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    Strange bugs 3.3beta2

    Scheduled Pinned Locked Moved Unsolved
    Beta Firmware
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    • dc42undefined
      dc42 administrators
      last edited by

      Run M122 and check that it reports "Bed compensation in use: mesh" while it is printing.

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

      Depundefined 1 Reply Last reply Reply Quote 0
      • Depundefined
        Dep @dc42
        last edited by Dep

        @dc42
        I usually do that.

        The size of the table at the printer is 1x1 meter. And the unevenness is about 0.5mm. I usually see the Z motors move.

        Should I try to install an older firmware? Or does everything work for you?

        1 Reply Last reply Reply Quote 0
        • Depundefined
          Dep
          last edited by

          Another dangerous bug!

          M558 K0 H5 A5 F120
          Works as it should

          M558 K0 H5 A5 F120: 120
          Also works as it should

          M558 K0 H5 A5 F120: 60
          Broke today probe.
          The bed goes up and breaks the probe. And continue to rise.

          I checked it several times.

          Phaedruxundefined dc42undefined 2 Replies Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @Dep
            last edited by Phaedrux

            @Dep said in Strange bugs 3.3beta2:

            M558 K0 H5 A5 F120: 60
            Broke today probe.

            Why would you use F120: 60 at all?

            To better understand why the mesh isn't moving the Z axis please provide your config.g and homing files so we can see what other commands are taking affect.

            Z-Bot CoreXY Build | Thingiverse Profile

            Depundefined 1 Reply Last reply Reply Quote 0
            • Depundefined
              Dep @Phaedrux
              last edited by Dep

              @Phaedrux thanks!

              Below is my config:

              ; Configuration file for Duet 3 (firmware version 3)
              ; executed by the firmware on start-up
              
              ; General preferences
              G90                                             ; send absolute coordinates...
              M83                                             ; ...but relative extruder moves
              M550 P"Pr-1100x1100"                               ; set printer name
              M575 P1 B57600 S1       						; Comms parameters for PanelDue
              M564 S1 H1              						; Forbid axis movements when not homed
              
              ; Network
              M552 P0.0.0.0 S1                                 ; enable network and acquire dynamic address via DHCP
              M586 P0 S1                                       ; enable HTTP
              M586 P1 S0                                       ; disable FTP
              M586 P2 S0                                       ; disable Telnet
              
              
              ; Drives
              M569 P0.0 S0                                     ; X drive goes back
              M569 P0.1 S1                                     ; Z1 drive
              M569 P0.2 S0                                     ; Z2 drive
              M569 P0.3 S1                                     ; Z3 drive
              M569 P0.4 S0                                     ; Z4 drive
              M569 P0.5 S0                                     ; Y drive
              G4 P500											; Pause for toolboards init
              M569 P21.0 S1                                   ; Extruder 1 (T0)
              M569 P1.1 S0                                    ; Extruder 1 spool driver
              M569 P22.0 S1                                   ; Extruder 2 (T1)
              M569 P1.2 S0                                   ; Extruder 2 spool driver
              M569 P1.0 S1                                   ; Coupler
              
              M584 X0.0 Y0.5 Z0.1:0.2:0.3:0.4 C1.0        ; set Move drive mapping
              M584 E21.0:1.1:22.0:1.2                    ; set Extruder drive mapping
              
              ; Axis Limits
              M208 Z-4:875 C0:500
              M208 X-570:570 Y-630:500
              
              ; Define the bed mounting coordinates
              M671 X-473:473:473:-473 Y730:730:-735:-735 S10 ;Snn Maximum correction allowed for each leadscrew in mm (optional, default 1.0)
              
              ; Endstops
              M574 X1 S1 P"!io1.in"                           ; configure active-high endstop for high end on X via pin !io1.in
              M574 Y2 S1 P"!io2.in"                           ; configure active-high endstop for low end on Y via pin !io2.in
              M574 Z0 P"nil"									; no endstop on Z
              M574 C1 S3										; Stall detect coupler at low end of its range
              
              ;Steps per mm = (Motor Steps per Revolution * Driver Microstep) / (Belt Pitch * Pully Number of Teeth)
              ; X: GT2-20 / Y: HTD3-20 * (48/16) / Z: HTD5-20 * 6
              M92 X80 Y160 Z800 C200 					; set steps per mm
              M92 E420.00:115.00:420.00:115.00 				; set steps per mm
              
              M350 X16 Y16 Z16 E16:16 I1                       ; configure microstepping with interpolation
              M350 C16 I1
              
              M566 X420 Y420 Z8 C2 E200:200:200:200			; Set maximum instantaneous speed changes (mm/min)
              M203 X9000.00 Y9000.00 Z600.00 C10000 E6000.00 	; set maximum speeds (mm/min)
              M201 X1200.00 Y1200.00 Z100.00 C500 E2500       	; set accelerations (mm/s^2)
              M204 P250 T1200										; Travel and print acceleration
              
              M906 X1200 Y1600 Z2400 C500 E900:900:900:900	 	; set motor currents (mA) and motor idle factor in per cent
              M913 C50 											
              M906 I30
              
              M913 E100:0:100:0									; set Working current to Extruders
              M84 S120                                       		; Set idle timeout
              
              ;Stall Detection
              M915 C S5 F0 H200 					; Coupler
              
              ; Calibrate Nozzle Height probe
              M558 K1 P8 B0 C"^io8.in" H30 F120 T9000
              
              ; Z-Probe
              M558 K0 P5 B1 C"^io7.in" H5 A5 F120 T9000			; set Z probe type to switch and the dive height + speeds
              G31 K0 X0 Y0 Z0 P1000                            	; set Z probe trigger value, offset and trigger height
              M557 X-500:500 Y-500:500 S100                       ; define mesh grid
              
              
              ; ==== Heaters ====
              ; Bed
              M308 S0 P"temp0" Y"thermistor" T100000 B3950     	; configure sensor 0 as thermistor on pin temp0
              ;M950 H0 C"out0" T0                             	; create bed heater output on out0 and map it to sensor 0
              M950 H0 C"out0" T0 Q10         						; Heater --> SSD-Steuerung
              ;M307 H0 B0 S0.80                                 	; disable bang-bang mode for the bed heater and set PWM limit
              ;M307 H0 R0.425 C261.3 D4.03 S0.80				; Tuned
              M307 H0 R0.191 C560.9 D3.56 S1.00 V24.1
              M140 H0                                          ; map heated bed to heater 0
              M143 H0 S120                                     ; set temperature limit for heater 0 to 120C
              
              ; Chamber
              M308 S5 P"temp1" Y"thermistor" T100000 B4138  ; configure sensor 5 as thermistor on pin temp1
              M950 H5 C"out9" T5 Q10                          ; create chamber heater output on temp1 and map it to sensor 5
              M307 H5 R1.000 C30.9 D9.18 S1.00 V24.1 		; Tuned
              M141 H5                                       ; map chamber to heater 5
              M143 H5 S75                                   ; set temperature limit for heater
              M950 F5 C"out4" Q500                          ; cooling fan
              M106 P5 S0 H-1 C"Filament FAN" 					; Control be trigger2
              ;M106 P5 S1 H5 T22:60                          	; thermistatic control
              
              M950 J8 C"0.io6.in"							; Input 8 for filament Fan
              M581 T2 P8 S1 R0							; Invoke trigger 2 when an inactive-to-active edge is detected on input 8
              
              ; Extruder 1
              M308 S1 P"21.temp0" Y"thermistor" T100000 B4725 ; configure sensor 1 as thermistor on pin 121.temp0
              M950 H1 C"21.out0" T1                           ; create nozzle heater output on 121.out0 and map it to sensor 1
              M307 H1 B0 S1.00                                ; disable bang-bang mode for heater  and set PWM limit
              M143 H1 S285                                    ; set temperature limit for heater 1 to 285C
              ;M307 H1 R3.214 C42.3 D7.77 S0.75 V23.2 		; Tuned
              M307 H1 R0.056 C194.7 D8.90 S1.00 V23.9		; small block
              ;M307 H1 R3.358 C190.6 D7.20 S0.60 V23.6
              
              ; Extruder 2
              M308 S2 P"22.temp0" Y"thermistor" T100000 B4725 ; configure sensor 2 as thermistor on pin 122.temp0
              M950 H2 C"22.out0" T2                           ; create nozzle heater output on 122.out0 and map it to sensor 2
              M307 H2 B0 S1.00                                ; disable bang-bang mode for heater  and set PWM limit
              M143 H2 S285                                    ; set temperature limit for heater 2 to 285C
              ;M307 H2 R3.056 C229.5 D7.91 S0.80 V23.3 		; Tuned
              ;M307 H2 R3.090 C199.8 D7.36 S0.75 V23.3
              ;M307 H2 R3.202 C234.301:234.301 D7.52 S0.70 V23.3 B0 I0
              M307 H2 R3.358 C190.6 D7.20 S0.60 V23.6
              
              ; *** Fans
              ; Extruder 1 Fan
              M950 F0 C"21.out1" Q500                         ; Part cooling fan
              M106 P0 S0 B0.1 H-1                             ; Default off. booststart for 0.1s (B0.1); thermostatic control off 
              
              M950 F1 C"21.out2" Q500                         ; Hotend cooling fan
              M106 P1 S1 H1 T50                            	; Default on. thermistatic control on above 50C
              
              ; Extruder 2 Fan
              M950 F2 C"22.out1" Q500                         ; Part cooling fan
              M106 P2 S0 B0.1 H-1                             ; Default off. booststart for 0.1s (B0.1); thermostatic control off 
              
              M950 F3 C"22.out2" Q500                         ; Hotend cooling fan
              M106 P3 S0 H2 T50                            	; Default on. thermistatic control on above 50C
              
              ; Tools
              ; Extruder 1 Tool
              M563 P0 S"Extruder-1" D0:1 H1 F0
              M567 P0 E1:1									; mixing
              G10 P0 R0 S0                                    ; set initial tool 0 active and standby temperatures to 0C
              G10 P0 X0 Y76 Z0 								; Reset tool axis offsets
              
              ; Extruder 2 Tool
              M563 P1 S"Extruder-2" D2:3 H2 F2 				; define tool 1
              M567 P1 E1:1									; mixing
              G10 P1 R0 S0                                    ; set initial tool 1 active and standby temperatures to 0C
              G10 P1 X0 Y76 Z0 								; Reset tool axis offsets
              
              ; Retraction
              ;M207 S6.5 R0.0 F4800 T4800 Z0.0
              M207 S4 R0.0 F3000 T2100 Z0.4 		
              
              	; M207: Set retract length
              	; Parameters
                  ; 	Pn Tool number (optional, supported in RRF 3.01 and later only)
              	; 	Snnn positive length to retract, in mm
              	; 	Rnnn positive or negative additional length to un-retract, in mm, default zero
              	; 	Fnnn retraction feedrate, in mm/min
              	; 	Tnnn feedrate for un-retraction if different from retraction, mm/min (RepRapFirmware 1.16 and later only)
              	; 	Znnn additional zlift/hop
              	; Example: M207 S4.0 F2400 Z0.075
              
              ; FEEDRATE CONVERSIONS
              	; 20mm/s = F1200	; 100mm/s = F6000
              	; 35mm/s = F2100	; 120mm/s = F7200
              	; 50mm/s = F3000	; 133mm/s = F8000
              	; 70mm/s = F4200
              
              
              ; * ======= tool offsets ======== *
              ; Set in config-override.g
              ;G10 P0 X0 Y76 Z-21					; T0
              ;G10 P1 X0 Y76 Z-21					; T1
              
              ; Filament monitors
              ;  ** Rotating
              M591 P3 C"21.io1.in" D0 R30:160 S1
              M591 P3 C"22.io1.in" D2 R30:160 S1
              ;  ** Endstops
              M950 J4 C"!^1.io1.in"		; Input 4 for filament trigger
              M950 J5 C"!^1.io2.in"		; Input 5 for filament trigger
              ; Invoke trigger 1 (M25) when an active-to-inactive edge is detected on input 4 and 5 and a file is being printed from SD card
              M581 T1 P4 S0 R1		
              M581 T1 P5 S0 R1		
              
              ; Miscellaneous
              M572 D0 S0.02 							; pressure advance T0
              M572 D1 S0.02 							; pressure advance T1
              ;M572 D2 S0.05 							; pressure advance T2
              ;M572 D3 S0.05 							; pressure advance T3
              
              ; Set up the dock indicator switches on the tools. 
              M950 J0 C"!^io3.in"					; GpIn 3 = tool 0 dock switch
              M950 J1 C"!^io4.in"					; GpIn 4 = tool 1 dock switch
              
              ; Z Motors brake
              M950 P0 C"0.out1"
              
              ; Z Motors brake OFF
              G92 Z0
              G91 					; Relative mode
              M400 					; make sure everything has stopped before we change the motor currents
              M913 Z100	 			; drop motor currents to 20%
              G1 Z0.05
              M400
              G4 P1000								; Pause 
              M42 P0 S1 								; Brake oFF
              M911 S23.5 R23.8 P"M42 P0 S0"
              G90
              
              ;M593 F50							; cancel ringing at 50Hz 
              M376 H20							; bed compensation taper
              
              M501                                ; load saved parameters from non-volatile memory
              ;G29 S1 							; Do not use G29 S1 within config.g, because no Z=0 datum has been established at that point
              G90						; !!! absolute positioning
              

              homez:

              ; homez.g
              ; called to home the Z axis
              
              while iterations < 2
                if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
                  M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
                  abort
              
              ;M290 R0 S0 ; clear babystepping
              ;M561 ; clear any bed transform
              
              G91 					; Relative mode
              M400 					; make sure everything has stopped before we change the motor currents
              ;M913 Z80	 			; drop motor currents to 20%
              G1 H2 Z5 F1000			; Lower the bed
              ;M913 Z100	 			; motor currents to 100%
              G90						; back to absolute positioning
              
              ;G1 X0 Y0 F9000			; Position the endstop above the bed centre
              G1 X-473 Y500 F9000		; Position the endstop near leadscrew
              ;G1 X473 Y500 F9000		; Position for test
              M400
              
              ;if move.axes[2].machinePosition > 9
              ;	M558 K0 F1000 H3
              ;	G30 Z-9999
              
              M558 K0 F600 H5 A1
              G30 Z-9999
              M558 K0 F120 H5 A5
              G30 Z-9999
              M400
              ;M558 K0 H30
              
              ;G91 				; Relative mode
              ;G1 Z10 F1000			; Lower the bed
              ;G90				; back to absolute positioning
              

              bed.g (called from homeall.g)

              ; bed.g
              ; Called to align the gantry to the bed plane via G32
              
              while iterations < 2
                if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
                  M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
                  abort
              
              M290 R0 S0 				; clear babystepping
              M561 					; clear any bed transform
              M84 E0:1				; Turn off noisy Extruder motor
              M400 					; make sure everything has stopped
              
              M98 P"homez.g"
              
              M558 K0 H10 F120			; F120
              M98 P"/macros/Move/bed_level_points"
              ;M98 P"homez.g"
              ;G28 Z
              
              ;G1 X0 Y0 F12000		; Position the endstop above the bed centre
              ;M558 F120
              ;G30 Z-9999
              ;M400
              
              M98 P"homez.g" 
              M558 K0 H5
              

              mesh.g

              ; mesh.g
              if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed || !move.axes[3].homed
              	M291 S1 T5 P{"Please Home before probe"} R"Cannot probe"
              	abort
              
              if state.currentTool != -1
              	M291 S1 T5 P{"Please return All tools to dock before probing"} R"Cannot probe"
              	abort "Cannot do mesh probing when a tool is selected"
              
              M290 R0 S0 				; clear babystepping
              M561 					; clear any bed transform
              
              ;G32						; Level the gantry
              ;M98 P"homez.g"
              
              ; Heat the bed to 80C
              ;M291 P"Heating up the bed..." R"Probing New Bed Mesh" T5
              ;M190 S80
              ;M116
              
              ;G32						; Level the gantry again while everything is hot
              
              M558 K0 H3 T9000 F120 A5
              G29 S0
              M558 K0 H5 T9000
              
              M140 S0 				; Turn off bed
              M291 P"Done!" R"Bed Mesh" T5
              

              homeall.g (G29 S1 here)

              ; homeall.g
              ; called to home all axes
              ;
              M98 P"homex.g"
              M98 P"homey.g"
              M98 P"bed.g"
              G29 S1
              
              1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                @Dep said in Strange bugs 3.3beta2:

                M98 P"/macros/Move/bed_level_points"

                What's in that macro?

                @Dep said in Strange bugs 3.3beta2:

                M98 P"homex.g" M98 P"homey.g"

                Can you share these as well?

                Can you also share the results of sending M98 P"config.g" and share your slicer start gcode.

                Z-Bot CoreXY Build | Thingiverse Profile

                Depundefined 1 Reply Last reply Reply Quote 0
                • Depundefined
                  Dep @Phaedrux
                  last edited by

                  @Phaedrux оf course

                  bed_level_points :

                  G30 P0 X-473 Y500 Z-99999 ;P0 - Probe point 0 (not drive)
                  G30 P1 X473 Y500 Z-99999
                  G30 P2 X473 Y-500 Z-99999
                  G30 P3 X-473 Y-500 Z-99999 S4 ;set correction
                  

                  homex.g

                  ; homex.g
                  ; called to home the X axis
                  ;
                  
                  while iterations < 2
                    if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
                      M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
                      abort
                  
                  
                  G91              	; relative positioning
                  M400 				; make sure everything has stopped before we change the motor currents
                  ;M913 Z80	 		; drop motor currents to 20%
                  G1 H2 Z5 F6000 		; lift Z relative to current position
                  ;M913 Z100	 		; motor currents to 100%
                  G1 H1 X-1200 F6000 	; move quickly to X axis endstop and stop there (first pass)
                  G1 H2 X5 F6000  	; go back a few mm
                  G1 H1 X-1200 F360  	; move slowly to X axis endstop once more (second pass)
                  G1 H2 X5 F6000 	; move away from end
                  G1 H2 Z-5 F6000  	; up Z again
                  G90              	; absolute positioning
                  

                  homey.g

                  ; homey.g
                  ; called to home the Y axis
                  ;
                  
                  while iterations < 2
                    if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
                      M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
                      abort
                  
                  if !move.axes[0].homed 
                        M98 P"homex.g"
                  
                  G91                ; relative positioning
                  M400 				; make sure everything has stopped before we change the motor currents
                  ;M913 Z80	 		; drop motor currents to 20%
                  G1 H2 Z5 F6000 		; lift Z relative to current position
                  ;M913 Z100	 		; motor currents to 100%
                  G1 H1 Y1205 F6000  ; move quickly to Y axis endstop and stop there (first pass)
                  G1 H2 Y-5 F6000      ; go back a few mm
                  G1 H1 Y1205 F360   ; move slowly to Y axis endstop once more (second pass)
                  G1 H2 Y-50 F6000  	; move away from end
                  G1 H2 Z-5 F6000     ; up Z again
                  G90                 ; absolute positioning
                  

                  Slicer (S3D) start code:

                  ; START code
                  M140 S[bed0_temperature]
                  M106 S0 ;fan off
                  G92 E0; reset extruder distance
                  G28
                  T0 ; Select tool 0
                  M116
                  G10 P0 S[extruder0_temperature] R160
                  M116
                  M98 P"/macros/Purge Filament"
                  ;---  end start gcode ---
                  
                  1 Reply Last reply Reply Quote 0
                  • Depundefined
                    Dep
                    last edited by Dep

                    @Phaedrux said in Strange bugs 3.3beta2:

                    M98 P"config.g"

                    18.03.2021, 22:24:45	M98 P"config.g"
                    HTTP is enabled on port 80
                    FTP is disabled
                    TELNET is disabled
                    
                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      @Dep said in Strange bugs 3.3beta2:

                      M376 H20 ; bed compensation taper

                      With a taper set the amount moved to compensate is diminished over the duration of the print and for small amounts can make it very hard to see.

                      Can you post a screenshot showing your heightmap?

                      How often do you re-create the heightmap?

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Depundefined 1 Reply Last reply Reply Quote 0
                      • Depundefined
                        Dep
                        last edited by

                        2021-03-19_13-09-59.png

                        I've done it many times. The print shows that the compensation does not work. I also attach a long stick to the pulley to check if there is movement or not.

                        If necessary, I can shoot a video.

                        1 Reply Last reply Reply Quote 0
                        • Depundefined
                          Dep @Phaedrux
                          last edited by

                          @Phaedrux said in Strange bugs 3.3beta2:

                          @Dep said in Strange bugs 3.3beta2:

                          M376 H20 ; bed compensation taper

                          With a taper set the amount moved to compensate is diminished over the duration of the print and for small amounts can make it very hard to see.

                          I've tried disabling taper. M376 H0
                          Nothing changes.

                          1 Reply Last reply Reply Quote 0
                          • jay_s_ukundefined
                            jay_s_uk
                            last edited by

                            add G29 S1 after the G28 in your start script

                            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                            Depundefined 1 Reply Last reply Reply Quote 0
                            • Depundefined
                              Dep @jay_s_uk
                              last edited by

                              @jay_s_uk It is added:

                              homeall.g (G29 S1 here)

                              ; homeall.g
                              ; called to home all axes
                              ;
                              M98 P"homex.g"
                              M98 P"homey.g"
                              M98 P"bed.g"
                              G29 S1
                              
                              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                              • jay_s_ukundefined
                                jay_s_uk @Dep
                                last edited by

                                @Dep ah, missed that

                                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                1 Reply Last reply Reply Quote 0
                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  All I can think is that the conditional gcode in your homing files is skipping something.

                                  Can you try adding G29 S1 to your slicer start gcode after the purge filament macro?

                                  Then check if mesh compensation is active in M122 during the print and see if the Z axis is moving.

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  1 Reply Last reply Reply Quote 0
                                  • OwenDundefined
                                    OwenD
                                    last edited by

                                    Could it be that you're not homing Z after you run bed.g ?

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • Phaedruxundefined
                                      Phaedrux Moderator @OwenD
                                      last edited by

                                      @OwenD said in Strange bugs 3.3beta2:

                                      Could it be that you're not homing Z after you run bed.g ?

                                      Bed.g is getting called as part of homeall. bed.g calls homez.

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      1 Reply Last reply Reply Quote 0
                                      • Depundefined
                                        Dep
                                        last edited by

                                        The oddities continue. Now there is a problem with the filament monitor: min -5% and printing continues:

                                        20.03.2021, 10:39:40	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.37mm/rev, min -5% max 105% over 153582.5mm
                                        20.03.2021, 10:32:45	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 151673.8mm
                                        20.03.2021, 10:25:49	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 149761.4mm
                                        20.03.2021, 10:22:38	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148885.3mm
                                        20.03.2021, 10:21:55	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148686.4mm
                                        20.03.2021, 10:21:18	M591 d0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148515.8mm
                                        

                                        After the "reset":

                                        20.03.2021, 10:52:50	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.51mm/rev, min 97% max 104% over 2092.2mm
                                        20.03.2021, 10:50:15	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.51mm/rev, min 97% max 104% over 1380.5mm
                                        20.03.2021, 10:48:02	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.53mm/rev, min 97% max 104% over 766.6mm
                                        20.03.2021, 10:47:35	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.54mm/rev, min 97% max 104% over 644.5mm
                                        20.03.2021, 10:45:52	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.57mm/rev, min 97% max 104% over 171.1mm
                                        20.03.2021, 10:45:22	M591 D0
                                        Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.57mm/rev, min 97% max 101% over 26.5mm
                                        20.03.2021, 10:45:02	M292
                                        Printing paused at X-21.7 Y-33.3 Z2.5 C40.0
                                        20.03.2021, 10:44:51	Resume state saved
                                        20.03.2021, 10:44:24	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:44:14	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:43:53	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:43:39	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:43:19	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:42:57	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:42:43	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:42:34	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:42:31	M591 d0 s1
                                        20.03.2021, 10:42:24	M591 d0
                                        Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, disabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                        20.03.2021, 10:42:21	M591 d0 s0
                                        

                                        All settings are higher in this thread.

                                        I ran 170 hours long print. I should have tried to install the old firmware, something is wrong here 😞

                                        And a couple of screenshots to tread:
                                        IMG_3010.jpg
                                        IMG_3013.jpg

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                                        • Depundefined
                                          Dep
                                          last edited by

                                          And I already had it. But at that moment
                                          I had one of the extruders disabled on the CAN bus and errors were pouring in. I thought it was because of this.

                                          Last time min was -107% the extruder ended up stuck, but the printer kept printing in air all night.

                                          In general, the filament monitor does not work on this firmware.

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                                          • Depundefined
                                            Dep
                                            last edited by

                                            I installed 3.2.2 firmware - the errors disappeared, the mesh is working, the filament monitor is working.

                                            The printer is printing 5 hours, the flight is normal. So pay attention to what I wrote above.

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