X0.0 Y0.0 Z2.55
                                    
                                    M501                                             ; Record
                                    M593 F66.6
                                    
                                    M575 P1 S1 B57600                                ;Panel due 
                                    ;G92 Z150
                                    ;G91
                                    ;G1 Z0.1 f100
                                    ;G90
                                    

                                    There is more , while printing in the air I pushed baybysteping up to - 2.5 , as a result the Z on panel due become almost +6 mm and the nozzle was still printing in air

                                    Muldex IDEX Duet2+Duex5
                                    Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                    Sapphire Pro with Duet2, with closed-loop motors
                                    custom high temp E3D tool changer with Duet2+Duex

                                    3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                                    • 3DPrintingWorldundefined
                                      3DPrintingWorld @martin7404
                                      last edited by 3DPrintingWorld

                                      @martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                                      It's because you have a offset of "Z2.55" On the U axis tool for some reason.

                                      M563 P1 D1 H2 X3 F2 S"Right"                     ; define tool 1 Right
                                      G10 P1 X0 Y0 Z2.55                          ; set tool 1 axis offsets - adjust Y to alignn nozzle
                                      G10 P1 R0 S0                                     ; set initial tool 1 active and standby temperatures to 0C
                                      

                                      Not sure why it was the same when you tried it manually.

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                                      • martin7404undefined
                                        martin7404
                                        last edited by

                                        My left tool head is V6 and is 2.55 mm different from the copperhead

                                        Muldex IDEX Duet2+Duex5
                                        Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                        Sapphire Pro with Duet2, with closed-loop motors
                                        custom high temp E3D tool changer with Duet2+Duex

                                        3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                                        • martin7404undefined
                                          martin7404
                                          last edited by martin7404

                                          Just revert back to PRG 3.1.1 and it is the same
                                          Start print the head (T1) prints on Z 2.55 on the screen of DWC and is about 2.55 in the air. So just like there are 2 offsets applied one over the other,
                                          One of them is just like you made it in the slicer.
                                          One more thing using babysteps it changes the dimension on the DWC screen If I do - babysteps the screen Z goes up . It is the same with PRF3.1.1 and 3.2

                                          Muldex IDEX Duet2+Duex5
                                          Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                          Sapphire Pro with Duet2, with closed-loop motors
                                          custom high temp E3D tool changer with Duet2+Duex

                                          3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                                          • 3DPrintingWorldundefined
                                            3DPrintingWorld @martin7404
                                            last edited by

                                            @martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                                            My left tool head is V6 and is 2.55 mm different from the copperhead

                                            oh, sorry I forgot that you had one V6.

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