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Strange bugs 3.3beta2

Scheduled Pinned Locked Moved Unsolved
Beta Firmware
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  • undefined
    Phaedrux Moderator @Dep
    last edited by Phaedrux 17 Mar 2021, 16:12

    @Dep said in Strange bugs 3.3beta2:

    M558 K0 H5 A5 F120: 60
    Broke today probe.

    Why would you use F120: 60 at all?

    To better understand why the mesh isn't moving the Z axis please provide your config.g and homing files so we can see what other commands are taking affect.

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 1 Reply Last reply 18 Mar 2021, 16:50 Reply Quote 0
    • undefined
      Dep @Phaedrux
      last edited by Dep 18 Mar 2021, 16:50

      @Phaedrux thanks!

      Below is my config:

      ; Configuration file for Duet 3 (firmware version 3)
      ; executed by the firmware on start-up
      ; General preferences
      G90 ; send absolute coordinates...
      M83 ; ...but relative extruder moves
      M550 P"Pr-1100x1100" ; set printer name
      M575 P1 B57600 S1 ; Comms parameters for PanelDue
      M564 S1 H1 ; Forbid axis movements when not homed
      ; Network
      M552 P0.0.0.0 S1 ; enable network and acquire dynamic address via DHCP
      M586 P0 S1 ; enable HTTP
      M586 P1 S0 ; disable FTP
      M586 P2 S0 ; disable Telnet
      ; Drives
      M569 P0.0 S0 ; X drive goes back
      M569 P0.1 S1 ; Z1 drive
      M569 P0.2 S0 ; Z2 drive
      M569 P0.3 S1 ; Z3 drive
      M569 P0.4 S0 ; Z4 drive
      M569 P0.5 S0 ; Y drive
      G4 P500 ; Pause for toolboards init
      M569 P21.0 S1 ; Extruder 1 (T0)
      M569 P1.1 S0 ; Extruder 1 spool driver
      M569 P22.0 S1 ; Extruder 2 (T1)
      M569 P1.2 S0 ; Extruder 2 spool driver
      M569 P1.0 S1 ; Coupler
      M584 X0.0 Y0.5 Z0.1:0.2:0.3:0.4 C1.0 ; set Move drive mapping
      M584 E21.0:1.1:22.0:1.2 ; set Extruder drive mapping
      ; Axis Limits
      M208 Z-4:875 C0:500
      M208 X-570:570 Y-630:500
      ; Define the bed mounting coordinates
      M671 X-473:473:473:-473 Y730:730:-735:-735 S10 ;Snn Maximum correction allowed for each leadscrew in mm (optional, default 1.0)
      ; Endstops
      M574 X1 S1 P"!io1.in" ; configure active-high endstop for high end on X via pin !io1.in
      M574 Y2 S1 P"!io2.in" ; configure active-high endstop for low end on Y via pin !io2.in
      M574 Z0 P"nil" ; no endstop on Z
      M574 C1 S3 ; Stall detect coupler at low end of its range
      ;Steps per mm = (Motor Steps per Revolution * Driver Microstep) / (Belt Pitch * Pully Number of Teeth)
      ; X: GT2-20 / Y: HTD3-20 * (48/16) / Z: HTD5-20 * 6
      M92 X80 Y160 Z800 C200 ; set steps per mm
      M92 E420.00:115.00:420.00:115.00 ; set steps per mm
      M350 X16 Y16 Z16 E16:16 I1 ; configure microstepping with interpolation
      M350 C16 I1
      M566 X420 Y420 Z8 C2 E200:200:200:200 ; Set maximum instantaneous speed changes (mm/min)
      M203 X9000.00 Y9000.00 Z600.00 C10000 E6000.00 ; set maximum speeds (mm/min)
      M201 X1200.00 Y1200.00 Z100.00 C500 E2500 ; set accelerations (mm/s^2)
      M204 P250 T1200 ; Travel and print acceleration
      M906 X1200 Y1600 Z2400 C500 E900:900:900:900 ; set motor currents (mA) and motor idle factor in per cent
      M913 C50
      M906 I30
      M913 E100:0:100:0 ; set Working current to Extruders
      M84 S120 ; Set idle timeout
      ;Stall Detection
      M915 C S5 F0 H200 ; Coupler
      ; Calibrate Nozzle Height probe
      M558 K1 P8 B0 C"^io8.in" H30 F120 T9000
      ; Z-Probe
      M558 K0 P5 B1 C"^io7.in" H5 A5 F120 T9000 ; set Z probe type to switch and the dive height + speeds
      G31 K0 X0 Y0 Z0 P1000 ; set Z probe trigger value, offset and trigger height
      M557 X-500:500 Y-500:500 S100 ; define mesh grid
      ; ==== Heaters ====
      ; Bed
      M308 S0 P"temp0" Y"thermistor" T100000 B3950 ; configure sensor 0 as thermistor on pin temp0
      ;M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
      M950 H0 C"out0" T0 Q10 ; Heater --> SSD-Steuerung
      ;M307 H0 B0 S0.80 ; disable bang-bang mode for the bed heater and set PWM limit
      ;M307 H0 R0.425 C261.3 D4.03 S0.80 ; Tuned
      M307 H0 R0.191 C560.9 D3.56 S1.00 V24.1
      M140 H0 ; map heated bed to heater 0
      M143 H0 S120 ; set temperature limit for heater 0 to 120C
      ; Chamber
      M308 S5 P"temp1" Y"thermistor" T100000 B4138 ; configure sensor 5 as thermistor on pin temp1
      M950 H5 C"out9" T5 Q10 ; create chamber heater output on temp1 and map it to sensor 5
      M307 H5 R1.000 C30.9 D9.18 S1.00 V24.1 ; Tuned
      M141 H5 ; map chamber to heater 5
      M143 H5 S75 ; set temperature limit for heater
      M950 F5 C"out4" Q500 ; cooling fan
      M106 P5 S0 H-1 C"Filament FAN" ; Control be trigger2
      ;M106 P5 S1 H5 T22:60 ; thermistatic control
      M950 J8 C"0.io6.in" ; Input 8 for filament Fan
      M581 T2 P8 S1 R0 ; Invoke trigger 2 when an inactive-to-active edge is detected on input 8
      ; Extruder 1
      M308 S1 P"21.temp0" Y"thermistor" T100000 B4725 ; configure sensor 1 as thermistor on pin 121.temp0
      M950 H1 C"21.out0" T1 ; create nozzle heater output on 121.out0 and map it to sensor 1
      M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
      M143 H1 S285 ; set temperature limit for heater 1 to 285C
      ;M307 H1 R3.214 C42.3 D7.77 S0.75 V23.2 ; Tuned
      M307 H1 R0.056 C194.7 D8.90 S1.00 V23.9 ; small block
      ;M307 H1 R3.358 C190.6 D7.20 S0.60 V23.6
      ; Extruder 2
      M308 S2 P"22.temp0" Y"thermistor" T100000 B4725 ; configure sensor 2 as thermistor on pin 122.temp0
      M950 H2 C"22.out0" T2 ; create nozzle heater output on 122.out0 and map it to sensor 2
      M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
      M143 H2 S285 ; set temperature limit for heater 2 to 285C
      ;M307 H2 R3.056 C229.5 D7.91 S0.80 V23.3 ; Tuned
      ;M307 H2 R3.090 C199.8 D7.36 S0.75 V23.3
      ;M307 H2 R3.202 C234.301:234.301 D7.52 S0.70 V23.3 B0 I0
      M307 H2 R3.358 C190.6 D7.20 S0.60 V23.6
      ; *** Fans
      ; Extruder 1 Fan
      M950 F0 C"21.out1" Q500 ; Part cooling fan
      M106 P0 S0 B0.1 H-1 ; Default off. booststart for 0.1s (B0.1); thermostatic control off
      M950 F1 C"21.out2" Q500 ; Hotend cooling fan
      M106 P1 S1 H1 T50 ; Default on. thermistatic control on above 50C
      ; Extruder 2 Fan
      M950 F2 C"22.out1" Q500 ; Part cooling fan
      M106 P2 S0 B0.1 H-1 ; Default off. booststart for 0.1s (B0.1); thermostatic control off
      M950 F3 C"22.out2" Q500 ; Hotend cooling fan
      M106 P3 S0 H2 T50 ; Default on. thermistatic control on above 50C
      ; Tools
      ; Extruder 1 Tool
      M563 P0 S"Extruder-1" D0:1 H1 F0
      M567 P0 E1:1 ; mixing
      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
      G10 P0 X0 Y76 Z0 ; Reset tool axis offsets
      ; Extruder 2 Tool
      M563 P1 S"Extruder-2" D2:3 H2 F2 ; define tool 1
      M567 P1 E1:1 ; mixing
      G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C
      G10 P1 X0 Y76 Z0 ; Reset tool axis offsets
      ; Retraction
      ;M207 S6.5 R0.0 F4800 T4800 Z0.0
      M207 S4 R0.0 F3000 T2100 Z0.4
      ; M207: Set retract length
      ; Parameters
      ; Pn Tool number (optional, supported in RRF 3.01 and later only)
      ; Snnn positive length to retract, in mm
      ; Rnnn positive or negative additional length to un-retract, in mm, default zero
      ; Fnnn retraction feedrate, in mm/min
      ; Tnnn feedrate for un-retraction if different from retraction, mm/min (RepRapFirmware 1.16 and later only)
      ; Znnn additional zlift/hop
      ; Example: M207 S4.0 F2400 Z0.075
      ; FEEDRATE CONVERSIONS
      ; 20mm/s = F1200 ; 100mm/s = F6000
      ; 35mm/s = F2100 ; 120mm/s = F7200
      ; 50mm/s = F3000 ; 133mm/s = F8000
      ; 70mm/s = F4200
      ; * ======= tool offsets ======== *
      ; Set in config-override.g
      ;G10 P0 X0 Y76 Z-21 ; T0
      ;G10 P1 X0 Y76 Z-21 ; T1
      ; Filament monitors
      ; ** Rotating
      M591 P3 C"21.io1.in" D0 R30:160 S1
      M591 P3 C"22.io1.in" D2 R30:160 S1
      ; ** Endstops
      M950 J4 C"!^1.io1.in" ; Input 4 for filament trigger
      M950 J5 C"!^1.io2.in" ; Input 5 for filament trigger
      ; Invoke trigger 1 (M25) when an active-to-inactive edge is detected on input 4 and 5 and a file is being printed from SD card
      M581 T1 P4 S0 R1
      M581 T1 P5 S0 R1
      ; Miscellaneous
      M572 D0 S0.02 ; pressure advance T0
      M572 D1 S0.02 ; pressure advance T1
      ;M572 D2 S0.05 ; pressure advance T2
      ;M572 D3 S0.05 ; pressure advance T3
      ; Set up the dock indicator switches on the tools.
      M950 J0 C"!^io3.in" ; GpIn 3 = tool 0 dock switch
      M950 J1 C"!^io4.in" ; GpIn 4 = tool 1 dock switch
      ; Z Motors brake
      M950 P0 C"0.out1"
      ; Z Motors brake OFF
      G92 Z0
      G91 ; Relative mode
      M400 ; make sure everything has stopped before we change the motor currents
      M913 Z100 ; drop motor currents to 20%
      G1 Z0.05
      M400
      G4 P1000 ; Pause
      M42 P0 S1 ; Brake oFF
      M911 S23.5 R23.8 P"M42 P0 S0"
      G90
      ;M593 F50 ; cancel ringing at 50Hz
      M376 H20 ; bed compensation taper
      M501 ; load saved parameters from non-volatile memory
      ;G29 S1 ; Do not use G29 S1 within config.g, because no Z=0 datum has been established at that point
      G90 ; !!! absolute positioning

      homez:

      ; homez.g
      ; called to home the Z axis
      while iterations < 2
      if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
      M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
      abort
      ;M290 R0 S0 ; clear babystepping
      ;M561 ; clear any bed transform
      G91 ; Relative mode
      M400 ; make sure everything has stopped before we change the motor currents
      ;M913 Z80 ; drop motor currents to 20%
      G1 H2 Z5 F1000 ; Lower the bed
      ;M913 Z100 ; motor currents to 100%
      G90 ; back to absolute positioning
      ;G1 X0 Y0 F9000 ; Position the endstop above the bed centre
      G1 X-473 Y500 F9000 ; Position the endstop near leadscrew
      ;G1 X473 Y500 F9000 ; Position for test
      M400
      ;if move.axes[2].machinePosition > 9
      ; M558 K0 F1000 H3
      ; G30 Z-9999
      M558 K0 F600 H5 A1
      G30 Z-9999
      M558 K0 F120 H5 A5
      G30 Z-9999
      M400
      ;M558 K0 H30
      ;G91 ; Relative mode
      ;G1 Z10 F1000 ; Lower the bed
      ;G90 ; back to absolute positioning

      bed.g (called from homeall.g)

      ; bed.g
      ; Called to align the gantry to the bed plane via G32
      while iterations < 2
      if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
      M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
      abort
      M290 R0 S0 ; clear babystepping
      M561 ; clear any bed transform
      M84 E0:1 ; Turn off noisy Extruder motor
      M400 ; make sure everything has stopped
      M98 P"homez.g"
      M558 K0 H10 F120 ; F120
      M98 P"/macros/Move/bed_level_points"
      ;M98 P"homez.g"
      ;G28 Z
      ;G1 X0 Y0 F12000 ; Position the endstop above the bed centre
      ;M558 F120
      ;G30 Z-9999
      ;M400
      M98 P"homez.g"
      M558 K0 H5

      mesh.g

      ; mesh.g
      if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed || !move.axes[3].homed
      M291 S1 T5 P{"Please Home before probe"} R"Cannot probe"
      abort
      if state.currentTool != -1
      M291 S1 T5 P{"Please return All tools to dock before probing"} R"Cannot probe"
      abort "Cannot do mesh probing when a tool is selected"
      M290 R0 S0 ; clear babystepping
      M561 ; clear any bed transform
      ;G32 ; Level the gantry
      ;M98 P"homez.g"
      ; Heat the bed to 80C
      ;M291 P"Heating up the bed..." R"Probing New Bed Mesh" T5
      ;M190 S80
      ;M116
      ;G32 ; Level the gantry again while everything is hot
      M558 K0 H3 T9000 F120 A5
      G29 S0
      M558 K0 H5 T9000
      M140 S0 ; Turn off bed
      M291 P"Done!" R"Bed Mesh" T5

      homeall.g (G29 S1 here)

      ; homeall.g
      ; called to home all axes
      ;
      M98 P"homex.g"
      M98 P"homey.g"
      M98 P"bed.g"
      G29 S1
      1 Reply Last reply Reply Quote 0
      • undefined
        Phaedrux Moderator
        last edited by 18 Mar 2021, 19:01

        @Dep said in Strange bugs 3.3beta2:

        M98 P"/macros/Move/bed_level_points"

        What's in that macro?

        @Dep said in Strange bugs 3.3beta2:

        M98 P"homex.g" M98 P"homey.g"

        Can you share these as well?

        Can you also share the results of sending M98 P"config.g" and share your slicer start gcode.

        Z-Bot CoreXY Build | Thingiverse Profile

        undefined 1 Reply Last reply 18 Mar 2021, 19:19 Reply Quote 0
        • undefined
          Dep @Phaedrux
          last edited by 18 Mar 2021, 19:19

          @Phaedrux оf course

          bed_level_points :

          G30 P0 X-473 Y500 Z-99999 ;P0 - Probe point 0 (not drive)
          G30 P1 X473 Y500 Z-99999
          G30 P2 X473 Y-500 Z-99999
          G30 P3 X-473 Y-500 Z-99999 S4 ;set correction

          homex.g

          ; homex.g
          ; called to home the X axis
          ;
          while iterations < 2
          if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
          M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
          abort
          G91 ; relative positioning
          M400 ; make sure everything has stopped before we change the motor currents
          ;M913 Z80 ; drop motor currents to 20%
          G1 H2 Z5 F6000 ; lift Z relative to current position
          ;M913 Z100 ; motor currents to 100%
          G1 H1 X-1200 F6000 ; move quickly to X axis endstop and stop there (first pass)
          G1 H2 X5 F6000 ; go back a few mm
          G1 H1 X-1200 F360 ; move slowly to X axis endstop once more (second pass)
          G1 H2 X5 F6000 ; move away from end
          G1 H2 Z-5 F6000 ; up Z again
          G90 ; absolute positioning

          homey.g

          ; homey.g
          ; called to home the Y axis
          ;
          while iterations < 2
          if iterations < #sensors.gpIn && sensors.gpIn[iterations] != null && sensors.gpIn[iterations].value = 0
          M291 S1 T5 P{"Please return tool "^iterations^" to dock before homing"} R"Cannot home"
          abort
          if !move.axes[0].homed
          M98 P"homex.g"
          G91 ; relative positioning
          M400 ; make sure everything has stopped before we change the motor currents
          ;M913 Z80 ; drop motor currents to 20%
          G1 H2 Z5 F6000 ; lift Z relative to current position
          ;M913 Z100 ; motor currents to 100%
          G1 H1 Y1205 F6000 ; move quickly to Y axis endstop and stop there (first pass)
          G1 H2 Y-5 F6000 ; go back a few mm
          G1 H1 Y1205 F360 ; move slowly to Y axis endstop once more (second pass)
          G1 H2 Y-50 F6000 ; move away from end
          G1 H2 Z-5 F6000 ; up Z again
          G90 ; absolute positioning

          Slicer (S3D) start code:

          ; START code
          M140 S[bed0_temperature]
          M106 S0 ;fan off
          G92 E0; reset extruder distance
          G28
          T0 ; Select tool 0
          M116
          G10 P0 S[extruder0_temperature] R160
          M116
          M98 P"/macros/Purge Filament"
          ;--- end start gcode ---
          1 Reply Last reply Reply Quote 0
          • undefined
            Dep
            last edited by Dep 18 Mar 2021, 19:20

            @Phaedrux said in Strange bugs 3.3beta2:

            M98 P"config.g"

            18.03.2021, 22:24:45 M98 P"config.g"
            HTTP is enabled on port 80
            FTP is disabled
            TELNET is disabled
            1 Reply Last reply Reply Quote 0
            • undefined
              Phaedrux Moderator
              last edited by 18 Mar 2021, 20:50

              @Dep said in Strange bugs 3.3beta2:

              M376 H20 ; bed compensation taper

              With a taper set the amount moved to compensate is diminished over the duration of the print and for small amounts can make it very hard to see.

              Can you post a screenshot showing your heightmap?

              How often do you re-create the heightmap?

              Z-Bot CoreXY Build | Thingiverse Profile

              undefined 1 Reply Last reply 19 Mar 2021, 10:18 Reply Quote 0
              • undefined
                Dep
                last edited by 19 Mar 2021, 10:14

                2021-03-19_13-09-59.png

                I've done it many times. The print shows that the compensation does not work. I also attach a long stick to the pulley to check if there is movement or not.

                If necessary, I can shoot a video.

                1 Reply Last reply Reply Quote 0
                • undefined
                  Dep @Phaedrux
                  last edited by 19 Mar 2021, 10:18

                  @Phaedrux said in Strange bugs 3.3beta2:

                  @Dep said in Strange bugs 3.3beta2:

                  M376 H20 ; bed compensation taper

                  With a taper set the amount moved to compensate is diminished over the duration of the print and for small amounts can make it very hard to see.

                  I've tried disabling taper. M376 H0
                  Nothing changes.

                  1 Reply Last reply Reply Quote 0
                  • undefined
                    jay_s_uk
                    last edited by 19 Mar 2021, 10:27

                    add G29 S1 after the G28 in your start script

                    Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                    undefined 1 Reply Last reply 19 Mar 2021, 10:35 Reply Quote 0
                    • undefined
                      Dep @jay_s_uk
                      last edited by 19 Mar 2021, 10:35

                      @jay_s_uk It is added:

                      homeall.g (G29 S1 here)

                      ; homeall.g
                      ; called to home all axes
                      ;
                      M98 P"homex.g"
                      M98 P"homey.g"
                      M98 P"bed.g"
                      G29 S1
                      undefined 1 Reply Last reply 19 Mar 2021, 10:35 Reply Quote 0
                      • undefined
                        jay_s_uk @Dep
                        last edited by 19 Mar 2021, 10:35

                        @Dep ah, missed that

                        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                        1 Reply Last reply Reply Quote 0
                        • undefined
                          Phaedrux Moderator
                          last edited by 19 Mar 2021, 21:41

                          All I can think is that the conditional gcode in your homing files is skipping something.

                          Can you try adding G29 S1 to your slicer start gcode after the purge filament macro?

                          Then check if mesh compensation is active in M122 during the print and see if the Z axis is moving.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            OwenD
                            last edited by 19 Mar 2021, 22:04

                            Could it be that you're not homing Z after you run bed.g ?

                            undefined 1 Reply Last reply 19 Mar 2021, 22:23 Reply Quote 0
                            • undefined
                              Phaedrux Moderator @OwenD
                              last edited by 19 Mar 2021, 22:23

                              @OwenD said in Strange bugs 3.3beta2:

                              Could it be that you're not homing Z after you run bed.g ?

                              Bed.g is getting called as part of homeall. bed.g calls homez.

                              Z-Bot CoreXY Build | Thingiverse Profile

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                Dep
                                last edited by 20 Mar 2021, 07:57

                                The oddities continue. Now there is a problem with the filament monitor: min -5% and printing continues:

                                20.03.2021, 10:39:40 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.37mm/rev, min -5% max 105% over 153582.5mm
                                20.03.2021, 10:32:45 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 151673.8mm
                                20.03.2021, 10:25:49 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 149761.4mm
                                20.03.2021, 10:22:38 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148885.3mm
                                20.03.2021, 10:21:55 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148686.4mm
                                20.03.2021, 10:21:18 M591 d0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 131 agc 107, measured sensitivity 25.36mm/rev, min -5% max 105% over 148515.8mm

                                After the "reset":

                                20.03.2021, 10:52:50 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.51mm/rev, min 97% max 104% over 2092.2mm
                                20.03.2021, 10:50:15 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.51mm/rev, min 97% max 104% over 1380.5mm
                                20.03.2021, 10:48:02 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.53mm/rev, min 97% max 104% over 766.6mm
                                20.03.2021, 10:47:35 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.54mm/rev, min 97% max 104% over 644.5mm
                                20.03.2021, 10:45:52 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.57mm/rev, min 97% max 104% over 171.1mm
                                20.03.2021, 10:45:22 M591 D0
                                Duet3D rotating magnet filament monitor v3 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, version 3, mag 132 agc 107, measured sensitivity 25.57mm/rev, min 97% max 101% over 26.5mm
                                20.03.2021, 10:45:02 M292
                                Printing paused at X-21.7 Y-33.3 Z2.5 C40.0
                                20.03.2021, 10:44:51 Resume state saved
                                20.03.2021, 10:44:24 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:44:14 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:43:53 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:43:39 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:43:19 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:42:57 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:42:43 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:42:34 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, enabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:42:31 M591 d0 s1
                                20.03.2021, 10:42:24 M591 d0
                                Duet3D rotating magnet filament monitor v1 on pin 21.io1.in, disabled, sensitivity 28.80mm/rev, allow 30% to 160%, check every 3.0mm, no data received
                                20.03.2021, 10:42:21 M591 d0 s0

                                All settings are higher in this thread.

                                I ran 170 hours long print. I should have tried to install the old firmware, something is wrong here 😞

                                And a couple of screenshots to tread:
                                IMG_3010.jpg
                                IMG_3013.jpg

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                                • undefined
                                  Dep
                                  last edited by 20 Mar 2021, 08:14

                                  And I already had it. But at that moment
                                  I had one of the extruders disabled on the CAN bus and errors were pouring in. I thought it was because of this.

                                  Last time min was -107% the extruder ended up stuck, but the printer kept printing in air all night.

                                  In general, the filament monitor does not work on this firmware.

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                                  • undefined
                                    Dep
                                    last edited by 20 Mar 2021, 18:40

                                    I installed 3.2.2 firmware - the errors disappeared, the mesh is working, the filament monitor is working.

                                    The printer is printing 5 hours, the flight is normal. So pay attention to what I wrote above.

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                                    • undefined
                                      Phaedrux Moderator
                                      last edited by 20 Mar 2021, 18:56

                                      So it's all working fine in 3.2.2 but has problems with 3.3beta2?

                                      If so I will remove the Solved tag as it still needs to be investigated.

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • undefined
                                        Dep
                                        last edited by 20 Mar 2021, 20:00

                                        The errors that fell on the screen and the problem with the filament sensor disappeared immediately. So yes, this is a beta issue.

                                        As for the mesh calibration, I still do not understand. Now it seems to be working. But it somehow still worked on beta. I recalibrated many times, so I got completely confused.

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                                        • undefined
                                          oliof
                                          last edited by 22 Mar 2021, 08:38

                                          FWIW I see those errors too with a Paneldue, so I removed it for the time being. Machine is down for other reasons right now, so I forgot to report it.

                                          <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

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