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    BLT on Duet wifi problem

    Scheduled Pinned Locked Moved Solved
    Tuning and tweaking
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    • engikeneerundefined
      engikeneer @gibsea402
      last edited by

      @gibsea402 sounds like your issue is occurring when you are homing? Please post your homing files (home, homey, homez and homeall) so we can see what's going on

      PS, if you use the code snippet feature on the forum, it makes your code files easier for people to read. It's the </> button at the top (near bold/italic).

      E3D TC with D3Mini and Toolboards.
      Home-built CoreXY, Duet Wifi, Chimera direct drive, 2x BMG, 300x300x300 build volume
      i3 clone with a bunch of mods

      gibsea402undefined 1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Did you update your deploy and retract macros? Please post those.
        Also test if M401 and M402 work to deploy and retract the pin.

        And for good measure include the results of sending M122 and M98 P"config.g"

        Z-Bot CoreXY Build | Thingiverse Profile

        gibsea402undefined 1 Reply Last reply Reply Quote 0
        • gibsea402undefined
          gibsea402 @engikeneer
          last edited by

          @engikeneer

          ; homeall.g
          ; called to home all axes
          ;
          ; generated by RepRapFirmware Configuration Tool v3.3.6 on Fri Nov 26 2021 13:06:38 GMT+0100 (Centraleuropæisk normaltid)
          G91                     ; relative positioning
          G1 H2 Z5 F6000          ; lift Z relative to current position
          G1 H1 X-335 Y-341 F1800 ; move quickly to X or Y endstop and stop there (first pass)
          G1 H1 X-335             ; home X axis
          G1 H1 Y-341             ; home Y axis
          G1 X5 Y5 F6000          ; go back a few mm
          G1 H1 X-335 F360        ; move slowly to X axis endstop once more (second pass)
          G1 H1 Y-341             ; then move slowly to Y axis endstop
          G1 H1 Z-395 F360        ; move Z down stopping at the endstop
          G90                     ; absolute positioning
          G92 Z0                  ; set Z position to axis minimum (you may want to adjust this)
          
          ; Uncomment the following lines to lift Z after probing
          ;G91                    ; relative positioning
          ;G1 Z5 F100             ; lift Z relative to current position
          ;G90                    ; absolute positioning
          

          Here is the home all. Thanks for the tip on the code mode.

          A Former User? engikeneerundefined 2 Replies Last reply Reply Quote 0
          • A Former User?
            A Former User @gibsea402
            last edited by A Former User

            This post is deleted!
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            • engikeneerundefined
              engikeneer @gibsea402
              last edited by

              @gibsea402 This is the section of your homeall that you want to change

              G1 H1 Z-395 F360        ; move Z down stopping at the endstop
              G90                     ; absolute positioning
              G92 Z0                  ; set Z position to axis minimum (you may want to adjust this)
              

              It is using a G1 H1 homing move for Z (i.e. using an endstop which you don't have!), rather than a probing move using the BLTouch. For this you would want to use a G30 probing move (https://duet3d.dozuki.com/Wiki/G30)

              So, I would suggest replacing those three lines of code with:

              G90    ; set absolute positioning
              G1 X150 Y150 F1800   ; move quickly to bed centre - May need to change the X/Y values to suit your printer size
              G30  ; probe with BLTouch
              

              You'll see that these commands are in @Arnold_R_Clark's homeall file (though he also has a bunch of extra stuff which may confuse things).

              E3D TC with D3Mini and Toolboards.
              Home-built CoreXY, Duet Wifi, Chimera direct drive, 2x BMG, 300x300x300 build volume
              i3 clone with a bunch of mods

              gibsea402undefined 1 Reply Last reply Reply Quote 2
              • gibsea402undefined
                gibsea402 @Phaedrux
                last edited by

                @phaedrux
                Hi here is the following. I think the issue is that the macro is not updated. But i am not sure how to do that.

                Pin down: M280 P3 S10 I1
                Pin Up: M280 P3 S90 I1 ; retract BLTouch

                If i click on the macros in the web browser they do not work. But if i send the commands M401 and M402 they work.

                Result of M122:

                M122
                === Diagnostics ===
                RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later
                Used output buffers: 3 of 24 (23 max)
                === RTOS ===
                Static ram: 23876
                Dynamic ram: 75312 of which 148 recycled
                Never used RAM 15080, free system stack 184 words
                Tasks: NETWORK(ready,13.7%,227) HEAT(delaying,0.0%,314) Move(notifyWait,0.1%,364) MAIN(running,86.2%,387) IDLE(ready,0.0%,29), total 100.0%
                Owned mutexes: WiFi(NETWORK)
                === Platform ===
                Last reset 00:04:06 ago, cause: power up
                Last software reset at 2021-11-30 16:41, reason: User, GCodes spinning, available RAM 12148, slot 1
                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                Error status: 0x08
                Aux0 errors 0,0,0
                Step timer max interval 0
                MCU temperature: min 29.4, current 29.9, max 30.2
                Supply voltage: min 23.8, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                Driver 0: position 0, standstill, SG min/max not available
                Driver 1: position 0, standstill, SG min/max not available
                Driver 2: position 0, standstill, SG min/max not available
                Driver 3: position 0, standstill, SG min/max not available
                Driver 4: position 0, standstill, SG min/max not available
                Driver 5: position 0
                Driver 6: position 0
                Driver 7: position 0
                Driver 8: position 0
                Driver 9: position 0
                Driver 10: position 0
                Driver 11: position 0
                Date/time: 2021-11-30 16:56:35
                Cache data hit count 4294967295
                Slowest loop: 5.02ms; fastest: 0.17ms
                I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                === Storage ===
                Free file entries: 10
                SD card 0 detected, interface speed: 20.0MBytes/sec
                SD card longest read time 1.3ms, write time 0.0ms, max retries 0
                === Move ===
                DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                === MainDDARing ===
                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === AuxDDARing ===
                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === Heat ===
                Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP is idle in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                Daemon is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty.
                === Network ===
                Slowest loop: 200.17ms; fastest: 0.08ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                HTTP sessions: 1 of 8
                - WiFi -
                Network state is active
                WiFi module is connected to access point 
                Failed messages: pending 0, notready 0, noresp 2
                WiFi firmware version 1.26
                WiFi MAC address d8:bf:c0:fc:2a:7e
                WiFi Vcc 3.39, reset reason Turned on by main processor
                WiFi flash size 4194304, free heap 25784
                WiFi IP address 192.168.87.164
                WiFi signal strength -50dBm, mode 802.11n, reconnections 0, sleep mode modem
                Clock register 00002002
                Socket states: 0 0 0 0 0 0 0 0
                

                Results of M98:

                M98 P"config.g"
                HTTP is enabled on port 80
                FTP is disabled
                TELNET is disabled
                Error: Pin 'fan1' is not free
                Error: Fan number 2 not found
                Warning: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 205C
                

                Hope you can help me 🙂

                Phaedruxundefined 1 Reply Last reply Reply Quote 0
                • gibsea402undefined
                  gibsea402 @engikeneer
                  last edited by

                  @engikeneer

                  This seem to work. But if i just give the g30 command the probe is not deploying.

                  1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator @gibsea402
                    last edited by

                    @gibsea402 said in BLT on Duet wifi problem:

                    If i click on the macros in the web browser they do not work. But if i send the commands M401 and M402 they work.

                    Which macros exactly are you clicking on? M401 and M402 call the deployprobe.g and retractprobe.g files in the /sys folder

                    Pin down: M280 P3 S10 I1
                    Pin Up: M280 P3 S90 I1 ; retract BLTouch

                    Those are incorrect for RRF3. Remove the I1 and instead of P3 you'd use P0 since you are using servo pin 0

                    M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch

                    Z-Bot CoreXY Build | Thingiverse Profile

                    gibsea402undefined 2 Replies Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @gibsea402
                      last edited by

                      @gibsea402 said in BLT on Duet wifi problem:

                      M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                      M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on
                      M950 F2 C"fan1" Q500 ; create fan 2 on pin fan1 and set its frequency
                      M106 P2 S1 H1 T45 ; set fan 2 value. Thermostatic control is turned on

                      One of those fan1 should be fan2

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • gibsea402undefined
                        gibsea402 @Phaedrux
                        last edited by

                        @phaedrux

                        In the macro folder on the web control site

                        1 Reply Last reply Reply Quote 0
                        • gibsea402undefined
                          gibsea402 @Phaedrux
                          last edited by

                          @phaedrux

                          Thanks! this helped alot! its all working now 🙂

                          1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined Phaedrux marked this topic as a question
                          • Phaedruxundefined Phaedrux has marked this topic as solved
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