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    Homing works, but repeats endlessly (mostly)

    Scheduled Pinned Locked Moved
    Tuning and tweaking
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    • b3njam1nundefined
      b3njam1n @b3njam1n
      last edited by

      @b3njam1n one more note- when I tried to connect to the D3 from the rPi, it would not show up. It completed the flash from windows, and verified. Now I am at a stand.

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      • b3njam1nundefined
        b3njam1n @b3njam1n
        last edited by

        This post is deleted!
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        • b3njam1nundefined
          b3njam1n @Phaedrux
          last edited by

          @phaedrux I think I have lost the power mosfet that provides regulated 12v to the board. I am only getting 3.3-3.6v on V12 according to DWC, and I am receiving an "attempting to move motor while Vin out of range" when I try to move a motor. That seems to be why the 12v fans stopped turning. The external PSU and the power it provides are unaffected, but this duet is probably out of action until I can replace that component. The board is genuine Duet3D, so the part is whatever is specified for a board marked v1.01. It is the mosfet clockwise of the shielded power strip. It says it is a 036N04L GAB830, and when I try to find a replacement at mouser.com it says there is a long lead time. Any chance you guys have one available?

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            What LEDs are lit on the board?

            When and where did you purchase the Duet?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • b3njam1nundefined
              b3njam1n @Phaedrux
              last edited by b3njam1n

              @phaedrux I bought it from filastruder. The three LEDs quite near the reset button are, anticlockwise from the corner, amber, red, green. The diagnostic LED us just flashing at about 1Hz- so normal, I think. Although you didn't ask me for it, here is the output of an M122:
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.2.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9F0-3S46P-9U2LD
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 149788
              Dynamic ram: 62628 of which 0 recycled
              Never used RAM 146416, free system stack 204 words
              Tasks: Linux(ready,122) HEAT(blocked,297) CanReceiv(blocked,927) CanSender(blocked,371) CanClock(blocked,358) TMC(blocked,65) MAIN(running,1203) IDLE(ready,19)
              Owned mutexes: HTTP(MAIN)
              === Platform ===
              Last reset 00:14:15 ago, cause: power up
              Last software reset time unknown, reason: MemoryProtectionFault mmarValid daccViol, FilamentSensors spinning, available RAM 148056, slot 2
              Software reset code 0x416d HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0x00000017 SP 0x2041fc80 Task MAIN Freestk 1710 ok
              Stack: 00000000 00000000 00000000 0000000d 00000100 00468f8b 00452558 61030000 00000000 00000000 00000000 00000000 00000000 00000000 00000000 ffffffff 0000002c 0000001f 20429288 20429a08 00000001 00444b2b 0000000d 2041dbcc 2041b8e8 00452555 00000000
              Error status: 0x00
              Aux0 errors 0,0,0
              Aux1 errors 0,0,0
              MCU temperature: min 14.8, current 29.2, max 29.5
              Supply voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0, over voltage events: 0, power good: no
              12V rail voltage: min 3.8, current 3.9, max 3.9, under voltage events: 0
              Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Date/time: 2021-05-08 00:54:50
              Slowest loop: 1.07ms; fastest: 0.04ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is doing "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === CAN ===
              Messages queued 3330, send timeouts 7607, received 0, lost 0, longest wait 0ms for reply type 0, free buffers 48
              === SBC interface ===
              State: 1, failed transfers: 0
              Last transfer: 0ms ago
              RX/TX seq numbers: 29475/29475
              SPI underruns 0, overruns 0
              Number of disconnects: 0, IAP RAM available 0x2c8a8
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.2.2
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 2.46
              Maximum length of RX/TX data transfers: 3240/744

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              • b3njam1nundefined
                b3njam1n @Phaedrux
                last edited by b3njam1n

                @phaedrux hold on, from the docs, it says " 12V will not be produced if only 12V is provided as VIN." -- perhaps I have not fried that mosfet. Is it normal for V12 to sit at around 3.9v if I am providing 12v to the board from a PSU? I would like to send a screenshot...Capture.JPG

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                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  I'm not exactly sure what's going on. 12v VIN should be within range for the motors to move, so that error message is a little concerning. I've asked DC42 to take a look when he is able.

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    It was trying to home before but looping, and how you've got a VIN out of range error? What transpired immediately before that error?

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • b3njam1nundefined
                      b3njam1n @Phaedrux
                      last edited by

                      @phaedrux I tried the three methods you shared trying to bring DSF in line with RFF on the duet3. First the missing files, and then the bossa flash of the board via USB- I tried from the Pi and it failed, so I flashed it with bossa from a windows box. It completed and verified.

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        And it looks like the firmware was properly applied and the pi is now in sync.

                        Can you show a photo of the board powered up showing the LEDs that are lit?

                        Is the Duet powering the Pi? or the Pi powering the Duet? Or are they independently powered?

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • b3njam1nundefined
                          b3njam1n @Phaedrux
                          last edited by b3njam1n

                          @phaedrux sure just one sec- the Pi is powered by an official adafruit rPi power supply with an added "Pi switch" so I can power it off individually. Taking a pic, just a minute...duet3-board.MP.jpg

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                          • b3njam1nundefined
                            b3njam1n @Phaedrux
                            last edited by

                            @phaedrux oh, and the duet 3 is powered by a 12v 360w psu.

                            droftartsundefined 1 Reply Last reply Reply Quote 0
                            • droftartsundefined
                              droftarts administrators @b3njam1n
                              last edited by

                              @b3njam1n I can see the V_FUSED LED is not lit, and it should be. Can you check the main fuse? It’s the one nearest the power input side of the terminal.

                              Ian

                              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

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                              • b3njam1nundefined
                                b3njam1n @droftarts
                                last edited by b3njam1n

                                @droftarts I pulled each of the two blue blade fuses by the shielded power strip, tested each for continuity, and both passed. Are there test points where I could get meter readings that would help in your diagnosis?

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  Would you be able to remove the board entirely and get a good clear well lit shot of the board with close ups in case we can spot a damaged component?

                                  Z-Bot CoreXY Build | Thingiverse Profile

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                                  • b3njam1nundefined
                                    b3njam1n @Phaedrux
                                    last edited by

                                    @phaedrux Yes, absolutely, but I am not at home at the moment. I will put it on a contrasting background and take several shots with different lighting at the highest resolution I can to get the final under the upload size cap. It might be few hours, though.

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                                    • b3njam1nundefined
                                      b3njam1n @Phaedrux
                                      last edited by

                                      This post is deleted!
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                                      • b3njam1nundefined
                                        b3njam1n @Phaedrux
                                        last edited by

                                        @phaedrux just let me know if you want a close look at any specific part of the board, and I will get another image to you quickly. Here are some shots from different angles that should do the trick:
                                        PXL_20210509_153852494.jpg

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                                        • b3njam1nundefined
                                          b3njam1n @Phaedrux
                                          last edited by

                                          @phaedrux can you please boost me to a 1 reputation so I don't have to wait 60 secs between posts?
                                          PXL_20210509_153859450.jpg

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                                          • b3njam1nundefined
                                            b3njam1n @Phaedrux
                                            last edited by

                                            @phaedrux PXL_20210509_153907210.jpg

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