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    Same .gcode file - two different printers - very different results

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    Tuning and tweaking
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    • Sinkundefined
      Sink
      last edited by

      Tried a jog of +100 and measured 65 mm change.. Will repeat .. Pretty much same result ..
      Could this be a current problem to the Z steppers (2)

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      • Sinkundefined
        Sink
        last edited by

        Looking to find your answers .. Have to find the old marlin code .. and of course it is not on this computer .. will be back when I have the answers .. I believe the P3 came with M5x295 screw rods if that helps ..

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        • dc42undefined
          dc42 administrators
          last edited by

          It could be that your Z steps/mm are wrong, or your X acceleration is too high, or your Z maximum speed is too high, or the Z motor current is too low. You should be able to get all of these details except the motor current from your Marlin config file.

          One other possibility: if you have two Z motors and they are badly-chosen high inductance low current types, then the series connection used by the two Z motors connectors on the Duet won't work well with them, and you will need to connect them in parallel instead. Can you read the model number of the Z motors from the label?

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

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          • Sinkundefined
            Sink
            last edited by

            Some numbers :

            Steppers SL42STH40-1684A

            MARLIN:

            DefaultAxisStepsPerUnit 80,80,4000, 775 – the 4000 looks bigger than the config val

            Default Acceleration 3000

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            • Sinkundefined
              Sink
              last edited by

              Yup z Steps are set to 2560 .. try a change to 4000?

              Ratios look about right for measurements ..
              warmin up for a test print ..

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              • number40fanundefined
                number40fan
                last edited by

                If you got a 65mm change when commanding 100, then 4000 will get you close.

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                • number40fanundefined
                  number40fan
                  last edited by

                  BTW, your pictures in this post and another you posted in, are not working.

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                  • Sinkundefined
                    Sink
                    last edited by

                    It is printing .. hopeful .. damn, you guys are good ..

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                    • dc42undefined
                      dc42 administrators
                      last edited by

                      Glad you sorted it. Those steppers are good for plugging directly into the 2 Z motor sockets on the Duet. 1000mA current in the M906 command would be about right.

                      Duet WiFi hardware designer and firmware engineer
                      Please do not ask me for Duet support via PM or email, use the forum
                      http://www.escher3d.com, https://miscsolutions.wordpress.com

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                      • Sinkundefined
                        Sink
                        last edited by

                        Print looks much better .. still not perfect but closer, do a few more calcs and adjusts.. will up the current to 1000 in M906 and increase the extruder steps for the titan and the 0.9 motor .and keep trying . Thanks again all ..

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